X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

Difference between revisions of "34-115-60248"

m
 
m
Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-115-60248
 
| Well ID: 34-115-60248
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.6473968695, -82.0176905366 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.64739687, -82.01769054 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Morgan County, Ohio|Morgan]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[KNOX ENERGY INC.]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
| Spud Date:
+
| Spud Date:  
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Producing
 
|-
 
|-
| Violations: 2
+
| Violations: 0
 
|-
 
|-
| Latitude: 39.6473968695
+
| Latitude: 39.64739687
 
|-
 
|-
| Longitude: -82.0176905366
+
| Longitude: -82.01769054
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 2008-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 120.0
 +
|
 +
|-
 +
|-
 +
| 2009-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 459.0
 +
|
 +
|-
 +
|-
 +
| 2010-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 356.0
 +
|
 +
|-
 +
|-
 +
| 2012-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 456.0
 +
|
 +
|-
 +
|-
 +
| 2013-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 361.0
 +
|
 +
|-
 +
|-
 +
| 2014-0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 365.0
 +
|
 +
|
 +
| style="text-align:right;" | 442.0
 +
| style="text-align:right;" | 365.0
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 112:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
|-
 
| -173921699
 
| 2013-06-19
 
|
 
| Well is currently in production. There is a dike with two 50bbl tanks adjacent to the wellhead, however there are also 2 100bbl tanks at entrance to the access road where they have posted the identification. The stuffing box is leaking at the wellhead and there is some crude down around the base of the 4.5" casing. Operator must repair or replace leaking equipment and must properly remove the contamination from wellhead. I called and left a message with Bill Mitton describing the issues.
 
|
 
| 9-9-05(A)1
 
|
 
|-
 
|-
 
| -173921699
 
| 2013-06-19
 
|
 
| Well is currently in production. There is a dike with two 50bbl tanks adjacent to the wellhead, however there are also 2 100bbl tanks at entrance to the access road where they have posted the identification. The stuffing box is leaking at the wellhead and there is some crude down around the base of the 4.5" casing. Operator must repair or replace leaking equipment and must properly remove the contamination from wellhead. I called and left a message with Bill Mitton describing the issues.
 
|
 
| 9-9-05(A)8
 
|
 
|-
 
 
|-
 
|-
 
| 1376919387
 
| 1376919387
 
| 2013-08-19
 
| 2013-08-19
|
+
|  
 
| Compliance Action Follow-Up -173921699: Well tender has cleaned up the area and has thrown down some peat/sawdust adsorbent around the wellhead. I called and explained the issues and he will be out this week to repair the stuffing box and remove any residual contamination.
 
| Compliance Action Follow-Up -173921699: Well tender has cleaned up the area and has thrown down some peat/sawdust adsorbent around the wellhead. I called and explained the issues and he will be out this week to repair the stuffing box and remove any residual contamination.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1383577710
 
| 1383577710
 
| 2013-11-04
 
| 2013-11-04
|
+
|  
 
| Compliance Action Follow-Up -173921699: There are no issues to report at this time.
 
| Compliance Action Follow-Up -173921699: There are no issues to report at this time.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -173921699
 +
| 2013-06-19
 +
|
 +
| Well is currently in production. There is a dike with two 50bbl tanks adjacent to the wellhead, however there are also 2 100bbl tanks at entrance to the access road where they have posted the identification. The stuffing box is leaking at the wellhead and there is some crude down around the base of the 4.5 casing. Operator must repair or replace leaking equipment and must properly remove the contamination from wellhead. I called and left a message with Bill Mitton describing the issues.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 2111129298
 
| 2111129298
 
| 2013-10-30
 
| 2013-10-30
|
+
|  
 
| Compliance Action Follow-Up -173921699: There was crude onto of the casing head and around the wellhead at ground level. Bobby, with Knox, had stuffed some diapers into the hole but there has been no resolution to the main issues. I did talk to Bobby and he is going to come over tomorrow and work on the stuffing box to determine the source of the leak.
 
| Compliance Action Follow-Up -173921699: There was crude onto of the casing head and around the wellhead at ground level. Bobby, with Knox, had stuffed some diapers into the hole but there has been no resolution to the main issues. I did talk to Bobby and he is going to come over tomorrow and work on the stuffing box to determine the source of the leak.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 21:55, 15 July 2015

Well Details

Well ID: 34-115-60248
Loading map...
County: Morgan
Municipality:
Operator Name: KNOX ENERGY INC.
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.64739687
Longitude: -82.01769054

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2008-0 0.0 120.0
2009-0 0.0 459.0
2010-0 0.0 356.0
2012-0 0.0 456.0
2013-0 0.0 361.0
2014-0 0.0 365.0 442.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1376919387 2013-08-19 Compliance Action Follow-Up -173921699: Well tender has cleaned up the area and has thrown down some peat/sawdust adsorbent around the wellhead. I called and explained the issues and he will be out this week to repair the stuffing box and remove any residual contamination.
1383577710 2013-11-04 Compliance Action Follow-Up -173921699: There are no issues to report at this time.
-173921699 2013-06-19 Well is currently in production. There is a dike with two 50bbl tanks adjacent to the wellhead, however there are also 2 100bbl tanks at entrance to the access road where they have posted the identification. The stuffing box is leaking at the wellhead and there is some crude down around the base of the 4.5 casing. Operator must repair or replace leaking equipment and must properly remove the contamination from wellhead. I called and left a message with Bill Mitton describing the issues.
2111129298 2013-10-30 Compliance Action Follow-Up -173921699: There was crude onto of the casing head and around the wellhead at ground level. Bobby, with Knox, had stuffed some diapers into the hole but there has been no resolution to the main issues. I did talk to Bobby and he is going to come over tomorrow and work on the stuffing box to determine the source of the leak.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.