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Difference between revisions of "34-111-63101"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-111-63101
 
| Well ID: 34-111-63101
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.83716347, -81.20614246 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.83, -81.2 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Monroe County, Ohio|Monroe]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Monroe_County,_Ohio|Monroe]]
 +
|-
 +
| Municipality: [[Malaga_Township,_Monroe_County,_Ohio|Malaga Township]]
 
|-
 
|-
 
| Operator Name: [[NORTHWOOD ENERGY CORP]]
 
| Operator Name: [[NORTHWOOD ENERGY CORP]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: ANKROM
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2014-05-29
 
|-
 
|-
 
| Spud Date:  
 
| Spud Date:  
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:  
 
|-
 
|-
| Configuration: Vertical
+
| Final Drill Date: 1944-07-02
 
|-
 
|-
| Well Status: Final Restoration
+
| Well Total Depth: 1860.00 ft
 
|-
 
|-
| Violations: 0
+
| Configuration: Vertical
 
|-
 
|-
| Latitude: 39.83716347
+
| Latitude: 39.830000
|-
 
| Longitude: -81.20614246
 
 
|-
 
|-
 +
| Longitude: -81.200000
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Well Status
!scope="col" | GAS QUANTITY
+
!scope="col" style="width: 15%;text-align: center"| Well Status Date
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Comment
!scope="col" | CONDENSATE QUANTITY
 
!scope="col" | CONDENSATE PRODUCTION DAYS
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
 
|-
 
|-
| 2008-0
+
| Completed
| style="text-align:right;" | 0.0
+
| 1944-07-02
 
|  
 
|  
 +
|-
 +
| Reached Total Depth
 +
| 1944-07-02
 
|  
 
|  
|
 
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| Change of Owner
 +
| 1999-08-23
 +
| Operator changed from 3735, CHRISTMAN NOVA A to 4695, P P & G OIL
 +
|-
 +
| Change of Owner
 +
| 2010-02-08
 +
| Operator changed from 4695, P P & G OIL to 1634, NORTHWOOD ENERGY CORP
 +
|-
 +
| APP
 +
| 2014-05-29
 +
| Proposed Formations:BEREA, Issued Date:5/29/2014, Expired Date:5/28/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
 
|-
 
|-
| 2009-0
+
| Plugged/Abandoned
| style="text-align:right;" | 0.0
+
| 2014-06-09
 
|  
 
|  
 +
|-
 +
| Construction Permit Expires
 +
| 2016-05-28
 
|  
 
|  
 +
|-
 +
| Record Last Modified
 +
| 2017-02-10
 
|  
 
|  
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 2008
 +
| [[P P & G OIL]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2009
 +
| [[P P & G OIL]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2010
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2011
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2012
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2013
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2010-0
+
| 2014
| style="text-align:right;" | 0.0
+
| [[NORTHWOOD ENERGY CORP]]
|  
+
| style="text-align: right;" | 0.00
|
+
| style="text-align: right;" | 0.00
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| 2011-0
+
| 2008
| style="text-align:right;" | 0.0
+
| [[P P & G OIL]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2009
 +
| [[P P & G OIL]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2012-0
+
| 2010
| style="text-align:right;" | 0.0
+
| [[NORTHWOOD ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 30
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2011
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 24
 +
| style="text-align: right;" |
 
|-
 
|-
| 2013-0
+
| 2012
| style="text-align:right;" | 0.0
+
| [[NORTHWOOD ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2013
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2014-0
+
| 2014
| style="text-align:right;" | 0.0
+
| [[NORTHWOOD ENERGY CORP]]
| style="text-align:right;" | 0.0
+
| Brine
|  
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2020-11-16
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2020-11-16 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
+
|-
!scope="col" | VIOLATION COMMENT
+
| -1943697088
 +
| 2014-9-23 0:00:
 +
| FR
 +
| No Violations
 +
| 0.60
 
|-
 
|-
 
| 1402312250
 
| 1402312250
 
| 2014-06-09
 
| 2014-06-09
|  
+
| Plug / Plug Back
| On 06/03/14 Davis well service moved on location and pulled 1200' of 2'' tubing and rods out of the hole, on 06/04/14 the well was bailed dry, on 06/05/14 Appalachian wireline was brought in to try and recover the 5'' intermediate string set inside the 6.250'' string with a free point being found at 110'. The remainder of the well was then plugged to surface with the hole topped off on 06/09/2014 and the rig moved off location. Historic well completion records indicate 3411163104 & 63101 are backwards, 63104 was a Berea & 63101 was a Keener well.
+
| No Violations
|
+
| On 06/03/14 Davis well service moved on location and pulled 1200 of 2 tubing and rods out of the hole, on 06/04/14 the well was bailed dry, on 06/05/14 Appalachian wireline was brought in to try and recover the 5 intermediate string set inside the 6.250 string with a free point being found at 110. The remainder of the well was then plugged to surface with the hole topped off on 06/09/2014 and the rig moved off location. Historic well completion records indicate 3411163104 & 63101 are backwards, 63104 was a Berea & 63101 was a Keener well.
|
 
|
 
|-
 
 
|-
 
|-
| -1943697088
+
| 1943697088
 
| 2014-09-23
 
| 2014-09-23
|  
+
| Final Restoration
| Final Restoration status check inspection found the well site meets ORC 1509.072 will all equipment removed.
+
| No Violations
|
+
Final Restoration status check inspection found the well site meets ORC 1509.072 will all equipment removed.
|
 
|
 
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 04:03, 12 January 2021

Well Details

Well ID: 34-111-63101
Loading map...
Country: United States
State: Ohio
County: Monroe
Municipality: Malaga Township
Operator Name: NORTHWOOD ENERGY CORP
Well Pad ID:
Farm/Lease Name: ANKROM
License Status: Final Restoration
License Date: 2014-05-29
Spud Date:
Spud Drilling Contractor:
Final Drill Date: 1944-07-02
Well Total Depth: 1860.00 ft
Configuration: Vertical
Latitude: 39.830000
Longitude: -81.200000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Completed 1944-07-02
Reached Total Depth 1944-07-02
Change of Owner 1999-08-23 Operator changed from 3735, CHRISTMAN NOVA A to 4695, P P & G OIL
Change of Owner 2010-02-08 Operator changed from 4695, P P & G OIL to 1634, NORTHWOOD ENERGY CORP
APP 2014-05-29 Proposed Formations:BEREA, Issued Date:5/29/2014, Expired Date:5/28/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2014-06-09
Construction Permit Expires 2016-05-28
Record Last Modified 2017-02-10

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2008 P P & G OIL 0.00 0.00 365
2009 P P & G OIL 0.00 0.00 365
2010 NORTHWOOD ENERGY CORP 0.00 0.00 0
2011 NORTHWOOD ENERGY CORP 0.00 0.00 0
2012 NORTHWOOD ENERGY CORP 0.00 0.00 0
2013 NORTHWOOD ENERGY CORP 0.00 0.00 0
2014 NORTHWOOD ENERGY CORP 0.00 0.00 0

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2008 P P & G OIL Brine 0 365
2009 P P & G OIL Brine 0 365
2010 NORTHWOOD ENERGY CORP Brine 30 0
2011 NORTHWOOD ENERGY CORP Brine 24
2012 NORTHWOOD ENERGY CORP Brine 0 0
2013 NORTHWOOD ENERGY CORP Brine 0 0
2014 NORTHWOOD ENERGY CORP Brine 0 0

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1943697088 2014-9-23 0:00: FR No Violations 0.60
1402312250 2014-06-09 Plug / Plug Back No Violations On 06/03/14 Davis well service moved on location and pulled 1200 of 2 tubing and rods out of the hole, on 06/04/14 the well was bailed dry, on 06/05/14 Appalachian wireline was brought in to try and recover the 5 intermediate string set inside the 6.250 string with a free point being found at 110. The remainder of the well was then plugged to surface with the hole topped off on 06/09/2014 and the rig moved off location. Historic well completion records indicate 3411163104 & 63101 are backwards, 63104 was a Berea & 63101 was a Keener well.
1943697088 2014-09-23 Final Restoration No Violations Final Restoration status check inspection found the well site meets ORC 1509.072 will all equipment removed.

For data sources see[7]

References