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Difference between revisions of "34-127-24258"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-127-24258
 
| Well ID: 34-127-24258
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.8016196564, -82.3769077254 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.8, -82.37 | width=100% | height=100% }}
 
|-
 
|-
| County:
+
| Country: United States
 
|-
 
|-
| Municipality:
+
| State: Ohio
 
|-
 
|-
| Operator Name:
+
| County: [[Perry_County,_Ohio|Perry]]
 
|-
 
|-
| Well Pad ID:
+
| Municipality: [[Reading_Township,_Perry_County,_Ohio|Reading Township]]
 
|-
 
|-
| Farm/Lease Name:
+
| Operator Name: [[JOHNSON MIKE]]
 
|-
 
|-
| First Permit Date:
+
| Well Pad ID:  
 
|-
 
|-
| Last Permit Date:
+
| Farm/Lease Name: DENNIS KEITH H & NANCY J
 
|-
 
|-
| Spud Date:
+
| License Status: Final Restoration
 
|-
 
|-
| Unconventional:
+
| License Date: 1978-12-22
 
|-
 
|-
| Horizontal:
+
| Spud Date:  
 
|-
 
|-
| Producing: No
+
| Spud Drilling Contractor:  
 
|-
 
|-
| Violations: 3
+
| Final Drill Date:  
 
|-
 
|-
| Latitude: 39.8016196564
+
| Well Total Depth:  
 
|-
 
|-
| Longitude: -82.3769077254
+
| Configuration: Vertical
 +
|-
 +
| Latitude: 39.800000
 +
|-
 +
| Longitude: -82.370000
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| CO
 +
| 1978-12-22
 +
| 1177  ENERGY DISTRIBUTORS INC  GeoDate  12/22/78
 +
|-
 +
| CO
 +
| 1992-02-05
 +
| 2920  TEXTRON OIL CORP  GeoDate  12/22/78
 +
|-
 +
| CO
 +
| 1994-05-23
 +
| 2573  JOHNSON M & GINGERICH M  GeoDate  12/22/78
 +
|-
 +
| CO
 +
| 1996-04-18
 +
| 5460  JOHNSON MIKE  GeoDate  12/22/78
 +
|-
 +
| APP
 +
| 2012-04-09
 +
| 5460  JOHNSON MIKE Proposed Formation CLINTON Issued Date 4/9/2012 Expired Date 4/9/2014 12:00:00 PM
 +
|-
 +
| Plugged/Abandoned
 +
| 2012-06-14
 +
| NO WELL COMPLETION REPORT. I&O CASE # 1988 04 109 (CLOSED, WELL HAS AN OWNER)
 +
|-
 +
| Record Last Modified
 +
| 2017-02-10
 +
| NO WELL COMPLETION REPORT. I&O CASE # 1988 04 109 (CLOSED, WELL HAS AN OWNER)
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 
== Production Data ==
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Period
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Operator Name
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Gas Quantity (mcf)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Oil Quantity (bbl)
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Production Days
!scope="col" | OIL QUANTITY
+
|-
!scope="col" | OIL PRODUCTION DAYS
+
| 1994
 +
| [[JOHNSON M & GINGERICH M]]
 +
| style="text-align: right;" | 995.00
 +
| style="text-align: right;" | 25.00
 +
| style="text-align: right;" | 245
 +
|-
 +
| 1996
 +
| [[JOHNSON MIKE]]
 +
| style="text-align: right;" | 942.00
 +
| style="text-align: right;" | 11.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1999
 +
| [[JOHNSON MIKE]]
 +
| style="text-align: right;" | 509.00
 +
| style="text-align: right;" | 11.00
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2000
 +
| [[JOHNSON MIKE]]
 +
| style="text-align: right;" | 378.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2002
 +
| [[JOHNSON MIKE]]
 +
| style="text-align: right;" | 448.00
 +
| style="text-align: right;" | 8.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2003
 +
| [[JOHNSON MIKE]]
 +
| style="text-align: right;" | 240.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2004
 +
| [[JOHNSON MIKE]]
 +
| style="text-align: right;" | 216.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2005
 +
| [[JOHNSON MIKE]]
 +
| style="text-align: right;" | 154.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2006
 +
| [[JOHNSON MIKE]]
 +
| style="text-align: right;" | 89.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2007
 +
| [[JOHNSON MIKE]]
 +
| style="text-align: right;" | 84.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2008
 +
| [[JOHNSON MIKE]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2009
 +
| [[JOHNSON MIKE]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2010
 +
| [[JOHNSON MIKE]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2011
 +
| [[JOHNSON MIKE]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 365
 +
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 
== Waste Data ==
 
== Waste Data ==
{| class="wikitable sortable" width="95%"
+
{| class="wikitable sortable"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Period
!scope="col" | TYPE
+
!scope="col" style="text-align: center"| Operator Name
!scope="col" | QUANTITY
+
!scope="col" style="text-align: center"| Waste Type
!scope="col" | UNITS
+
!scope="col" style="text-align: center"| Quantity (bbl)
!scope="col" | DISPOSAL METHOD
+
!scope="col" style="text-align: center"| Production Days
!scope="col" | WASTE FACILITY PERMIT ID
+
|-
!scope="col" | WASTE FACILITY NAME
+
| 1994
!scope="col" | FACILITY CITY
+
| [[JOHNSON M & GINGERICH M]]
!scope="col" | FACILITY STATE
+
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 245
 +
|-
 +
| 1996
 +
| [[JOHNSON MIKE]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1999
 +
| [[JOHNSON MIKE]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" |
 +
|-
 +
| 2000
 +
| [[JOHNSON MIKE]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" |
 +
|-
 +
| 2002
 +
| [[JOHNSON MIKE]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2003
 +
| [[JOHNSON MIKE]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2004
 +
| [[JOHNSON MIKE]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2005
 +
| [[JOHNSON MIKE]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2006
 +
| [[JOHNSON MIKE]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2007
 +
| [[JOHNSON MIKE]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2008
 +
| [[JOHNSON MIKE]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2009
 +
| [[JOHNSON MIKE]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2010
 +
| [[JOHNSON MIKE]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2011
 +
| [[JOHNSON MIKE]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION_COMMENT
 
 
|-
 
|-
 
| -1119966797
 
| -1119966797
| 2012-06-04
+
| 2012-6-4 0:00:0
|
+
| PB
| Dozer on site clearing woods in preparation of the rig moving in. They plan on removing tubing on 6/05/2012. Tubing pulled, waiting on clay to arrive.
+
| No Violations
|
+
| 5.00
|
 
|
 
|-
 
 
|-
 
|-
 
| -1333970568
 
| -1333970568
| 2012-06-08
+
| 2012-6-8 0:00:0
|
+
| PB
| Rip plug set, 500 feet,  removed 72 joints of 4.5'' casing, 2390.4 feet. Precast concrete plug set at 1056 feet.
+
| No Violations
|
+
| 5.00
|
 
|
 
|-
 
 
|-
 
|-
 
| -1477695678
 
| -1477695678
| 2012-06-13
+
| 2012-6-13 0:00:
|
+
| PB
| MH well service running clay into 8'' casing.
+
| No Violations
|
+
| 3.00
|
 
|
 
|-
 
 
|-
 
|-
 
| -1812202165
 
| -1812202165
| 2012-02-28
+
| 2012-2-28 0:00:
|
+
| PW
| The inspection revealed well is capable of producing, appears to be a gas well, valves are open on well head.  No production reported to the Division since 2007. No Identification (ID) at well head. Plug well or place in temporary inactive status. Need full and legible ID at the well head. Failure to comply may result in a forfeiture of Bond or Suspension Order.
+
| No Violations
|
+
|  
| 9-1-03C
 
|
 
 
|-
 
|-
 +
| -2082138786
 +
| 2012-6-14 0:00:
 +
| OR
 +
| No Violations
 +
| 1.00
 
|-
 
|-
| -1812202165
+
| -421744380
| 2012-02-28
+
| 2012-6-12 0:00:
|
+
| PB
| The inspection revealed well is capable of producing, appears to be a gas well, valves are open on well head.  No production reported to the Division since 2007. No Identification (ID) at well head. Plug well or place in temporary inactive status. Need full and legible ID at the well head. Failure to comply may result in a forfeiture of Bond or Suspension Order.
+
| No Violations
|
+
| 5.00
| 9-9-05(A)10
 
|
 
 
|-
 
|-
 +
| -532536849
 +
| 2012-6-11 0:00:
 +
| PB
 +
| No Violations
 +
|
 
|-
 
|-
| -1812202165
+
| 0384093120
| 2012-02-28
+
| 2012-04-16
|
+
| Annular Disposal
| The inspection revealed well is capable of producing, appears to be a gas well, valves are open on well head.  No production reported to the Division since 2007. No Identification (ID) at well head. Plug well or place in temporary inactive status. Need full and legible ID at the well head. Failure to comply may result in a forfeiture of Bond or Suspension Order.
+
| No Violations
|
+
| Follow-up on Compliance Notice, Non-Compliance.
| NONE_
 
|
 
 
|-
 
|-
 +
| 0421744380
 +
| 2012-06-12
 +
| Plug / Plug Back
 +
| No Violations
 +
| MH well service on site, they ran a 8 mandrel to open the 8 casing that was parted, then a spear was used, 20,000 pound of pull, the spear ripped out of the pipe, Dan Goins gave permission the continue plugging with clay.
 
|-
 
|-
| -2082138786
+
| 0532536849
| 2012-06-14
+
| 2012-06-11
|
+
| Plug / Plug Back
| MH well service finished clay plugging operations, hole has been left exposed to allow for settlement.
+
| No Violations
|
+
| MH well service on site, 55 of 8 casing removed, cased parted at 55. The will be using a 8 mandrel on 6/12/2012 to ensure they can attach to the 8 casing to finish removing it.
|
 
|
 
 
|-
 
|-
 +
| 0560455517
 +
| 2012-06-20
 +
| Plug / Plug Back
 +
| No Violations
 +
| Follow-up on Compliance Notice, In-Compliance.
 
|-
 
|-
| -421744380
+
| 1119966797
| 2012-06-12
+
| 2012-06-04
|
+
| Plug / Plug Back
| MH well service on site, they ran a 8'' mandrel to open the 8'' casing that was parted, then a spear was used, 20,000 pound of pull, the spear ripped out of the pipe, Dan Goins gave permission the continue plugging with clay.
+
| No Violations
|
+
| Dozer on site clearing woods in preparation of the rig moving in. They plan on removing tubing on 6/05/2012. Tubing pulled, waiting on clay to arrive.
|
 
|
 
|-
 
|-
 
| -532536849
 
| 2012-06-11
 
|
 
| MH well service on site, 55' of 8'' casing removed, cased parted at 55'. The will be using a 8'' mandrel on 6/12/2012 to ensure they can attach to the 8'' casing to finish removing it.
 
|
 
|
 
|
 
 
|-
 
|-
 +
| 1333970568
 +
| 2012-06-08
 +
| Plug / Plug Back
 +
| No Violations
 +
| Rip plug set, 500 feet,  removed 72 joints of 4.5 casing, 2390.4 feet. Precast concrete plug set at 1056 feet.
 
|-
 
|-
 
| 1338989754
 
| 1338989754
 
| 2012-06-06
 
| 2012-06-06
|
+
| Plug / Plug Back
 +
| No Violations
 
| MH well services on site preparing well for bottom hole clay plug. Bottom plug set by 3 PM.
 
| MH well services on site preparing well for bottom hole clay plug. Bottom plug set by 3 PM.
|
 
|
 
|
 
 
|-
 
|-
 +
| 1364704975
 +
| 2012-06-12
 +
| Plug / Plug Back
 +
| No Violations
 +
| Working on ripping 8 casing at this time. Casing has parted at 55ft and will try to reteive more casing.
 
|-
 
|-
 
| 1373553768
 
| 1373553768
 
| 2013-07-09
 
| 2013-07-09
|
+
| Final Restoration
 +
| No Violations
 
| The final restoration meets 1509.072.
 
| The final restoration meets 1509.072.
|
 
|
 
|
 
 
|-
 
|-
 +
| 1477695678
 +
| 2012-06-13
 +
| Plug / Plug Back
 +
| No Violations
 +
| MH well service running clay into 8 casing.
 +
|-
 +
| 1812202165
 +
| 2012-02-28
 +
| Production Wells
 +
| Violations Noted
 +
| The inspection revealed well is capable of producing, appears to be a gas well, valves are open on well head.  No production reported to the Division since 2007. No Identification (ID) at well head. Plug well or place in temporary inactive status. Need full and legible ID at the well head. Failure to comply may result in a forfeiture of Bond or Suspension Order.
 +
|-
 +
| 2082138786
 +
| 2012-06-14
 +
| Orphan
 +
| No Violations
 +
| MH well service finished clay plugging operations, hole has been left exposed to allow for settlement.
 
|-
 
|-
 
| 384093120
 
| 384093120
| 2012-04-16
+
| 2012-4-16 0:00:
|
+
| AD
| Follow-up on Compliance Notice, Non-Compliance.
+
| No Violations
|
+
|  
|
+
|-
|
+
| 560455517
 +
| 2012-6-20 0:00:
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
| 1812202165
 +
| US-OH-117983
 +
| 2012-02-28
 +
|  
 +
| Forfeiture of bond
 
|-
 
|-
 +
| 1812202165
 +
| US-OH-117984
 +
| 2012-02-28
 +
|
 +
| Failure to legibly identify well
 
|-
 
|-
| 560455517
+
| 1812202165
| 2012-06-20
+
| US-OH-117985
|
+
| 2012-02-28
| Follow-up on Compliance Notice, In-Compliance.
+
|  
|
+
| Nonproduction; well shall be plugged or placed in temporary inactive status
|
 
|
 
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
==References==
 +
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 13:14, 12 January 2021

Well Details

Well ID: 34-127-24258
Loading map...
Country: United States
State: Ohio
County: Perry
Municipality: Reading Township
Operator Name: JOHNSON MIKE
Well Pad ID:
Farm/Lease Name: DENNIS KEITH H & NANCY J
License Status: Final Restoration
License Date: 1978-12-22
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 39.800000
Longitude: -82.370000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1978-12-22 1177 ENERGY DISTRIBUTORS INC GeoDate 12/22/78
CO 1992-02-05 2920 TEXTRON OIL CORP GeoDate 12/22/78
CO 1994-05-23 2573 JOHNSON M & GINGERICH M GeoDate 12/22/78
CO 1996-04-18 5460 JOHNSON MIKE GeoDate 12/22/78
APP 2012-04-09 5460 JOHNSON MIKE Proposed Formation CLINTON Issued Date 4/9/2012 Expired Date 4/9/2014 12:00:00 PM
Plugged/Abandoned 2012-06-14 NO WELL COMPLETION REPORT. I&O CASE # 1988 04 109 (CLOSED, WELL HAS AN OWNER)
Record Last Modified 2017-02-10 NO WELL COMPLETION REPORT. I&O CASE # 1988 04 109 (CLOSED, WELL HAS AN OWNER)

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1994 JOHNSON M & GINGERICH M 995.00 25.00 245
1996 JOHNSON MIKE 942.00 11.00 365
1999 JOHNSON MIKE 509.00 11.00 0
2000 JOHNSON MIKE 378.00 0.00 0
2002 JOHNSON MIKE 448.00 8.00 365
2003 JOHNSON MIKE 240.00 0.00 365
2004 JOHNSON MIKE 216.00 0.00 365
2005 JOHNSON MIKE 154.00 0.00 365
2006 JOHNSON MIKE 89.00 0.00 365
2007 JOHNSON MIKE 84.00 0.00 365
2008 JOHNSON MIKE 0.00 0.00 365
2009 JOHNSON MIKE 0.00 0.00 365
2010 JOHNSON MIKE 0.00 0.00 365
2011 JOHNSON MIKE 0.00 0.00 365

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1994 JOHNSON M & GINGERICH M Brine 0 245
1996 JOHNSON MIKE Brine 0 365
1999 JOHNSON MIKE Brine 0
2000 JOHNSON MIKE Brine 0
2002 JOHNSON MIKE Brine 0 365
2003 JOHNSON MIKE Brine 0 365
2004 JOHNSON MIKE Brine 0 365
2005 JOHNSON MIKE Brine 0 365
2006 JOHNSON MIKE Brine 0 365
2007 JOHNSON MIKE Brine 0 365
2008 JOHNSON MIKE Brine 0 365
2009 JOHNSON MIKE Brine 0 365
2010 JOHNSON MIKE Brine 0 365
2011 JOHNSON MIKE Brine 0 365

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1119966797 2012-6-4 0:00:0 PB No Violations 5.00
-1333970568 2012-6-8 0:00:0 PB No Violations 5.00
-1477695678 2012-6-13 0:00: PB No Violations 3.00
-1812202165 2012-2-28 0:00: PW No Violations
-2082138786 2012-6-14 0:00: OR No Violations 1.00
-421744380 2012-6-12 0:00: PB No Violations 5.00
-532536849 2012-6-11 0:00: PB No Violations
0384093120 2012-04-16 Annular Disposal No Violations Follow-up on Compliance Notice, Non-Compliance.
0421744380 2012-06-12 Plug / Plug Back No Violations MH well service on site, they ran a 8 mandrel to open the 8 casing that was parted, then a spear was used, 20,000 pound of pull, the spear ripped out of the pipe, Dan Goins gave permission the continue plugging with clay.
0532536849 2012-06-11 Plug / Plug Back No Violations MH well service on site, 55 of 8 casing removed, cased parted at 55. The will be using a 8 mandrel on 6/12/2012 to ensure they can attach to the 8 casing to finish removing it.
0560455517 2012-06-20 Plug / Plug Back No Violations Follow-up on Compliance Notice, In-Compliance.
1119966797 2012-06-04 Plug / Plug Back No Violations Dozer on site clearing woods in preparation of the rig moving in. They plan on removing tubing on 6/05/2012. Tubing pulled, waiting on clay to arrive.
1333970568 2012-06-08 Plug / Plug Back No Violations Rip plug set, 500 feet, removed 72 joints of 4.5 casing, 2390.4 feet. Precast concrete plug set at 1056 feet.
1338989754 2012-06-06 Plug / Plug Back No Violations MH well services on site preparing well for bottom hole clay plug. Bottom plug set by 3 PM.
1364704975 2012-06-12 Plug / Plug Back No Violations Working on ripping 8 casing at this time. Casing has parted at 55ft and will try to reteive more casing.
1373553768 2013-07-09 Final Restoration No Violations The final restoration meets 1509.072.
1477695678 2012-06-13 Plug / Plug Back No Violations MH well service running clay into 8 casing.
1812202165 2012-02-28 Production Wells Violations Noted The inspection revealed well is capable of producing, appears to be a gas well, valves are open on well head. No production reported to the Division since 2007. No Identification (ID) at well head. Plug well or place in temporary inactive status. Need full and legible ID at the well head. Failure to comply may result in a forfeiture of Bond or Suspension Order.
2082138786 2012-06-14 Orphan No Violations MH well service finished clay plugging operations, hole has been left exposed to allow for settlement.
384093120 2012-4-16 0:00: AD No Violations
560455517 2012-6-20 0:00: PB No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1812202165 US-OH-117983 2012-02-28 Forfeiture of bond
1812202165 US-OH-117984 2012-02-28 Failure to legibly identify well
1812202165 US-OH-117985 2012-02-28 Nonproduction; well shall be plugged or placed in temporary inactive status

For data sources see[7]

References