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Difference between revisions of "34-029-61323"

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__TOC__
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__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-029-61323
 
| Well ID: 34-029-61323
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.8459713, -81.02730469 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.84, -81.02 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Columbiana County, Ohio|Columbiana]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Columbiana_County,_Ohio|Columbiana]]
 +
|-
 +
| Municipality: [[Knox_Township,_Columbiana_County,_Ohio|Knox Township]]
 
|-
 
|-
 
| Operator Name: [[HISTORIC OWNER]]
 
| Operator Name: [[HISTORIC OWNER]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: HINEBACH LOUIS
 
|-
 
|-
| First Permit Date:  
+
| License Status: Orphan Well - Ready
 
|-
 
|-
| Last Permit Date:  
+
| License Date:  
 
|-
 
|-
 
| Spud Date:  
 
| Spud Date:  
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:
 +
|-
 +
| Final Drill Date: 1925-01-01
 +
|-
 +
| Well Total Depth:  
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status:  
+
| Latitude: 40.840000
 +
|-
 +
| Longitude: -81.020000
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| Completed
 +
| 1925-01-01
 +
 
|-
 
|-
| Violations: 0
+
| Reached Total Depth
 +
| 1925-01-01
 +
 
|-
 
|-
| Latitude: 40.8459713
+
| Changed to  Orphan Well Ready
 +
| 2019-03-25
 +
| Changed Well To Orphan Ready
 
|-
 
|-
| Longitude: -81.02730469
+
| Record Last Modified
 +
| 2019-03-25
 +
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 +
<!--== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 +
<!--== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
+
|-
!scope="col" | VIOLATION COMMENT
+
| 0341594029
 +
| 2015-06-23
 +
| Production Wells
 +
| No Violations
 +
| My inspection found the well to be equipped with a shackle line run pumpjack, 8 casing, 6.25 production casing, 2.375 tubing and rods. The shackle lines have been removed from the well. The tank battery consists of a 210 BBL production tank. The tank battery is being shared by 6 Berea wells on the property. There is no identification on the well or the tank battery. The well is easily accessed by a lease road and a open field.
 
|-
 
|-
| 603438196
+
| 0603438196
 
| 2004-04-26
 
| 2004-04-26
|  
+
| Production Wells
 +
| Violations Noted
 
| The tank battery is shared with permits 61320, 61321, 61322, 61319 and 61318 and consists of 10100 bbl storage tank.
 
| The tank battery is shared with permits 61320, 61321, 61322, 61319 and 61318 and consists of 10100 bbl storage tank.
 +
|-
 +
| 341594029
 +
| 2015-6-23 0:00:
 +
| PW
 +
| No Violations
 
|  
 
|  
 +
|-
 +
| 603438196
 +
| 2004-4-26 0:00:
 +
| PW
 +
| No Violations
 +
| 3.00
 +
|-
 +
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
| 0603438196
 +
| US-OH-126801
 +
| 2004-04-30
 
|  
 
|  
|  
+
| Well shall be plugged
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 20:45, 11 January 2021

Well Details

Well ID: 34-029-61323
Loading map...
Country: United States
State: Ohio
County: Columbiana
Municipality: Knox Township
Operator Name: HISTORIC OWNER
Well Pad ID:
Farm/Lease Name: HINEBACH LOUIS
License Status: Orphan Well - Ready
License Date:
Spud Date:
Spud Drilling Contractor:
Final Drill Date: 1925-01-01
Well Total Depth:
Configuration: Vertical
Latitude: 40.840000
Longitude: -81.020000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Completed 1925-01-01
Reached Total Depth 1925-01-01
Changed to Orphan Well Ready 2019-03-25 Changed Well To Orphan Ready
Record Last Modified 2019-03-25

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0341594029 2015-06-23 Production Wells No Violations My inspection found the well to be equipped with a shackle line run pumpjack, 8 casing, 6.25 production casing, 2.375 tubing and rods. The shackle lines have been removed from the well. The tank battery consists of a 210 BBL production tank. The tank battery is being shared by 6 Berea wells on the property. There is no identification on the well or the tank battery. The well is easily accessed by a lease road and a open field.
0603438196 2004-04-26 Production Wells Violations Noted The tank battery is shared with permits 61320, 61321, 61322, 61319 and 61318 and consists of 10100 bbl storage tank.
341594029 2015-6-23 0:00: PW No Violations
603438196 2004-4-26 0:00: PW No Violations 3.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0603438196 US-OH-126801 2004-04-30 Well shall be plugged

For data sources see[3]

References