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Difference between revisions of "37-125-27556"

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Revision as of 18:51, 25 June 2015

Well Details

Well ID: 37-125-27556
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County: Washington
Municipality:
Operator Name: EQT PRODUCTION CO
Well Pad ID:
Farm/Lease Name: HARBISON 592593
First Permit Date:
Last Permit Date: 2015-01-16
Spud Date: 2015-01-24
Unconventional: Yes
Horizontal:
Well Status: ACTIVE
Violations: 0
Latitude: 40.229278
Longitude: -80.031894

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2015-02 0.0 0.0 0.0 0.0 0.0 0.0
2015-01 0.0 0.0 0.0 0.0 0.0 0.0
2015-03 0.0 0.0 0.0 0.0 0.0 0.0

For data sources see[1]

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

For data sources see[2]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
2339091 2015-01-27 No Violations Noted Himes Diversified auger rig Drilled a 24 wellbore and set 20 conductor casing at 40 ft. on 1/24/15.
2348678 2015-02-27 No Violations Noted Alpha Hunter Rig #4 Began moving onto this location on 2/24/15. Resumed drilling at 40 ft. on 2/26/15. The 13 3/8 casing was set at 334 ft. on 2/27/15. Currently at 386 ft. and waiting on cement pump truck after first pump truck broke down. Coal was found from 284 ft. to 292 ft. There were 2 baskets set at 259 ft.
2349856 2015-03-06 No Violations Noted Alpha Hunter Rig #4 The 9 5/8 casing was set at 1571 ft. on 3/1/15 and cemented to surface with 40 bbl.

For data sources see[3]

References