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Difference between revisions of "37-063-30797"

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== Well Details ==
 
== Well Details ==
{| class="wikitable" width="95%"
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{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-063-30797
 
| Well ID: 37-063-30797
| style="width: 50%; height=100%; align=center" rowspan="14" | {{#display_map: 40.452612, -79.190155 | width=100% | height=100% }}  
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| style="height=100%; align=center" rowspan="14" | {{#display_map: 40.452612, -79.190155 | width=100% | height=100% }}  
 
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| Operator Name: [[XTO ENERGY INC]]
 
| Operator Name: [[XTO ENERGY INC]]

Revision as of 20:42, 28 June 2014

Well Details

Well ID: 37-063-30797
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Operator Name: XTO ENERGY INC
First Permit Date: 1993-12-07
Last Permit Date: 1993-12-07
Spud Date: 1993-12-31
Unconventional: No
Horizontal: No
Violations: None
Latitude: 40.452612
Longitude: -79.190155

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2013-0 2650.0 365.0 0.0 0.0 0.0 0.0
2012-0 2740.0 366.0 0.0 0.0 0.0 0.0
2011-0 3106.0 363.0 0.0 0.0 0.0 0.0
2010-0 3191.0 365.0 0.0 0.0 0.0 0.0
2009-0 3518.0 365.0 0.0 0.0 0.0 0.0
2008-0 3742.0 366.0 0.0 0.0 0.0 0.0
2007-0 4581.0 365.0 0.0 0.0 0.0 0.0
2006-0 4944.0 365.0 0.0 0.0 0.0 0.0
2005-0 5058.0 342.0 0.0 0.0 0.0 0.0
2004-0 6030.0 366.0 0.0 0.0 0.0 0.0
2003-0 7270.0 265.0 0.0 0.0 0.0 265.0
2002-0 2632.0 64.0 0.0 0.0 0.0 0.0
2001-0 5404.0 155.0 0.0 0.0 0.0 0.0
2000-0 2658.0 59.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2003-0 BRINE 0.0 Bbl BRINE OR INDUSTRIAL WASTE TREATMENT PLT PHILLIPS PROD / PC EXPL BRINE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
566146 1994-03-24 No Violations Noted E&S OK; TANK
1863341 2010-02-03 No Violations Noted According to records, operator completed the well on 1/24/94 to depth of 3867ft. Well head consisted of 8¿ pipe to 4¿ to 2¿ production pipe with shut off valves. Production equipment consisted of separator; totalize meter (75916 MCF) and 100 bbl brine tank (with 20 bbl fluid). At the time of inspection, no IW and E&S issues at the site. No sign of gas leakage around pipe fitting at well head was noted.

References