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Difference between revisions of "34-121-21441"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-121-21441
 
| Well ID: 34-121-21441
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.90482946, -81.44380939 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.904757514, -81.44396789 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Noble County, Ohio|Noble]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Noble_County,_Ohio|Noble]]
 +
|-
 +
| Municipality: [[Wayne_Township,_Noble_County,_Ohio|Wayne Township]]
 
|-
 
|-
 
| Operator Name: [[RMB CORPORATION]]
 
| Operator Name: [[RMB CORPORATION]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: BURNS MILES
 
|-
 
|-
| First Permit Date:  
+
| License Status: Producing
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 1970-10-02
 
|-
 
|-
 
| Spud Date: 1970-10-20
 
| Spud Date: 1970-10-20
 
|-
 
|-
| Unconventional:  
+
| Spud Drilling Contractor:  
 +
|-
 +
| Final Drill Date: 1971-05-25
 
|-
 
|-
| Configuration:  
+
| Well Total Depth: 1314 ft
 
|-
 
|-
| Well Status: Producing
+
| Configuration: Vertical
 
|-
 
|-
| Violations: 0
+
| Latitude: 39.904757514
 
|-
 
|-
| Latitude: 39.90482946
+
| Longitude: -81.44396789
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 
|-
 
|-
| Longitude: -81.44380939
+
| CO
 +
| 1970-10-02
 +
| 594  RMB CORPORATION  GeoDate  10/2/70
 +
|-
 +
| Original Spud
 +
| 1970-10-20
 +
| I.P. SR., I.P. NAT, OIL 10 GAL. OIL.
 +
|-
 +
| Completed
 +
| 1971-05-25
 +
| I.P. SR., I.P. NAT, OIL 10 GAL. OIL.
 +
|-
 +
| Reached Total Depth
 +
| 1971-05-25
 +
| I.P. SR., I.P. NAT, OIL 10 GAL. OIL.
 +
|-
 +
| Record Last Modified
 +
| 2013-10-03
 +
| I.P. SR., I.P. NAT, OIL 10 GAL. OIL.
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
== Stimulations Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Stimulation Date
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Chemical Agent
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Fracking Fluid Volume
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
!scope="col" | OIL QUANTITY
+
!scope="col" style="text-align: center"| Fracking Company
!scope="col" | OIL PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
| 2013-0
 
| style="text-align:right;" | 0.0
 
 
|  
 
|  
 +
| GEL
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 250 Lbs
 +
| style="text-align: right;" | 0
 
|  
 
|  
 
|  
 
|  
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 2013
 +
| [[RMB CORPORATION]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2014
 +
| [[RMB CORPORATION]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2015
 +
| [[RMB CORPORATION]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2016
 +
| [[RMB CORPORATION]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 2013
 +
| [[RMB CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2014
 +
| [[RMB CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2015
 +
| [[RMB CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2016
 +
| [[RMB CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Inspection Data ==
 +
==== Inspections Performed ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Inspection Date
 +
!scope="col" style="text-align: center"| Inspection Type
 +
!scope="col" style="text-align: center"| Inspection Result
 +
!scope="col" style="text-align: center"| Inspection Comments
 +
|-
 +
| 0976552996
 +
| 2016-03-01
 +
| Production Wells
 +
| No Violations
 +
| I met with Ruth Burns the owner of RMB Corp.  Ms. Burns stated that the well was plugged, but could not find any record of it.  I walked the area around the coordinates in RBDMS and found no sign of a well.  I was shown an indentation in the ground at 39.90483 -81.4444 by a former employee of RMB Corp. who stated that was the location of the well.
 
|-
 
|-
| 2014-0
+
| 2103878712
| style="text-align:right;" | 0.0
+
| 2018-11-16
| style="text-align:right;" | 0.0
+
| Production Wells
|  
+
| No Violations
|  
+
| On the day of my inspection I was unable to locate the well.  After speaking with the landowner Bill Combs, he informed me that the well had been plugged years ago.  There was no Plug Report on file in RBDMS.  Southwest Supervisor Eric Conrad performed a field inspection in 2016 and was also unsuccessful at locating the well.  Eric met with the owner of RMB Corporation Ruth Burns and according to his report she informed him that the well was plugged but she was unable to locate any documents regarding the plug job.  He informed me that Ruth Burns the owner of RMB Corporation had passed away and there was no one operating the company anymore.  I attempted to reach RMB Corporation with the contact information in RBDMS and was unsuccessful. After further investigation there are 5 wells that are listed in RBDMS as producing under the Bond.
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 00:29, 24 July 2019

Well Details

Well ID: 34-121-21441
Loading map...
Country: United States
State: Ohio
County: Noble
Municipality: Wayne Township
Operator Name: RMB CORPORATION
Well Pad ID:
Farm/Lease Name: BURNS MILES
License Status: Producing
License Date: 1970-10-02
Spud Date: 1970-10-20
Spud Drilling Contractor:
Final Drill Date: 1971-05-25
Well Total Depth: 1314 ft
Configuration: Vertical
Latitude: 39.904757514
Longitude: -81.44396789

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1970-10-02 594 RMB CORPORATION GeoDate 10/2/70
Original Spud 1970-10-20 I.P. SR., I.P. NAT, OIL 10 GAL. OIL.
Completed 1971-05-25 I.P. SR., I.P. NAT, OIL 10 GAL. OIL.
Reached Total Depth 1971-05-25 I.P. SR., I.P. NAT, OIL 10 GAL. OIL.
Record Last Modified 2013-10-03 I.P. SR., I.P. NAT, OIL 10 GAL. OIL.

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
GEL 0 250 Lbs 0

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2013 RMB CORPORATION 0 0 0
2014 RMB CORPORATION 0 0 0
2015 RMB CORPORATION 0 0 0
2016 RMB CORPORATION 0 0 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2013 RMB CORPORATION Brine 0 0
2014 RMB CORPORATION Brine 0 0
2015 RMB CORPORATION Brine 0 0
2016 RMB CORPORATION Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0976552996 2016-03-01 Production Wells No Violations I met with Ruth Burns the owner of RMB Corp. Ms. Burns stated that the well was plugged, but could not find any record of it. I walked the area around the coordinates in RBDMS and found no sign of a well. I was shown an indentation in the ground at 39.90483 -81.4444 by a former employee of RMB Corp. who stated that was the location of the well.
2103878712 2018-11-16 Production Wells No Violations On the day of my inspection I was unable to locate the well. After speaking with the landowner Bill Combs, he informed me that the well had been plugged years ago. There was no Plug Report on file in RBDMS. Southwest Supervisor Eric Conrad performed a field inspection in 2016 and was also unsuccessful at locating the well. Eric met with the owner of RMB Corporation Ruth Burns and according to his report she informed him that the well was plugged but she was unable to locate any documents regarding the plug job. He informed me that Ruth Burns the owner of RMB Corporation had passed away and there was no one operating the company anymore. I attempted to reach RMB Corporation with the contact information in RBDMS and was unsuccessful. After further investigation there are 5 wells that are listed in RBDMS as producing under the Bond.

For data sources see[8]

References