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Difference between revisions of "34-157-21471"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-157-21471
 
| Well ID: 34-157-21471
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.37202774, -81.30096827 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.371961524, -81.30113691 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Tuscarawas County, Ohio|Tuscarawas]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Tuscarawas_County,_Ohio|Tuscarawas]]
 +
|-
 +
| Municipality: [[Mill_Township,_Tuscarawas_County,_Ohio|Mill Township]]
 
|-
 
|-
 
| Operator Name: [[COTTRELL AARON]]
 
| Operator Name: [[COTTRELL AARON]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: KENDALL
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2014-05-27
 
|-
 
|-
 
| Spud Date: 1971-10-04
 
| Spud Date: 1971-10-04
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor: [[ARMSTRONG DRLG]]
 +
|-
 +
| Final Drill Date: 1971-10-12
 +
|-
 +
| Well Total Depth: 5570 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Final Restoration
+
| Latitude: 40.371961524
 +
|-
 +
| Longitude: -81.30113691
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| Original Spud
 +
| 1971-10-04
 +
| CN 2012 09 045
 +
|-
 +
| Completed
 +
| 1971-10-12
 +
| CN 2012 09 045
 +
|-
 +
| Reached Total Depth
 +
| 1971-10-12
 +
| CN 2012 09 045
 +
|-
 +
| Completion Report Received
 +
| 1973-03-30
 +
| CN 2012 09 045
 +
|-
 +
| CO
 +
| 1982-04-19
 +
| 602  CARTER RESOURCES  GeoDate  4/19/82
 +
|-
 +
| Unknown
 +
| 1982-04-19
 +
| Issued Date 4/20/82 Expired Date 10/17/82 Proposed Purpose OG Was Plug Supervised  Who Superivsed Plug and Abandon Date
 +
|-
 +
| CO
 +
| 1995-01-24
 +
| 5051  BURDETTE EVERETTE S  GeoDate  4/19/82
 +
|-
 +
| CO
 +
| 1995-01-24
 +
| 602    CARTER RESOURCES
 
|-
 
|-
| Violations: 0
+
| Change of Owner
 +
| 2014-01-13
 +
| Operator changed from 5051, BURDETTE EVERETTE S to 8318, ORPHAN WELL PROGRAM
 
|-
 
|-
| Latitude: 40.37202774
+
| APP
 +
| 2014-01-17
 +
| Proposed Formations:CLINTON, Issued Date:1/17/2014, Expired Date:1/17/2016 12:00:00 PM, Drilling unit acres:50, Proposed Well Type:OG, Proposed Well Class:
 
|-
 
|-
| Longitude: -81.30096827
+
| Change of Owner
 +
| 2014-02-12
 +
| Operator changed from 8318, ORPHAN WELL PROGRAM to 40004, COTTRELL AARON
 +
|-
 +
| Plugged by Orphan Well Program
 +
| 2014-07-25
 +
| Plugged by Orphan Well Program
 +
|-
 +
| Plugged/Abandoned
 +
| 2014-07-25
 +
| CN 2012 09 045
 +
|-
 +
| Construction Permit Expires
 +
| 2016-01-17
 +
| CN 2012 09 045
 +
|-
 +
| Record Last Modified
 +
| 2017-02-15
 +
| CN 2012 09 045
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
| 2006-06-02
 +
| style="text-align: right;" | 5366
 +
| style="text-align: right;" | 5452
 +
| style="text-align: right;" | 19
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Perfs Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
== Stimulations Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Stimulation Date
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Chemical Agent
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Fracking Fluid Volume
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
!scope="col" | OIL QUANTITY
+
!scope="col" style="text-align: center"| Fracking Company
!scope="col" | OIL PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
| 1984-0
 
| style="text-align:right;" | 2482.0
 
 
|  
 
|  
 +
| H2O
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 1800 Bbl
 +
| style="text-align: right;" | 0
 
|  
 
|  
 
|  
 
|  
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 1984
 +
| [[CARTER RESOURCES]]
 +
| style="text-align: right;" | 2482
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1985
 +
| [[CARTER RESOURCES]]
 +
| style="text-align: right;" | 1317
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1986
 +
| [[CARTER RESOURCES]]
 +
| style="text-align: right;" | 1367
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1987
 +
| [[CARTER RESOURCES]]
 +
| style="text-align: right;" | 611
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1985-0
+
| 1988
| style="text-align:right;" | 1317.0
+
| [[CARTER RESOURCES]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 10
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1991
 +
| [[MIDCOAST RESOURCES CO]]
 +
| style="text-align: right;" | 192
 +
| style="text-align: right;" | 66
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1986-0
+
|}
| style="text-align:right;" | 1367.0
+
For data sources see<ref>{{cite web
|  
+
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
|  
+
|publisher = [[Ohio Department of Natural Resources]]
|  
+
| date =  2019-05-07
| style="text-align:right;" | 0.0
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
|
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
| 1984
 +
| [[CARTER RESOURCES]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1987-0
+
| 1985
| style="text-align:right;" | 611.0
+
| [[CARTER RESOURCES]]
|
+
| Brine
|
+
| style="text-align: right;" | 35
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1986
 +
| [[CARTER RESOURCES]]
 +
| Brine
 +
| style="text-align: right;" | 60
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1988-0
+
| 1987
| style="text-align:right;" | 0.0
+
| [[CARTER RESOURCES]]
|
+
| Brine
|
+
| style="text-align: right;" | 38
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 10.0
 
|
 
 
|-
 
|-
 +
| 1988
 +
| [[CARTER RESOURCES]]
 +
| Brine
 +
| style="text-align: right;" | 30
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1991-0
+
| 1991
| style="text-align:right;" | 192.0
+
| [[MIDCOAST RESOURCES CO]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 66.0
 
|
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2019-05-07
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2019-05-21 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
+
|-
!scope="col" | VIOLATION COMMENT
+
| 0009698174
 +
| 2014-04-21
 +
| Orphan
 +
| No Violations
 +
| A follow up Inspection was conducted on 04/21/2014 for contract compliance.
 +
-100 pound bags of cement to top off the casing.
 +
|-
 +
| 0034718564
 +
| 2014-05-27
 +
| Final Restoration
 +
| No Violations
 +
| A follow-up inspection was conducted on 03/26/2014 for contract compliance.
 +
 
 +
The gravel driveway used to access the site has been finish graded.  The access from the gravel drive to the well and the wellsite has also been finish graded and seeded and vegetative growth established. The visible piping, downgradient of the well has been removed.
 +
  Final Restoration completed and approved.
 +
|-
 +
| 0038266933
 +
| 2014-03-14
 +
| Orphan
 +
| No Violations
 +
| This follow up Inspection was conducted on 03/14/2014  for contract compliance.
 +
I obtained a signed Right-of-Entry (ROE) from the landowner (Michael and Sarah Cady) at address 7318. It will be their driveway which the contactor will be using to access the well.
 +
I walked the perimeter of the location with my Sperian gas meter to check levels of H2S and natural gas - none detected.
 +
- none detected.
 +
The Contractor excavated around the well bore, to a depth of approximately 4, and found 8.625 diameter casing with a well head and 4.5 diameter casing rusted off at top of slips.  The contractor had to replace the side port fittings on the wellhead, due to corrosion.
 +
The Contractor welded an 11 diameter collar onto the wellhead to install a control head and then positioned the rig over wellhead and commenced the clean out.
 +
 
 +
|-
 +
| 0068119658
 +
| 2014-03-27
 +
| Orphan
 +
| No Violations
 +
| No site inspection was conducted on 03-27 due to a meeting held in the New Philadelphia office with Gene Chini (Orphan Program Manager), Keith and Jeff Moore and I to discuss what remedial action that will be taken to correct the top cement plug, which is leaking. The decision was made to drill out the top plug to a depth of approximately 100 and re-plug. Moore will submit a cost estimate for this remedial action.
 
|-
 
|-
| 1194451610
+
| 0141843849
| 2007-04-27
+
| 2014-04-07
|  
+
| Orphan
| Arrived on location and found well idle wellhead has fallen off, I cannot get in touch with complainant, Mr Todd rents this property and I told the renter to have mr todd get in touch with me.
+
| No Violations
 
|  
 
|  
 +
This follow up inspection was conducted on 04-07 for contract compliance.
 +
-
 +
The landowner visited the site and inquired on the drilling status.  I advised him that the surface plug had to be drilled out and re-set.
 +
-5 minutes to see if the cuttings would drop out and then re-start the mud pump. When Keith called back he stated that he could tell the cuttings had dropped out due the increased pressure on mud pump. I then advised him to mud up the freshwater.
 +
This loss of circulation maybe due to a hole or part in the surface casing.
 +
|-
 +
| 0366557058
 +
| 2014-03-21
 +
| Orphan
 +
| No Violations
 +
| This follow up Inspection was conducted on 03/21/2014 for contract compliance.
 +
I walked area with my Sperian gas meter to check for H2S and natural gas ---2 in diameter.
 +
|-
 +
| 0446515875
 +
| 2014-03-31
 +
| Orphan
 +
| No Violations
 
|  
 
|  
 +
A follow up  Inspection was conducted on 03/31/2014 for contract compliance.
 +
No work done on well, just site cleanup and fluid removal from the half tank, to get ready for the drillout of the surface plug.
 +
Checked well and found gas bubbling through the fluid in the well bore.  Gas readings are as follows: CH4 - .01 PPM, 1% LEL, 4% CO and H2S - 0 PPM.
 +
|-
 +
| 0712143399
 +
| 2014-03-24
 +
| Orphan
 +
| No Violations
 +
| This follow up Inspection was conducted on 03/24/2014 for contract compliance.
 +
 +
I walked area with my Sperian gas meter to check for H2S and natural gas - none detected.
 +
- none was detected.
 +
 +
|-
 +
| 0809120167
 +
| 2015-12-29
 +
| Final Restoration
 +
| No Violations
 +
| Gathering photographic evidence of final restoration. Final restoration is approved.
 +
|-
 +
| 0959349471
 +
| 2014-04-09
 +
| Orphan
 +
| No Violations
 
|  
 
|  
 +
This follow up inspection was conducted on 04-09 for contract compliance.
 +
 +
I checked the casing for natural gas and H2S with my Sperian meter - no detectable readings.
 +
 +
|-
 +
| 0981242030
 +
| 2014-03-17
 +
| Orphan
 +
| No Violations
 +
| A follow up Inspection was conducted on 03/17/2014 for contract compliance.
 +
- none detected.
 +
- none detected this morning.
 +
 +
 +
 
|-
 
|-
 +
| 1194451610
 +
| 2007-04-27
 +
| Production Wells
 +
| No Violations
 +
| Arrived on location and found well idle wellhead has fallen off, I cannot get in touch with complainant, Mr Todd rents this property and I told the renter to have mr todd get in touch with me.
 
|-
 
|-
| -1200320344
+
| 1200320344
 
| 2014-04-03
 
| 2014-04-03
|  
+
| Orphan
 +
| No Violations
 
| A follow up Inspection was conducted on 04-03 for contract compliance.
 
| A follow up Inspection was conducted on 04-03 for contract compliance.
    Moore
+
 
|
+
        tubing, using a power swivel and fresh water as drilling fluid.
|
+
 
|
+
        Monday.
 
|-
 
|-
|-
+
| 1296110128
| -1296110128
 
 
| 2014-03-19
 
| 2014-03-19
|  
+
| Orphan
 +
| No Violations
 
| A follow up Inspection was conducted on 03/19/2014 for contract compliance.  
 
| A follow up Inspection was conducted on 03/19/2014 for contract compliance.  
 
  I walked the perimeter of the location with my Sperian gas meter to check for H2S and natural gas - none detected.
 
  I walked the perimeter of the location with my Sperian gas meter to check for H2S and natural gas - none detected.
  O
+
- none was detected.
|
+
  The Contractor was on site and checked the well for pressure. They then ran 2.375 diameter steel pipe down over hill to the access road, where the cement equipment will be set up.
|
+
Cementers arrived, rigged up and connected up to the tubing and pumped to see if the tubing is open.  They mixed 40 sacks of 50/50 Poz mix at 15.1#/gallon and displaced it with 19.5 barrels of fluid to set the bottom plug (5337-4837).
|
+
 
|-
+
The Contractor called Logging Company and arranged for them to be on location at 1:00 PM.
 +
 
 +
The Contractor pulled stretch and rotated the tubing and, after several attempts, the tubing came free. Pulled the tubing out of the hole and shut down for the day.
 
|-
 
|-
 
| 1320009765
 
| 1320009765
 
| 2014-04-18
 
| 2014-04-18
|  
+
| Orphan
 +
| No Violations
 
| A follow up Inspection was conducted on 04/18/2014 for contract compliance.
 
| A follow up Inspection was conducted on 04/18/2014 for contract compliance.
 
Checked well for leakage but was unable to check inside well bore because of the cementing head on the 7 diameter casing.
 
Checked well for leakage but was unable to check inside well bore because of the cementing head on the 7 diameter casing.
 
Checked the annulus of 8.625 and 7 diameter casings with my gas meter - no Ch4, LEL, CO or H2S detected.
 
Checked the annulus of 8.625 and 7 diameter casings with my gas meter - no Ch4, LEL, CO or H2S detected.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1332550364
 
| 1332550364
 
| 2014-03-25
 
| 2014-03-25
|  
+
| Orphan
 +
| No Violations
 
| A follow up Inspection was conducted on 03/25/2014 for contract compliance.
 
| A follow up Inspection was conducted on 03/25/2014 for contract compliance.
I walked area with my Sperian gas meter to check for H2S and natural gas - none detected. O
+
I walked area with my Sperian gas meter to check for H2S and natural gas --
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1345926622
 
| 1345926622
 
| 2014-03-19
 
| 2014-03-19
|  
+
| Plug / Plug Back
| Accompanies Inspector Norburt Lowder while witnessing plugging operations on this well.  We witnessed the bottom hole plug being pumped.  After it was pumped, the tubing got hung in the hole and the wire line company came out and shot the tubing.  I also participated with Inspectors Justin Smith, LJ Parkins and Josh Garland in taking an H2S awareness class put on by O'Brian Safety Services.  They were also there monitoring the site for H2S gas coming out of the well bore.
+
| No Violations
|
+
| Accompanies Inspector Norburt Lowder while witnessing plugging operations on this well.  We witnessed the bottom hole plug being pumped.  After it was pumped, the tubing got hung in the hole and the wire line company came out and shot the tubing.  I also participated with Inspectors Justin Smith, LJ Parkins and Josh Garland in taking an H2S awareness class put on by OBrian Safety Services.  They were also there monitoring the site for H2S gas coming out of the well bore.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1395259000
 
| 1395259000
 
| 2014-03-19
 
| 2014-03-19
|  
+
| Plug / Plug Back
| Accompanied Inspectors Josh Garland, Andy Thomas, and Justin Smith to this idle/orphan well site to attend an H2S safety training meeting with O'Brien Safety Services. After the training, we witnessed the attempted removal of the 2.5 tubing, which had become hung up inside the 4.5 casing. The tubing had been shot by Appalachian Well Surveys in an attempt to free it, but the attempt was not successful.
+
| No Violations
|
+
| Accompanied Inspectors Josh Garland, Andy Thomas, and Justin Smith to this idle/orphan well site to attend an H2S safety training meeting with OBrien Safety Services. After the training, we witnessed the attempted removal of the 2.5 tubing, which had become hung up inside the 4.5 casing. The tubing had been shot by Appalachian Well Surveys in an attempt to free it, but the attempt was not successful.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1395263914
 
| 1395263914
 
| 2014-03-19
 
| 2014-03-19
|  
+
| Plug / Plug Back
 +
| No Violations
 
| Witnessed portion of plugging operations. Tubing was hung in hole after bottom hole plug was set. A casing cutter was used in an attempt to free tubing at 4560 feet. Service rig still unable to pull tubing when I left.
 
| Witnessed portion of plugging operations. Tubing was hung in hole after bottom hole plug was set. A casing cutter was used in an attempt to free tubing at 4560 feet. Service rig still unable to pull tubing when I left.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1416102631
 
| 1416102631
 
| 2014-03-13
 
| 2014-03-13
|  
+
| Orphan
 +
| No Violations
 
| Inspection on 03/13/2014 was conducted for contract compliance.
 
| Inspection on 03/13/2014 was conducted for contract compliance.
Gene Chini, Orphan Well Manager, advised me that he had a phone conference with Mr. Rennicker (land owner) as to the access the contractors will be using. He suggested using the driveway for address 7318, which is located directly off of State Route 800, between Bison Water and Mr. Rennicker
+
 
|
+
- none detected.
|
+
 
|
+
 
|-
 
 
|-
 
|-
 
| 1416147055
 
| 1416147055
 
| 2014-03-17
 
| 2014-03-17
|  
+
| Orphan
 +
| No Violations
 
| This follow up Inspection was conducted on 03/17/2014 for contract compliance.
 
| This follow up Inspection was conducted on 03/17/2014 for contract compliance.
  
 
I walked the location perimeter with my Sperian gas meter to check levels of H2S and natural gas - none detected.
 
I walked the location perimeter with my Sperian gas meter to check levels of H2S and natural gas - none detected.
O
+
- none detected.
|
+
 
|
+
 
|
+
 
|-
 
|-
 
| 141843849
 
| 2014-04-07
 
|
 
|
 
This follow up inspection was conducted on 04-07 for contract compliance.
 
Moore
 
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1491380923
 
| 1491380923
 
| 2014-03-18
 
| 2014-03-18
|  
+
| Administrative Inspection
| I attended H2S training with O'Brien Safety Service. The well is being plugged by Moore well service. Inspector Norbert Lowder was the lead inspector.
+
| No Violations
|
+
| I attended H2S training with OBrien Safety Service. The well is being plugged by Moore well service. Inspector Norbert Lowder was the lead inspector.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1496886673
 
| 1496886673
 
| 2014-03-20
 
| 2014-03-20
|  
+
| Orphan
 +
| No Violations
 
| This follow up Inspection was conducted on 03/20/2014 for contract compliance.
 
| This follow up Inspection was conducted on 03/20/2014 for contract compliance.
  
 
I walked area with my Sperian gas meter to check for H2S and natural gas - none detected.
 
I walked area with my Sperian gas meter to check for H2S and natural gas - none detected.
O
+
-
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1733255341
 
| 1733255341
 
| 2014-03-26
 
| 2014-03-26
|  
+
| Orphan
 +
| No Violations
 
| This follow up Inspection was conducted on 03/26/2014 for contract compliance.
 
| This follow up Inspection was conducted on 03/26/2014 for contract compliance.
 
I walked area with my Sperian gas meter to check for H2S and natural gas none detected.
 
I walked area with my Sperian gas meter to check for H2S and natural gas none detected.
O
+
 
|
+
The Contactor opened the well bore and checked it with their meter and found: .01% - CH4, 2% LEL, 5% CO and 0 PPM - H2S.  A meeting is scheduled in New Philadelphia to discuss how to remediate this leakage from the surface plug.
|
+
The Contractor removed the tank from the tank battery area and then leveled the dike and removed the flow lines. Photos were taken though out the removal.
|
 
|-
 
 
|-
 
|-
 
| 1937857332
 
| 1937857332
 
| 2014-04-17
 
| 2014-04-17
|  
+
| Orphan
 +
| No Violations
 
| A follow up Inspection was conducted on 04/17/2014 for contract compliance.
 
| A follow up Inspection was conducted on 04/17/2014 for contract compliance.
  
The Contractor installed new 7 casing, with the collars removed and each joint welded together, to a depth of approximately 102
+
 
|
+
The well bore was checked for natural gas - none was detected.
|
 
|
 
|-
 
 
|-
 
|-
| -2002895509
+
| 2002895509
 
| 2014-03-18
 
| 2014-03-18
|  
+
| Orphan
 +
| No Violations
 
| A follow up Inspection was conducted on 03/18/2014 for contract compliance.
 
| A follow up Inspection was conducted on 03/18/2014 for contract compliance.
|
+
- none detected.
|
+
- none was detected.
|
+
Note:  Since the rig and logging crew will be working around well head and open casing, each crew member was issued an H2S meter.
|-
+
 
 +
 
 +
 
 +
 
 +
 
 +
 
 +
 
 
|-
 
|-
| -2038663627
+
| 2038663627
 
| 2012-08-29
 
| 2012-08-29
|  
+
| Orphan
 +
| No Violations
 
| I&O well leaking h2s gas . Complaint from Columbus ( Terracina Maxwell ) concerning a well which is leaking h2s. After checking well I found that thus well has been in the I&O file in Columbus for five years. Waiting for Columbus to plug this well.
 
| I&O well leaking h2s gas . Complaint from Columbus ( Terracina Maxwell ) concerning a well which is leaking h2s. After checking well I found that thus well has been in the I&O file in Columbus for five years. Waiting for Columbus to plug this well.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 2088193093
 
| 2088193093
 
| 2014-03-19
 
| 2014-03-19
|  
+
| Plug / Plug Back
| I went out to this plug job for H2S training. The well was an idle orphan well that is being plugged by the state. O'Brien's Safety Services was on site for the H2S. They were giving the training while the well was being plugged.
+
| No Violations
|
+
| I went out to this plug job for H2S training. The well was an idle orphan well that is being plugged by the state. OBriens Safety Services was on site for the H2S. They were giving the training while the well was being plugged.
|
 
|
 
|-
 
 
|-
 
|-
 
| 2109572886
 
| 2109572886
 
| 2014-04-08
 
| 2014-04-08
|  
+
| Orphan
 +
| No Violations
 
| This follow up inspection was conducted on 04-08 for contract compliance.
 
| This follow up inspection was conducted on 04-08 for contract compliance.
  
The Contactor ran the 7.875 diameter mill claw bit on 2.375 diameter tubing and drilled to approximately 120
+
-300) to the drilling fluid. There was no fluid loss and the circulated cutting size was .25 to .5 in diameter.
|
 
|
 
|
 
|-
 
|-
 
| 34718564
 
| 2014-05-27
 
|
 
| A follow-up inspection was conducted on 03/26/2014 for contract compliance.
 
 
 
The gravel driveway used to access the site has been finish graded.  The access from the gravel drive to the well and the wellsite has also been finish graded and seeded and vegetative growth established. The visible piping, downgradient of the well has been removed.
 
  Final Restoration completed and approved.
 
|
 
|
 
|
 
|-
 
|-
 
| -366557058
 
| 2014-03-21
 
|
 
| This follow up Inspection was conducted on 03/21/2014 for contract compliance.
 
I walked area with my Sperian gas meter to check for H2S and natural gas - none detected. O
 
|
 
|
 
|
 
|-
 
|-
 
| 38266933
 
| 2014-03-14
 
|
 
| This follow up Inspection was conducted on 03/14/2014  for contract compliance.
 
I obtained a signed Right-of-Entry (ROE) from the landowner (Michael and Sarah Cady) at address 7318. It will be their driveway which the contactor will be using to access the well.
 
I walked the perimeter of the location with my Sperian gas meter to check levels of H2S and natural gas - none detected.
 
O
 
|
 
|
 
|
 
|-
 
|-
 
| 446515875
 
| 2014-03-31
 
|
 
|
 
A follow up  Inspection was conducted on 03/31/2014 for contract compliance.
 
No work done on well, just site cleanup and fluid removal from the half tank, to get ready for the drillout of the surface plug.
 
Checked well and found gas bubbling through the fluid in the well bore.  Gas readings are as follows: CH4 - .01 PPM, 1% LEL, 4% CO and H2S - 0 PPM.
 
|
 
|
 
|
 
|-
 
|-
 
| 68119658
 
| 2014-03-27
 
|
 
| No site inspection was conducted on 03-27 due to a meeting held in the New Philadelphia office with Gene Chini (Orphan Program Manager), Keith and Jeff Moore and I to discuss what remedial action that will be taken to correct the top cement plug, which is leaking. The decision was made to drill out the top plug to a depth of approximately 100' and re-plug. Moore will submit a cost estimate for this remedial action.
 
|
 
|
 
|
 
|-
 
|-
 
| 712143399
 
| 2014-03-24
 
|
 
| This follow up Inspection was conducted on 03/24/2014 for contract compliance.
 
  
I walked area with my Sperian gas meter to check for H2S and natural gas - none detected.
+
Without warning, the circulating fluid changed to a black foam and they lost approximately 10 barrels of fluid. I advised the contractor to stop circulating and remove all the drilling fluid from half-tank. This black fluid could be coal water coming from a possible hole or part in the casing. I advised the Contractor to bail the fluid out of the well bore so a down hole camera can be run.
O
 
|
 
|
 
|
 
 
|-
 
|-
 +
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 
|-
 
|-
| 959349471
+
|}-->
| 2014-04-09
 
|
 
|
 
This follow up inspection was conducted on 04-09 for contract compliance.
 
The rig bailed the fluid in the hole down to a depth of 120
 
|
 
|
 
|
 
|-
 
|-
 
| -9698174
 
| 2014-04-21
 
|
 
| A follow up Inspection was conducted on 04/21/2014 for contract compliance.
 
The Contractor was on site and removed the cementing head, tagged the top of the cement at a depth of 60
 
|
 
|
 
|
 
|-
 
|-
 
| -981242030
 
| 2014-03-17
 
|
 
| A follow up Inspection was conducted on 03/17/2014 for contract compliance.
 
|
 
|
 
|
 
|-
 
|}
 
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 23:05, 24 July 2019

Well Details

Well ID: 34-157-21471
Loading map...
Country: United States
State: Ohio
County: Tuscarawas
Municipality: Mill Township
Operator Name: COTTRELL AARON
Well Pad ID:
Farm/Lease Name: KENDALL
License Status: Final Restoration
License Date: 2014-05-27
Spud Date: 1971-10-04
Spud Drilling Contractor: ARMSTRONG DRLG
Final Drill Date: 1971-10-12
Well Total Depth: 5570 ft
Configuration: Vertical
Latitude: 40.371961524
Longitude: -81.30113691

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1971-10-04 CN 2012 09 045
Completed 1971-10-12 CN 2012 09 045
Reached Total Depth 1971-10-12 CN 2012 09 045
Completion Report Received 1973-03-30 CN 2012 09 045
CO 1982-04-19 602 CARTER RESOURCES GeoDate 4/19/82
Unknown 1982-04-19 Issued Date 4/20/82 Expired Date 10/17/82 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
CO 1995-01-24 5051 BURDETTE EVERETTE S GeoDate 4/19/82
CO 1995-01-24 602 CARTER RESOURCES
Change of Owner 2014-01-13 Operator changed from 5051, BURDETTE EVERETTE S to 8318, ORPHAN WELL PROGRAM
APP 2014-01-17 Proposed Formations:CLINTON, Issued Date:1/17/2014, Expired Date:1/17/2016 12:00:00 PM, Drilling unit acres:50, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2014-02-12 Operator changed from 8318, ORPHAN WELL PROGRAM to 40004, COTTRELL AARON
Plugged by Orphan Well Program 2014-07-25 Plugged by Orphan Well Program
Plugged/Abandoned 2014-07-25 CN 2012 09 045
Construction Permit Expires 2016-01-17 CN 2012 09 045
Record Last Modified 2017-02-15 CN 2012 09 045

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-06-02 5366 5452 19

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1800 Bbl 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 CARTER RESOURCES 2482 0 0
1985 CARTER RESOURCES 1317 0 365
1986 CARTER RESOURCES 1367 0 365
1987 CARTER RESOURCES 611 0 365
1988 CARTER RESOURCES 0 10 365
1991 MIDCOAST RESOURCES CO 192 66 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 CARTER RESOURCES Brine 0 0
1985 CARTER RESOURCES Brine 35 365
1986 CARTER RESOURCES Brine 60 365
1987 CARTER RESOURCES Brine 38 365
1988 CARTER RESOURCES Brine 30 365
1991 MIDCOAST RESOURCES CO Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0009698174 2014-04-21 Orphan No Violations A follow up Inspection was conducted on 04/21/2014 for contract compliance.

-100 pound bags of cement to top off the casing.

0034718564 2014-05-27 Final Restoration No Violations A follow-up inspection was conducted on 03/26/2014 for contract compliance.

The gravel driveway used to access the site has been finish graded. The access from the gravel drive to the well and the wellsite has also been finish graded and seeded and vegetative growth established. The visible piping, downgradient of the well has been removed.

 Final Restoration completed and approved.
0038266933 2014-03-14 Orphan No Violations This follow up Inspection was conducted on 03/14/2014 for contract compliance.
I obtained a signed Right-of-Entry (ROE) from the landowner (Michael and Sarah Cady) at address 7318. It will be their driveway which the contactor will be using to access the well.
I walked the perimeter of the location with my Sperian gas meter to check levels of H2S and natural gas - none detected.

- none detected.

The 	Contractor excavated around the well bore, to a depth of approximately 4, and found 8.625 diameter casing with a well head and 4.5 diameter casing rusted off at top of slips.  The contractor had to replace the side port fittings on the wellhead, due to corrosion.
The 	Contractor welded an 11 diameter collar onto the wellhead to install a control head and then positioned the rig over wellhead and commenced the clean out.
0068119658 2014-03-27 Orphan No Violations No site inspection was conducted on 03-27 due to a meeting held in the New Philadelphia office with Gene Chini (Orphan Program Manager), Keith and Jeff Moore and I to discuss what remedial action that will be taken to correct the top cement plug, which is leaking. The decision was made to drill out the top plug to a depth of approximately 100 and re-plug. Moore will submit a cost estimate for this remedial action.
0141843849 2014-04-07 Orphan No Violations

This follow up inspection was conducted on 04-07 for contract compliance. - The landowner visited the site and inquired on the drilling status. I advised him that the surface plug had to be drilled out and re-set. -5 minutes to see if the cuttings would drop out and then re-start the mud pump. When Keith called back he stated that he could tell the cuttings had dropped out due the increased pressure on mud pump. I then advised him to mud up the freshwater. This loss of circulation maybe due to a hole or part in the surface casing.

0366557058 2014-03-21 Orphan No Violations This follow up Inspection was conducted on 03/21/2014 for contract compliance.

I walked area with my Sperian gas meter to check for H2S and natural gas ---2 in diameter.

0446515875 2014-03-31 Orphan No Violations

A follow up Inspection was conducted on 03/31/2014 for contract compliance. No work done on well, just site cleanup and fluid removal from the half tank, to get ready for the drillout of the surface plug. Checked well and found gas bubbling through the fluid in the well bore. Gas readings are as follows: CH4 - .01 PPM, 1% LEL, 4% CO and H2S - 0 PPM.

0712143399 2014-03-24 Orphan No Violations This follow up Inspection was conducted on 03/24/2014 for contract compliance.

I walked area with my Sperian gas meter to check for H2S and natural gas - none detected. - none was detected.

0809120167 2015-12-29 Final Restoration No Violations Gathering photographic evidence of final restoration. Final restoration is approved.
0959349471 2014-04-09 Orphan No Violations

This follow up inspection was conducted on 04-09 for contract compliance.

I checked the casing for natural gas and H2S with my Sperian meter - no detectable readings.

0981242030 2014-03-17 Orphan No Violations A follow up Inspection was conducted on 03/17/2014 for contract compliance.

- none detected. - none detected this morning.


1194451610 2007-04-27 Production Wells No Violations Arrived on location and found well idle wellhead has fallen off, I cannot get in touch with complainant, Mr Todd rents this property and I told the renter to have mr todd get in touch with me.
1200320344 2014-04-03 Orphan No Violations A follow up Inspection was conducted on 04-03 for contract compliance.
       tubing, using a power swivel and fresh water as drilling fluid.
       Monday.
1296110128 2014-03-19 Orphan No Violations A follow up Inspection was conducted on 03/19/2014 for contract compliance.
I walked the perimeter of the location with my Sperian gas meter to check for H2S and natural gas - none detected.

- none was detected.

The Contractor was on site and checked the well for pressure. They then ran 2.375 diameter steel pipe down over hill to the access road, where the cement equipment will be set up.
	Cementers arrived, rigged up and connected up to the tubing and pumped to see if the tubing is open.  They mixed 40 sacks of 50/50 Poz mix at 15.1#/gallon and displaced it with 19.5 barrels of fluid to set the bottom plug (5337-4837).
The Contractor called Logging Company and arranged for them to be on location at 1:00 PM.
	The Contractor pulled stretch and rotated the tubing and, after several attempts, the tubing came free. Pulled the tubing out of the hole and shut down for the day.
1320009765 2014-04-18 Orphan No Violations A follow up Inspection was conducted on 04/18/2014 for contract compliance.

Checked well for leakage but was unable to check inside well bore because of the cementing head on the 7 diameter casing. Checked the annulus of 8.625 and 7 diameter casings with my gas meter - no Ch4, LEL, CO or H2S detected.

1332550364 2014-03-25 Orphan No Violations A follow up Inspection was conducted on 03/25/2014 for contract compliance.

I walked area with my Sperian gas meter to check for H2S and natural gas --

1345926622 2014-03-19 Plug / Plug Back No Violations Accompanies Inspector Norburt Lowder while witnessing plugging operations on this well. We witnessed the bottom hole plug being pumped. After it was pumped, the tubing got hung in the hole and the wire line company came out and shot the tubing. I also participated with Inspectors Justin Smith, LJ Parkins and Josh Garland in taking an H2S awareness class put on by OBrian Safety Services. They were also there monitoring the site for H2S gas coming out of the well bore.
1395259000 2014-03-19 Plug / Plug Back No Violations Accompanied Inspectors Josh Garland, Andy Thomas, and Justin Smith to this idle/orphan well site to attend an H2S safety training meeting with OBrien Safety Services. After the training, we witnessed the attempted removal of the 2.5 tubing, which had become hung up inside the 4.5 casing. The tubing had been shot by Appalachian Well Surveys in an attempt to free it, but the attempt was not successful.
1395263914 2014-03-19 Plug / Plug Back No Violations Witnessed portion of plugging operations. Tubing was hung in hole after bottom hole plug was set. A casing cutter was used in an attempt to free tubing at 4560 feet. Service rig still unable to pull tubing when I left.
1416102631 2014-03-13 Orphan No Violations Inspection on 03/13/2014 was conducted for contract compliance.

- none detected.


1416147055 2014-03-17 Orphan No Violations This follow up Inspection was conducted on 03/17/2014 for contract compliance.

I walked the location perimeter with my Sperian gas meter to check levels of H2S and natural gas - none detected. - none detected.


1491380923 2014-03-18 Administrative Inspection No Violations I attended H2S training with OBrien Safety Service. The well is being plugged by Moore well service. Inspector Norbert Lowder was the lead inspector.
1496886673 2014-03-20 Orphan No Violations This follow up Inspection was conducted on 03/20/2014 for contract compliance.

I walked area with my Sperian gas meter to check for H2S and natural gas - none detected. -

1733255341 2014-03-26 Orphan No Violations This follow up Inspection was conducted on 03/26/2014 for contract compliance.

I walked area with my Sperian gas meter to check for H2S and natural gas none detected.

The Contactor opened the well bore and checked it with their meter and found: .01% - CH4, 2% LEL, 5% CO and 0 PPM - H2S. A meeting is scheduled in New Philadelphia to discuss how to remediate this leakage from the surface plug. The Contractor removed the tank from the tank battery area and then leveled the dike and removed the flow lines. Photos were taken though out the removal.

1937857332 2014-04-17 Orphan No Violations A follow up Inspection was conducted on 04/17/2014 for contract compliance.


The well bore was checked for natural gas - none was detected.

2002895509 2014-03-18 Orphan No Violations A follow up Inspection was conducted on 03/18/2014 for contract compliance.

- none detected. - none was detected. Note: Since the rig and logging crew will be working around well head and open casing, each crew member was issued an H2S meter.




2038663627 2012-08-29 Orphan No Violations I&O well leaking h2s gas . Complaint from Columbus ( Terracina Maxwell ) concerning a well which is leaking h2s. After checking well I found that thus well has been in the I&O file in Columbus for five years. Waiting for Columbus to plug this well.
2088193093 2014-03-19 Plug / Plug Back No Violations I went out to this plug job for H2S training. The well was an idle orphan well that is being plugged by the state. OBriens Safety Services was on site for the H2S. They were giving the training while the well was being plugged.
2109572886 2014-04-08 Orphan No Violations This follow up inspection was conducted on 04-08 for contract compliance.

-300) to the drilling fluid. There was no fluid loss and the circulated cutting size was .25 to .5 in diameter.

Without warning, the circulating fluid changed to a black foam and they lost approximately 10 barrels of fluid. I advised the contractor to stop circulating and remove all the drilling fluid from half-tank. This black fluid could be coal water coming from a possible hole or part in the casing. I advised the Contractor to bail the fluid out of the well bore so a down hole camera can be run.

For data sources see[9]

References