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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-155-24075 | | Well ID: 34-155-24075 | ||
− | | style="height=100%; align=center" rowspan="15" | {{#display_map: 41. | + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 41.19572139, -80.77498137 | width=100% | height=100% }} |
|- | |- | ||
− | | County: | + | | County: [[Trumbull County, Ohio|Trumbull]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[AMERICAN WATER MGMT SERV LLC]] |
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
− | | Spud Date: | + | | Spud Date: |
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | | + | | Well Status: Active Injection |
|- | |- | ||
| Violations: 0 | | Violations: 0 | ||
|- | |- | ||
− | | Latitude: 41. | + | | Latitude: 41.19572139 |
|- | |- | ||
− | | Longitude: -80. | + | | Longitude: -80.77498137 |
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|} | |} | ||
== Inspection Data == | == Inspection Data == | ||
Line 64: | Line 42: | ||
!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
+ | |- | ||
+ | | 1098679789 | ||
+ | | 2014-01-16 | ||
+ | | | ||
+ | | A contractor was running a radioactive tracer test. All conditions were acceptable. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
|- | |- | ||
| -1193037062 | | -1193037062 | ||
| 2014-02-11 | | 2014-02-11 | ||
− | | | + | | |
| A mechanical integrity test was performed on the well. 2040 psi. of pressure was placed on the tubing/casing annulus. The test passed without pressure loss. | | A mechanical integrity test was performed on the well. 2040 psi. of pressure was placed on the tubing/casing annulus. The test passed without pressure loss. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | 1228490605 | ||
+ | | 2015-02-13 | ||
+ | | | ||
+ | | The injection well and surface facility were inspected. The well was not in use. There were no violations found at the time. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| -1296066111 | | -1296066111 | ||
| 2014-02-10 | | 2014-02-10 | ||
− | | | + | | |
| The packer installation was witnessed. | | The packer installation was witnessed. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| -130641778 | | -130641778 | ||
| 2014-06-09 | | 2014-06-09 | ||
− | | | + | | |
| The pump was in operation at the time. There were no violations found. | | The pump was in operation at the time. There were no violations found. | ||
− | + | | | |
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− | + | | | |
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− | |||
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− | |||
− | | | ||
− | | | ||
− | | | ||
|- | |- | ||
|- | |- | ||
| 1379950823 | | 1379950823 | ||
| 2013-08-26 | | 2013-08-26 | ||
− | | | + | | |
| I was with UIC Inspector Steven Oaks, Glenda Ostman-Besama ( ODNR ) and Steve Kilper with America Water Management to location various sites to install seismic monitoring stations for there disposal well. | | I was with UIC Inspector Steven Oaks, Glenda Ostman-Besama ( ODNR ) and Steve Kilper with America Water Management to location various sites to install seismic monitoring stations for there disposal well. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 1379959780 | | 1379959780 | ||
| 2013-09-20 | | 2013-09-20 | ||
− | | | + | | |
| The operator was closing the pit. The top of cement around the conductor was approximately two feet from the cellar floor. All conditions were acceptable. | | The operator was closing the pit. The top of cement around the conductor was approximately two feet from the cellar floor. All conditions were acceptable. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | -1384390051 | ||
+ | | 2013-09-12 | ||
+ | | | ||
+ | | Express Energy Services installed a cellar. A corrugated culvert, 8 feet deep and 8 feet in diameter, was grouted in place, using a ready mix truck. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| 1391109016 | | 1391109016 | ||
| 2014-01-29 | | 2014-01-29 | ||
− | | | + | | |
| A roof was on the pump house. There was no work in progress at the time. | | A roof was on the pump house. There was no work in progress at the time. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 1395666950 | | 1395666950 | ||
| 2014-03-04 | | 2014-03-04 | ||
− | | | + | | |
| Northeast Region Supervisor, UIC Inspector Steve Ochs and myself performed a status check on the above location. Tank pad and tanks are under construction. We walked the location. There were no violations noted at this time. | | Northeast Region Supervisor, UIC Inspector Steve Ochs and myself performed a status check on the above location. Tank pad and tanks are under construction. We walked the location. There were no violations noted at this time. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 1402332904 | | 1402332904 | ||
| 2014-05-14 | | 2014-05-14 | ||
− | | | + | | |
| The purpose of this inspection was to review the construction of the surface facility. | | The purpose of this inspection was to review the construction of the surface facility. | ||
My inspection was accompanied by Tom Tomastik and Andrew Adgate. We met with Steve Kilper, with American Water Management Services. | My inspection was accompanied by Tom Tomastik and Andrew Adgate. We met with Steve Kilper, with American Water Management Services. | ||
The surface facility construction was consistent with the facility plan and met all permit specifications. | The surface facility construction was consistent with the facility plan and met all permit specifications. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | 1410188658 | ||
+ | | 2014-07-15 | ||
+ | | | ||
+ | | There were no violations at the time of inspection. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -14835038 | ||
+ | | 2014-07-28 | ||
+ | | | ||
+ | | There were no violations at the time of inspection. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -1550982709 | ||
+ | | 2014-06-20 | ||
+ | | | ||
+ | | A mechanical integrity test on the injection line was witnessed. A pressure of 1680 psi. was placed on the injection line. The test passed with a gain in pressure. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -1827666455 | ||
+ | | 2013-09-13 | ||
+ | | | ||
+ | | I witnessed Express Energy cement the 30 conductor casing using approximately 22 yards grout. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| 2129979424 | | 2129979424 | ||
| 2014-01-09 | | 2014-01-09 | ||
− | | | + | | |
| The operator was moving mud and cuttings inside the drilling pits, in order to make room for cement. The cement will be used to solidify the pits. All conditions were acceptable. | | The operator was moving mud and cuttings inside the drilling pits, in order to make room for cement. The cement will be used to solidify the pits. All conditions were acceptable. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 217938545 | | 217938545 | ||
| 2013-09-13 | | 2013-09-13 | ||
− | | | + | | |
| 40 feet of 30 inch diameter casing was cemented with 8 yards of concrete. Cement operation and site conditions were acceptable. | | 40 feet of 30 inch diameter casing was cemented with 8 yards of concrete. Cement operation and site conditions were acceptable. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | -254408939 | ||
+ | | 2013-09-18 | ||
+ | | | ||
+ | | 100 feet of 20 inch diameter conductor was cemented at 95 feet below ground level, using 260 sacks of Class-A cement with 2% CaCl and 1/2 lb./sk. of cellophane flakes. Cement operation and site conditions were acceptable. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -39750702 | ||
+ | | 2014-09-03 | ||
+ | | | ||
+ | | A sample was taken from the facility. The sample, number SJO-116, was taken to the lab for analysis. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -423600398 | ||
+ | | 2014-11-07 | ||
+ | | | ||
+ | | The well operation has been suspended. There were no additional concerns found. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -477006335 | ||
+ | | 2014-01-03 | ||
+ | | | ||
+ | | The well owner was grading and compacting soil for the surface facility construction. The drilling contractor was moving drilling equipment off the pad. All conditions were acceptable. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -741839577 | ||
+ | | 2014-04-10 | ||
+ | | | ||
+ | | An attempt was made to pressure test the flow line. Equipment was not ready and the test was postponed. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 830340725 | ||
+ | | 2014-11-24 | ||
+ | | | ||
+ | | The well operation has been suspended. No additional concerns were found. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-155-24075 | Loading map...
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County: Trumbull | |
Municipality: | |
Operator Name: AMERICAN WATER MGMT SERV LLC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Active Injection | |
Violations: 0 | |
Latitude: 41.19572139 | |
Longitude: -80.77498137 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1098679789 | 2014-01-16 | A contractor was running a radioactive tracer test. All conditions were acceptable. | ||||
-1193037062 | 2014-02-11 | A mechanical integrity test was performed on the well. 2040 psi. of pressure was placed on the tubing/casing annulus. The test passed without pressure loss. | ||||
1228490605 | 2015-02-13 | The injection well and surface facility were inspected. The well was not in use. There were no violations found at the time. | ||||
-1296066111 | 2014-02-10 | The packer installation was witnessed. | ||||
-130641778 | 2014-06-09 | The pump was in operation at the time. There were no violations found. | ||||
1379950823 | 2013-08-26 | I was with UIC Inspector Steven Oaks, Glenda Ostman-Besama ( ODNR ) and Steve Kilper with America Water Management to location various sites to install seismic monitoring stations for there disposal well. | ||||
1379959780 | 2013-09-20 | The operator was closing the pit. The top of cement around the conductor was approximately two feet from the cellar floor. All conditions were acceptable. | ||||
-1384390051 | 2013-09-12 | Express Energy Services installed a cellar. A corrugated culvert, 8 feet deep and 8 feet in diameter, was grouted in place, using a ready mix truck. | ||||
1391109016 | 2014-01-29 | A roof was on the pump house. There was no work in progress at the time. | ||||
1395666950 | 2014-03-04 | Northeast Region Supervisor, UIC Inspector Steve Ochs and myself performed a status check on the above location. Tank pad and tanks are under construction. We walked the location. There were no violations noted at this time. | ||||
1402332904 | 2014-05-14 | The purpose of this inspection was to review the construction of the surface facility.
My inspection was accompanied by Tom Tomastik and Andrew Adgate. We met with Steve Kilper, with American Water Management Services. The surface facility construction was consistent with the facility plan and met all permit specifications. |
||||
1410188658 | 2014-07-15 | There were no violations at the time of inspection. | ||||
-14835038 | 2014-07-28 | There were no violations at the time of inspection. | ||||
-1550982709 | 2014-06-20 | A mechanical integrity test on the injection line was witnessed. A pressure of 1680 psi. was placed on the injection line. The test passed with a gain in pressure. | ||||
-1827666455 | 2013-09-13 | I witnessed Express Energy cement the 30 conductor casing using approximately 22 yards grout. | ||||
2129979424 | 2014-01-09 | The operator was moving mud and cuttings inside the drilling pits, in order to make room for cement. The cement will be used to solidify the pits. All conditions were acceptable. | ||||
217938545 | 2013-09-13 | 40 feet of 30 inch diameter casing was cemented with 8 yards of concrete. Cement operation and site conditions were acceptable. | ||||
-254408939 | 2013-09-18 | 100 feet of 20 inch diameter conductor was cemented at 95 feet below ground level, using 260 sacks of Class-A cement with 2% CaCl and 1/2 lb./sk. of cellophane flakes. Cement operation and site conditions were acceptable. | ||||
-39750702 | 2014-09-03 | A sample was taken from the facility. The sample, number SJO-116, was taken to the lab for analysis. | ||||
-423600398 | 2014-11-07 | The well operation has been suspended. There were no additional concerns found. | ||||
-477006335 | 2014-01-03 | The well owner was grading and compacting soil for the surface facility construction. The drilling contractor was moving drilling equipment off the pad. All conditions were acceptable. | ||||
-741839577 | 2014-04-10 | An attempt was made to pressure test the flow line. Equipment was not ready and the test was postponed. | ||||
830340725 | 2014-11-24 | The well operation has been suspended. No additional concerns were found. |
For data sources see[1]