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37-129-26923

Well Details

Well ID: 37-129-26923
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Country: United States
State: Pennsylvania
County: Westmoreland
Municipality: South Huntingdon Township
Operator Name: BARON GROUP INC
Well Pad ID:
Farm/Lease Name: J C MARTINI 1
License Status: ACTIVE
Spud Date:
Permit Date: 2007-05-09
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.173551
Longitude: -79.672164

For data sources see[1][2][3]

Well History

Date Event
2007-05-09 New Permit Application
2007-08-15 Performed Spud Operation
2007-08-20 Drilling Completion
2009-09-15 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2007 BARON GROUP INC 0.00 0 0.00 0 0.00 0
2008 BARON GROUP INC 12633.00 365 0.00 0 0.00 0
2009 BARON GROUP INC 4558.91 365 0.00 0 0.00 0
2010 BARON GROUP INC 2,663.89 365 0.00 0 0.00 0
2011 BARON GROUP INC 3,163.33 334 0.00 0 0.00 0
2012 BARON GROUP INC 1,968.00 366 0.00 0 0.00 0
2013 BARON GROUP INC 2,157.04 365 0.00 0 0.00 0
2014 BARON GROUP INC 1,115.41 365 0.00 0 0.00 0
2015 BARON GROUP INC 5.00 2 0.00 0 0.00 0
2016 BARON GROUP INC 0.00 0 0.00 0 0.00 0
2017 BARON GROUP INC 35.00 3 0.00 0 0.00 0
2018 BARON GROUP INC 976.00 365 0.00 0 0.00 0
2019 BARON GROUP INC 262.00 338 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1648620 Primary Facility 2007-08-20 Drilling/Alteration No Violations Noted PIT/FREEBOARD, E&S CONTROLS IN PLACE AND OK.
1648622 Primary Facility 2007-08-23 Drilling/Alteration No Violations Noted PIT/FREEBOARD, E&S CONTROLS IN PLACE AND OK.
1834831 Primary Facility 2009-10-09 Routine/Complete Inspection No Violations Noted WELL IS PRODUCING, TANK DRYER AND METER ALL IN GOOD CONDITION. WELL HEAD LEAKING AT SWEDGE NIPPLE, SITE RESTORED.
1835592 Primary Facility 2009-10-13 Routine/Complete Inspection No Violations Noted Drilling was completed on 8/20/2007. Well site has been restored. There are no signs of erosion and sedimentation on the access road and well site. The tank on-site is in sound condition. Operator should continue to monitor the well site and access road for erosion and sedimentation. Approximately 98% perrenial vegetative cover. Recommend the operator remove the pile of old filter fabric fence that is next to the brine tank.
1880632 Primary Facility 2010-04-12 Routine/Complete Inspection No Violations Noted tag e/s ok, tank removed from site

For data sources see[6]

References