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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-031-22468 | | Well ID: 34-031-22468 | ||
+ | | style="height=100%; align=center" rowspan="15" | {{#display_map: 40.22750232, -82.03268019 | width=100% | height=100% }} | ||
|- | |- | ||
− | | County: | + | | County: [[Coshocton County, Ohio|Coshocton]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[McCOY DOROTHY]] |
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
− | | Spud Date: | + | | Spud Date: |
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | | + | | Well Status: Plugged and Abandoned |
|- | |- | ||
− | | Violations: | + | | Violations: 0 |
|- | |- | ||
− | | Latitude: | + | | Latitude: 40.22750232 |
|- | |- | ||
− | | Longitude: | + | | Longitude: -82.03268019 |
|- | |- | ||
|} | |} | ||
Line 42: | Line 43: | ||
!scope="col" | OIL QUANTITY | !scope="col" | OIL QUANTITY | ||
!scope="col" | OIL PRODUCTION DAYS | !scope="col" | OIL PRODUCTION DAYS | ||
+ | |- | ||
+ | | 1986-0 | ||
+ | | style="text-align:right;" | 2897.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 441.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1987-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 309.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1988-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 168.0 | ||
+ | | | ||
+ | |- | ||
|} | |} | ||
− | + | For data sources see<ref>{{cite web | |
− | + | | title = Ohio Department of Natural Resources RBDMS | |
− | + | | publisher = [http://oilandgas.ohiodnr.gov/] | |
− | + | | date = 2015-06-19 | |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production | |
− | + | | accessdate = 2015-06-20 }}</ref> | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
== Inspection Data == | == Inspection Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 63: | Line 85: | ||
!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
+ | |- | ||
+ | | -1062587964 | ||
+ | | 2014-09-18 | ||
+ | | | ||
+ | | On the day of my inspection Mike Wheeler set a pre-cast cement plug on the 7 casing seat at 1073'. They washed 5 tons of clay down the well and started pulling the 8.625 casing. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
|- | |- | ||
| -1161128232 | | -1161128232 | ||
| 2003-12-09 | | 2003-12-09 | ||
− | | | + | | |
| Well in production . | | Well in production . | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | 201773457 | ||
+ | | 2014-09-22 | ||
+ | | | ||
+ | | On the day of my inspection I found that the well was filled to the surface with clay. It took approximately two tons to fill it up. The casing was still open and had not been cut of yet. The steel plate was made and sitting on top of the well. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| -481963123 | | -481963123 | ||
| 2011-03-07 | | 2011-03-07 | ||
− | | | + | | |
| Well capable of production. | | Well capable of production. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | -495596688 | ||
+ | | 2014-09-15 | ||
+ | | | ||
+ | | On the day of my inspection I found that Mike Wheeler had 1.5 tubing ran inside of 2.875 casing to a depth of 3510'. Cemenco pumped 15 sacks of class A cement for a 400' bottom plug. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 666222251 | ||
+ | | 2014-09-19 | ||
+ | | | ||
+ | | On the day of my inspection I found that Mike Wheeler got 420' of 8.625 casing out of the well. They washed approximately 6.5 tons of clay down the well before filling it to surface. The clay was slowly receding down the well. They were going to let the well sit open over the weekend to let the clay settle. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -772219473 | ||
+ | | 2014-09-17 | ||
+ | | | ||
+ | | Mike Wheeler reported that he parted the 2.875 casing at 1325' and pulled it from the well. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-031-22468 | Loading map...
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County: Coshocton | |
Municipality: | |
Operator Name: McCOY DOROTHY | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Plugged and Abandoned | |
Violations: 0 | |
Latitude: 40.22750232 | |
Longitude: -82.03268019 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1986-0 | 2897.0 | 441.0 | ||||
1987-0 | 0.0 | 309.0 | ||||
1988-0 | 0.0 | 168.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
-1062587964 | 2014-09-18 | On the day of my inspection Mike Wheeler set a pre-cast cement plug on the 7 casing seat at 1073'. They washed 5 tons of clay down the well and started pulling the 8.625 casing. | ||||
-1161128232 | 2003-12-09 | Well in production . | ||||
201773457 | 2014-09-22 | On the day of my inspection I found that the well was filled to the surface with clay. It took approximately two tons to fill it up. The casing was still open and had not been cut of yet. The steel plate was made and sitting on top of the well. | ||||
-481963123 | 2011-03-07 | Well capable of production. | ||||
-495596688 | 2014-09-15 | On the day of my inspection I found that Mike Wheeler had 1.5 tubing ran inside of 2.875 casing to a depth of 3510'. Cemenco pumped 15 sacks of class A cement for a 400' bottom plug. | ||||
666222251 | 2014-09-19 | On the day of my inspection I found that Mike Wheeler got 420' of 8.625 casing out of the well. They washed approximately 6.5 tons of clay down the well before filling it to surface. The clay was slowly receding down the well. They were going to let the well sit open over the weekend to let the clay settle. | ||||
-772219473 | 2014-09-17 | Mike Wheeler reported that he parted the 2.875 casing at 1325' and pulled it from the well. |
For data sources see[2]