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Difference between revisions of "34-173-20571"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-173-20571
 
| Well ID: 34-173-20571
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.1715874, -83.63557786 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.17, -83.63 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Wood County, Ohio|Wood]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Wood_County,_Ohio|Wood]]
 +
|-
 +
| Municipality: [[Bloom_Township,_Wood_County,_Ohio|Bloom Township]]
 
|-
 
|-
 
| Operator Name: [[LANDOWNER GRANT PROGRAM 2007]]
 
| Operator Name: [[LANDOWNER GRANT PROGRAM 2007]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: NEIL CLARK D
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2007-01-19
 
|-
 
|-
 
| Spud Date:  
 
| Spud Date:  
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:  
 +
|-
 +
| Final Drill Date:
 +
|-
 +
| Well Total Depth: 588.00 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Final Restoration
+
| Latitude: 41.170000
 
|-
 
|-
| Violations: 0
+
| Longitude: -83.630000
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 
|-
 
|-
| Latitude: 41.1715874
+
| APP
 +
| 2007-01-19
 +
| Proposed Formations:TRENTON, Issued Date:1/19/2007, Expired Date:1/19/2008 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
 
|-
 
|-
| Longitude: -83.63557786
+
| Construction Permit Expires
 +
| 2008-01-19
 +
 
 +
I&O CN 1997 06 053
 +
|-
 +
| Plugged by Orphan Well Program
 +
| 2008-02-14
 +
| Plugged by Orphan Well Program
 +
|-
 +
| Plugged/Abandoned
 +
| 2008-02-14
 +
 
 +
I&O CN 1997 06 053
 +
|-
 +
| Record Last Modified
 +
| 2013-03-14
 +
 
 +
I&O CN 1997 06 053
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 +
<!--== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 +
<!--== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
 
| 1201121279
 
| 1201121279
 
| 2008-01-23
 
| 2008-01-23
|  
+
| Orphan
 +
| No Violations
 
| Operator drilled approximately 60 feet when water started discharging from hole. Placed 80 feet of plastic 5 inch pipe in 8 inch hole. Cemented between 8 inch and 5 inch casing.. No water discharging from hole at time of inspection. Will return to resume drilling to clean out well.
 
| Operator drilled approximately 60 feet when water started discharging from hole. Placed 80 feet of plastic 5 inch pipe in 8 inch hole. Cemented between 8 inch and 5 inch casing.. No water discharging from hole at time of inspection. Will return to resume drilling to clean out well.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1202923724
 
| 1202923724
 
| 2008-02-13
 
| 2008-02-13
|  
+
| Orphan
 +
| No Violations
 
| Checked well at request of operator. Operator has been working on well for several weeks. Well was cleaned out to depth 588 when bit became stuck and the 2 inch tubing broke at 195 feet. A tool was used to try to retrieve the remaining tubing and bit but only 2 joints came out. A down hole camera was used and showed debris lodging in the 6 inch hole when pulling out from hole. Operator will run 1.5 inch tubing into hole to top of 2 inch tubing and try to run 1.5 inchtubing down outside of 2 inch tubing to depth 588. Cement will be pumped into well to plug well. Discussed procedure with supervisor Jeff Fry.
 
| Checked well at request of operator. Operator has been working on well for several weeks. Well was cleaned out to depth 588 when bit became stuck and the 2 inch tubing broke at 195 feet. A tool was used to try to retrieve the remaining tubing and bit but only 2 joints came out. A down hole camera was used and showed debris lodging in the 6 inch hole when pulling out from hole. Operator will run 1.5 inch tubing into hole to top of 2 inch tubing and try to run 1.5 inchtubing down outside of 2 inch tubing to depth 588. Cement will be pumped into well to plug well. Discussed procedure with supervisor Jeff Fry.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1203005299
 
| 1203005299
 
| 2008-02-14
 
| 2008-02-14
|  
+
| Plug / Plug Back
 +
| No Violations
 
| Operator ran 1.5 inch tubing into 6 inch well and hit 2 inch tubing stuck in well at approximately 237 feet. Could not get 1.5 inch tubing past 2 inch in hole. During drilling, when drill string broke, 9 joints of 21 foot pipe were retreived along with 5 feet of the broken section. After fishing for the 2 inch string an additional 2 sections of pipe were recovered, but the remaining piece of broken pipe was not found. Bob thinks that when the drill string broke that the remaining string on the drill continued down past the broken 2 inch in hole. The broken section of the 2 inch caught next to the 2 inch in the hole. Bob thinks the broken section of 2 inch prevented the 1.5 inch tubing used in reverse grouting to penetrate past the top of the remaing string in the hole.
 
| Operator ran 1.5 inch tubing into 6 inch well and hit 2 inch tubing stuck in well at approximately 237 feet. Could not get 1.5 inch tubing past 2 inch in hole. During drilling, when drill string broke, 9 joints of 21 foot pipe were retreived along with 5 feet of the broken section. After fishing for the 2 inch string an additional 2 sections of pipe were recovered, but the remaining piece of broken pipe was not found. Bob thinks that when the drill string broke that the remaining string on the drill continued down past the broken 2 inch in hole. The broken section of the 2 inch caught next to the 2 inch in the hole. Bob thinks the broken section of 2 inch prevented the 1.5 inch tubing used in reverse grouting to penetrate past the top of the remaing string in the hole.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1203446262
 
| 1203446262
 
| 2008-02-19
 
| 2008-02-19
|  
+
| Administrative Inspection
 +
| No Violations
 
| Voice mail message from Bob Harpster on 2/15/08 indicated that cement in well dropped 60 feet when check in the morning. Three bags of cement were mixed to fill the well. The casing was cut off 4 feet below ground elevation, ID plate attached and pit backfilled.
 
| Voice mail message from Bob Harpster on 2/15/08 indicated that cement in well dropped 60 feet when check in the morning. Three bags of cement were mixed to fill the well. The casing was cut off 4 feet below ground elevation, ID plate attached and pit backfilled.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1207165445
 
| 1207165445
 
| 2008-04-02
 
| 2008-04-02
|  
+
| Final Restoration
 +
| No Violations
 
| Checked site for final restoration. All equipment removed. Farm field in good condition, no significant erosion/rutting. Small pile dirt on top of well site. Well cut off below ground elevation. Final restoration acceptable.
 
| Checked site for final restoration. All equipment removed. Farm field in good condition, no significant erosion/rutting. Small pile dirt on top of well site. Well cut off below ground elevation. Final restoration acceptable.
|
 
|
 
|
 
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2020-11-16
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 11:33, 12 January 2021

Well Details

Well ID: 34-173-20571
Loading map...
Country: United States
State: Ohio
County: Wood
Municipality: Bloom Township
Operator Name: LANDOWNER GRANT PROGRAM 2007
Well Pad ID:
Farm/Lease Name: NEIL CLARK D
License Status: Final Restoration
License Date: 2007-01-19
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth: 588.00 ft
Configuration: Vertical
Latitude: 41.170000
Longitude: -83.630000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2007-01-19 Proposed Formations:TRENTON, Issued Date:1/19/2007, Expired Date:1/19/2008 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Construction Permit Expires 2008-01-19

I&O CN 1997 06 053

Plugged by Orphan Well Program 2008-02-14 Plugged by Orphan Well Program
Plugged/Abandoned 2008-02-14

I&O CN 1997 06 053

Record Last Modified 2013-03-14

I&O CN 1997 06 053

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1201121279 2008-01-23 Orphan No Violations Operator drilled approximately 60 feet when water started discharging from hole. Placed 80 feet of plastic 5 inch pipe in 8 inch hole. Cemented between 8 inch and 5 inch casing.. No water discharging from hole at time of inspection. Will return to resume drilling to clean out well.
1202923724 2008-02-13 Orphan No Violations Checked well at request of operator. Operator has been working on well for several weeks. Well was cleaned out to depth 588 when bit became stuck and the 2 inch tubing broke at 195 feet. A tool was used to try to retrieve the remaining tubing and bit but only 2 joints came out. A down hole camera was used and showed debris lodging in the 6 inch hole when pulling out from hole. Operator will run 1.5 inch tubing into hole to top of 2 inch tubing and try to run 1.5 inchtubing down outside of 2 inch tubing to depth 588. Cement will be pumped into well to plug well. Discussed procedure with supervisor Jeff Fry.
1203005299 2008-02-14 Plug / Plug Back No Violations Operator ran 1.5 inch tubing into 6 inch well and hit 2 inch tubing stuck in well at approximately 237 feet. Could not get 1.5 inch tubing past 2 inch in hole. During drilling, when drill string broke, 9 joints of 21 foot pipe were retreived along with 5 feet of the broken section. After fishing for the 2 inch string an additional 2 sections of pipe were recovered, but the remaining piece of broken pipe was not found. Bob thinks that when the drill string broke that the remaining string on the drill continued down past the broken 2 inch in hole. The broken section of the 2 inch caught next to the 2 inch in the hole. Bob thinks the broken section of 2 inch prevented the 1.5 inch tubing used in reverse grouting to penetrate past the top of the remaing string in the hole.
1203446262 2008-02-19 Administrative Inspection No Violations Voice mail message from Bob Harpster on 2/15/08 indicated that cement in well dropped 60 feet when check in the morning. Three bags of cement were mixed to fill the well. The casing was cut off 4 feet below ground elevation, ID plate attached and pit backfilled.
1207165445 2008-04-02 Final Restoration No Violations Checked site for final restoration. All equipment removed. Farm field in good condition, no significant erosion/rutting. Small pile dirt on top of well site. Well cut off below ground elevation. Final restoration acceptable.

For data sources see[3]

References