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Difference between revisions of "34-119-24612"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-119-24612
 
| Well ID: 34-119-24612
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.7965311826, -81.8517841136 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.79658963, -81.85248375 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Muskingum County, Ohio|Muskingum]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[NORTHWOOD ENERGY CORP]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1981-08-23
 
| Spud Date: 1981-08-23
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Final Restoration
 
|-
 
|-
 
| Violations: 0
 
| Violations: 0
 
|-
 
|-
| Latitude: 39.7965311826
+
| Latitude: 39.79658963
 
|-
 
|-
| Longitude: -81.8517841136
+
| Longitude: -81.85248375
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1984-0
 +
| style="text-align:right;" | 10304.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 2008.0
 +
|
 +
|-
 +
|-
 +
| 1985-0
 +
| style="text-align:right;" | 6504.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 545.0
 +
|
 +
|-
 +
|-
 +
| 1986-0
 +
| style="text-align:right;" | 2025.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 291.0
 +
|
 +
|-
 +
|-
 +
| 1987-0
 +
| style="text-align:right;" | 2938.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 361.0
 +
|
 +
|-
 +
|-
 +
| 1988-0
 +
| style="text-align:right;" | 3263.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 223.0
 +
|
 +
|-
 +
|-
 +
| 1989-0
 +
| style="text-align:right;" | 1998.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 246.0
 +
|
 +
|-
 +
|-
 +
| 1990-0
 +
| style="text-align:right;" | 1592.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 184.0
 +
|
 +
|-
 +
|-
 +
| 1991-0
 +
| style="text-align:right;" | 1926.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 230.0
 +
|
 +
|-
 +
|-
 +
| 1992-0
 +
| style="text-align:right;" | 1494.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 125.0
 +
|
 +
|-
 +
|-
 +
| 1993-0
 +
| style="text-align:right;" | 546.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 57.0
 +
|
 +
|-
 +
|-
 +
| 1994-0
 +
| style="text-align:right;" | 1057.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 63.0
 +
|
 +
|-
 +
|-
 +
| 1995-0
 +
| style="text-align:right;" | 1011.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 939.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 31.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 860.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 1058.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1999-0
 +
| style="text-align:right;" | 308.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 27.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
|
 +
|
 +
|
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 234.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2002-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2003-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2004-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2005-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2006-0
 +
| style="text-align:right;" | 380.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2007-0
 +
| style="text-align:right;" | 234.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2008-0
 +
| style="text-align:right;" | 274.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 9.0
 +
|
 +
|-
 +
|-
 +
| 2009-0
 +
| style="text-align:right;" | 251.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2010-0
 +
| style="text-align:right;" | 173.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 8.0
 +
|
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 301:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
 
| -1449638101
 
| -1449638101
 
| 2010-12-07
 
| 2010-12-07
|
+
|  
 
| Cemenco set top plug.  Well is plugged and abandoned this date.  See plugging report for details.
 
| Cemenco set top plug.  Well is plugged and abandoned this date.  See plugging report for details.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| -1614653855
 
| -1614653855
 
| 2010-12-08
 
| 2010-12-08
|
+
|  
 
| Top plug stayed up.  Cutting off casing below GL.
 
| Top plug stayed up.  Cutting off casing below GL.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| 2082945981
 +
| 2005-02-03
 +
|
 +
| Okay
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| -2138081262
 
| -2138081262
 
| 2010-12-06
 
| 2010-12-06
|
+
|  
 
| Cemenco set bottom, Big Lime and Berea plugs.  Pipe dragged excessively and we ran out of daylight.
 
| Cemenco set bottom, Big Lime and Berea plugs.  Pipe dragged excessively and we ran out of daylight.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| 737974027
 +
| 2012-04-12
 +
|
 +
| On the day of my inspection I found the well to have been plugged, the production equipment has been removed, there is good vegetation and erosion control, the pit has been back filled, the roadway has been restored.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| -903724499
 
| -903724499
 
| 2008-01-09
 
| 2008-01-09
|
+
|  
 
| Producing, no problems noted.
 
| Producing, no problems noted.
|
+
|  
|
+
|  
|
+
|  
|-
 
|-
 
| 2082945981
 
| 2005-02-03
 
|
 
| Okay
 
|
 
|
 
|
 
|-
 
|-
 
| 737974027
 
| 2012-04-12
 
|
 
| On the day of my inspection I found the well to have been plugged, the production equipment has been removed, there is good vegetation and erosion control, the pit has been back filled, the roadway has been restored.
 
|
 
|
 
|
 
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 22:08, 15 July 2015

Well Details

Well ID: 34-119-24612
Loading map...
County: Muskingum
Municipality:
Operator Name: NORTHWOOD ENERGY CORP
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1981-08-23
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 39.79658963
Longitude: -81.85248375

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 10304.0 2008.0
1985-0 6504.0 545.0
1986-0 2025.0 291.0
1987-0 2938.0 361.0
1988-0 3263.0 223.0
1989-0 1998.0 246.0
1990-0 1592.0 184.0
1991-0 1926.0 230.0
1992-0 1494.0 125.0
1993-0 546.0 57.0
1994-0 1057.0 63.0
1995-0 1011.0 0.0
1996-0 939.0 31.0
1997-0 860.0 0.0
1998-0 1058.0 0.0
1999-0 308.0 27.0
2000-0
2001-0 234.0 0.0
2002-0 0.0 0.0
2003-0 0.0 0.0
2004-0 0.0 0.0
2005-0 0.0 0.0
2006-0 380.0 0.0
2007-0 234.0 0.0
2008-0 274.0 9.0
2009-0 251.0 0.0
2010-0 173.0 8.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1449638101 2010-12-07 Cemenco set top plug. Well is plugged and abandoned this date. See plugging report for details.
-1614653855 2010-12-08 Top plug stayed up. Cutting off casing below GL.
2082945981 2005-02-03 Okay
-2138081262 2010-12-06 Cemenco set bottom, Big Lime and Berea plugs. Pipe dragged excessively and we ran out of daylight.
737974027 2012-04-12 On the day of my inspection I found the well to have been plugged, the production equipment has been removed, there is good vegetation and erosion control, the pit has been back filled, the roadway has been restored.
-903724499 2008-01-09 Producing, no problems noted.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.