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Difference between revisions of "34-143-60215"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-143-60215
 
| Well ID: 34-143-60215
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.29020729, -83.37956421 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.292112464, -83.37955064 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Sandusky County, Ohio|Sandusky]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Sandusky_County,_Ohio|Sandusky]]
 +
|-
 +
| Municipality: [[Scott_Township,_Sandusky_County,_Ohio|Scott Township]]
 
|-
 
|-
 
| Operator Name: [[ORPHAN WELL PROGRAM]]
 
| Operator Name: [[ORPHAN WELL PROGRAM]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: SAUTTER TIM (BRINKERHOFF)
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2012-10-26
 
|-
 
|-
 
| Spud Date:  
 
| Spud Date:  
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:
 +
|-
 +
| Final Drill Date:
 +
|-
 +
| Well Total Depth:  
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Final Restoration
+
| Latitude: 41.292112464
 
|-
 
|-
| Violations: 0
+
| Longitude: -83.37955064
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 
|-
 
|-
| Latitude: 41.29020729
+
| Well Added to System
 +
| 2007-10-17
 +
| NO PREVIOUS RECORD OF WELL. INSPECTION ON 2/19/1993 REVEALED WELL  HAS 10" & 7"CASING WITH TUBING & RODS.  I&O CASE # 1993 07 050. EXHIBIT B ON TITLE INSURANCE SHOWS THAT THERE WAS A LEASE FOR OIL & GAS FROM SAMUEL BRINKERHOFF TO J M SHERMAN IN 1898 (RECORDED 3/1/1905). WILL NEED TO CORRECT THE LOCATION WHEN GET A GPS LOCATION.
 
|-
 
|-
| Longitude: -83.37956421
+
| Change of Owner
 +
| 2012-10-18
 +
| Operator changed from 9998, HISTORIC OWNER to 8318, ORPHAN WELL PROGRAM
 +
|-
 +
| APP
 +
| 2012-10-26
 +
| Proposed Formations:, Issued Date:10/26/2012, Expired Date:10/26/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
 +
|-
 +
| Plugged by Orphan Well Program
 +
| 2013-06-19
 +
| Plugged by Orphan Well Program
 +
|-
 +
| Plugged/Abandoned
 +
| 2013-06-19
 +
| NO PREVIOUS RECORD OF WELL. INSPECTION ON 2/19/1993 REVEALED WELL  HAS 10" & 7"CASING,  WITH TUBING & RODS.  I&O CASE # 1993 07 050. EXHIBIT B ON TITLE INSURANCE SHOWS THAT THERE WAS A LEASE FOR OIL & GAS FROM SAMUEL BRINKERHOFF TO J M SHERMAN IN 1898 (RECORDED 3/1/1905). WILL NEED TO CORRECT THE LOCATION WHEN GET A GPS LOCATION.
 +
|-
 +
| Construction Permit Expires
 +
| 2014-10-26
 +
| NO PREVIOUS RECORD OF WELL. INSPECTION ON 2/19/1993 REVEALED WELL  HAS 10" & 7"CASING,  WITH TUBING & RODS.  I&O CASE # 1993 07 050. EXHIBIT B ON TITLE INSURANCE SHOWS THAT THERE WAS A LEASE FOR OIL & GAS FROM SAMUEL BRINKERHOFF TO J M SHERMAN IN 1898 (RECORDED 3/1/1905). WILL NEED TO CORRECT THE LOCATION WHEN GET A GPS LOCATION.
 +
|-
 +
| Record Last Modified
 +
| 2019-06-14
 +
| NO PREVIOUS RECORD OF WELL. INSPECTION ON 2/19/1993 REVEALED WELL  HAS 10" & 7"CASING,  WITH TUBING & RODS.  I&O CASE # 1993 07 050. EXHIBIT B ON TITLE INSURANCE SHOWS THAT THERE WAS A LEASE FOR OIL & GAS FROM SAMUEL BRINKERHOFF TO J M SHERMAN IN 1898 (RECORDED 3/1/1905). WILL NEED TO CORRECT THE LOCATION WHEN GET A GPS LOCATION.
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 +
<!--== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 +
<!--== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
+
|-
!scope="col" | VIOLATION COMMENT
+
| 0228078133
 +
| 2013-06-24
 +
| Plug / Plug Back
 +
| No Violations
 +
| An inspection of this plugged and abandoned well was conducted to check status of cement level and potential leakage.  During the inspection, it was noted that the cement was down approximately 5 with no observed gas bubbling within the fluid.
 +
|-
 +
| 0973722782
 +
| 2012-04-04
 +
| Orphan
 +
| No Violations
 +
| Inspection to update GPS and well status for a potential Orphan Well Package. At the time of my inspection the well had 8conductor casing, 6 surface casing with casing head, 2 tubing on a casing head ring and rods with a stuffing box still inside tubing. The well is in a cow pasture and is surrounded by smaller trees and brush.
 
|-
 
|-
 
| 1370956214
 
| 1370956214
 
| 2013-06-11
 
| 2013-06-11
|  
+
| Plug / Plug Back
| An inspection of plugging operations today revealed that the contractor fished all of the remaining parted steel tubing and wooden rods from the wellbore.  The contractor utilized the same overshot tool, but equipped only with (1) 10' joint of 4.5 instead of (3) 10' joints that were utilized on 6/7/2013.  The tool had initially set down on a rod at approx 340' however, the contractor was unable grab at this location.  Additional joints of tubing were then added to the fishing string to allow for the retrieval of wooden rods at a deeper location.  Note: Natural gas was smelled and felt through the tubing during this procedure.  The contractor latched onto the rods at a depth of 440', but his clutch began to slip and was unable to pull with rig.  The contractor consulted with his partner, Mr. Mike Coyer, and mobilized another rig to the location for the retrieval of this fish.  In summary, all wooden rods, steel tubing, and the working barrel excluding the mud anchor have now been removed from the wellbore.
+
| No Violations
|
+
| An inspection of plugging operations today revealed that the contractor fished all of the remaining parted steel tubing and wooden rods from the wellbore.  The contractor utilized the same overshot tool, but equipped only with (1) 10 joint of 4.5 instead of (3) 10 joints that were utilized on 6/7/2013.  The tool had initially set down on a rod at approx 340 however, the contractor was unable grab at this location.  Additional joints of tubing were then added to the fishing string to allow for the retrieval of wooden rods at a deeper location.  Note: Natural gas was smelled and felt through the tubing during this procedure.  The contractor latched onto the rods at a depth of 440, but his clutch began to slip and was unable to pull with rig.  The contractor consulted with his partner, Mr. Mike Coyer, and mobilized another rig to the location for the retrieval of this fish.  In summary, all wooden rods, steel tubing, and the working barrel excluding the mud anchor have now been removed from the wellbore.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1371752753
 
| 1371752753
 
| 2013-06-19
 
| 2013-06-19
|  
+
| Plug / Plug Back
| I witnessed plugging operations today.  The wellbore was filled solid with approx 7.8 yards of 9 sack grout mix from a total depth of 1230' to the surface.  Prior to cementing, the contractor bailed the hole dry on 6/18/2013 and 6/19/2013.  The contractor was instructed to leave the wellbore open to allow for settling and to ensure no leakage had occurred.
+
| No Violations
|
+
| I witnessed plugging operations today.  The wellbore was filled solid with approx 7.8 yards of 9 sack grout mix from a total depth of 1230 to the surface.  Prior to cementing, the contractor bailed the hole dry on 6/18/2013 and 6/19/2013.  The contractor was instructed to leave the wellbore open to allow for settling and to ensure no leakage had occurred.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1374062072
 
| 1374062072
 
| 2013-07-16
 
| 2013-07-16
|  
+
| Final Restoration
 +
| No Violations
 
| An inspection of the Final Restoration revealed compliance with Ohio Revised Code 1509.072.  The well site was situated on a location designated as pasture field.  At the conclusion of the inspections conducted on Permit Numbers 60214 and 60215, the results were discussed with the landowner, Mr. Tim Sautter, at his residence.  Mr. Sautter confirmed that he was satisfied with the restoration work on this property and the additional wells also plugged and abandoned but located within field crop.
 
| An inspection of the Final Restoration revealed compliance with Ohio Revised Code 1509.072.  The well site was situated on a location designated as pasture field.  At the conclusion of the inspections conducted on Permit Numbers 60214 and 60215, the results were discussed with the landowner, Mr. Tim Sautter, at his residence.  Mr. Sautter confirmed that he was satisfied with the restoration work on this property and the additional wells also plugged and abandoned but located within field crop.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1591383471
 
| 1591383471
 
| 2013-06-07
 
| 2013-06-07
|  
+
| Plug / Plug Back
| At 9:30 am, I arrived at the location with Gene Chini, Orphan Well Program Supervisor, to witness the fishing of parted steel tubing and wooden rods from the wellbore.  A wooden rod was allegedly was sticking up at a depth of approx 340
+
| No Violations
|
+
 
|
 
|
 
|-
 
|-
 
| -228078133
 
| 2013-06-24
 
|
 
| An inspection of this plugged and abandoned well was conducted to check status of cement level and potential leakage.  During the inspection, it was noted that the cement was down approximately 5' with no observed gas bubbling within the fluid.
 
|
 
|
 
|
 
 
|-
 
|-
 +
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 
|-
 
|-
| -973722782
+
|}-->
| 2012-04-04
 
|
 
| Inspection to update GPS and well status for a potential Orphan Well Package. At the time of my inspection the well had 8conductor casing, 6 surface casing with casing head, 2 tubing on a casing head ring and rods with a stuffing box still inside tubing. The well is in a cow pasture and is surrounded by smaller trees and brush.
 
|
 
|
 
|
 
|-
 
|}
 
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 07:39, 31 July 2019

Well Details

Well ID: 34-143-60215
Loading map...
Country: United States
State: Ohio
County: Sandusky
Municipality: Scott Township
Operator Name: ORPHAN WELL PROGRAM
Well Pad ID:
Farm/Lease Name: SAUTTER TIM (BRINKERHOFF)
License Status: Final Restoration
License Date: 2012-10-26
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 41.292112464
Longitude: -83.37955064

For data sources see[1]

Well History

Well Status Well Status Date Comment
Well Added to System 2007-10-17 NO PREVIOUS RECORD OF WELL. INSPECTION ON 2/19/1993 REVEALED WELL HAS 10" & 7"CASING WITH TUBING & RODS. I&O CASE # 1993 07 050. EXHIBIT B ON TITLE INSURANCE SHOWS THAT THERE WAS A LEASE FOR OIL & GAS FROM SAMUEL BRINKERHOFF TO J M SHERMAN IN 1898 (RECORDED 3/1/1905). WILL NEED TO CORRECT THE LOCATION WHEN GET A GPS LOCATION.
Change of Owner 2012-10-18 Operator changed from 9998, HISTORIC OWNER to 8318, ORPHAN WELL PROGRAM
APP 2012-10-26 Proposed Formations:, Issued Date:10/26/2012, Expired Date:10/26/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged by Orphan Well Program 2013-06-19 Plugged by Orphan Well Program
Plugged/Abandoned 2013-06-19 NO PREVIOUS RECORD OF WELL. INSPECTION ON 2/19/1993 REVEALED WELL HAS 10" & 7"CASING, WITH TUBING & RODS. I&O CASE # 1993 07 050. EXHIBIT B ON TITLE INSURANCE SHOWS THAT THERE WAS A LEASE FOR OIL & GAS FROM SAMUEL BRINKERHOFF TO J M SHERMAN IN 1898 (RECORDED 3/1/1905). WILL NEED TO CORRECT THE LOCATION WHEN GET A GPS LOCATION.
Construction Permit Expires 2014-10-26 NO PREVIOUS RECORD OF WELL. INSPECTION ON 2/19/1993 REVEALED WELL HAS 10" & 7"CASING, WITH TUBING & RODS. I&O CASE # 1993 07 050. EXHIBIT B ON TITLE INSURANCE SHOWS THAT THERE WAS A LEASE FOR OIL & GAS FROM SAMUEL BRINKERHOFF TO J M SHERMAN IN 1898 (RECORDED 3/1/1905). WILL NEED TO CORRECT THE LOCATION WHEN GET A GPS LOCATION.
Record Last Modified 2019-06-14 NO PREVIOUS RECORD OF WELL. INSPECTION ON 2/19/1993 REVEALED WELL HAS 10" & 7"CASING, WITH TUBING & RODS. I&O CASE # 1993 07 050. EXHIBIT B ON TITLE INSURANCE SHOWS THAT THERE WAS A LEASE FOR OIL & GAS FROM SAMUEL BRINKERHOFF TO J M SHERMAN IN 1898 (RECORDED 3/1/1905). WILL NEED TO CORRECT THE LOCATION WHEN GET A GPS LOCATION.

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0228078133 2013-06-24 Plug / Plug Back No Violations An inspection of this plugged and abandoned well was conducted to check status of cement level and potential leakage. During the inspection, it was noted that the cement was down approximately 5 with no observed gas bubbling within the fluid.
0973722782 2012-04-04 Orphan No Violations Inspection to update GPS and well status for a potential Orphan Well Package. At the time of my inspection the well had 8conductor casing, 6 surface casing with casing head, 2 tubing on a casing head ring and rods with a stuffing box still inside tubing. The well is in a cow pasture and is surrounded by smaller trees and brush.
1370956214 2013-06-11 Plug / Plug Back No Violations An inspection of plugging operations today revealed that the contractor fished all of the remaining parted steel tubing and wooden rods from the wellbore. The contractor utilized the same overshot tool, but equipped only with (1) 10 joint of 4.5 instead of (3) 10 joints that were utilized on 6/7/2013. The tool had initially set down on a rod at approx 340 however, the contractor was unable grab at this location. Additional joints of tubing were then added to the fishing string to allow for the retrieval of wooden rods at a deeper location. Note: Natural gas was smelled and felt through the tubing during this procedure. The contractor latched onto the rods at a depth of 440, but his clutch began to slip and was unable to pull with rig. The contractor consulted with his partner, Mr. Mike Coyer, and mobilized another rig to the location for the retrieval of this fish. In summary, all wooden rods, steel tubing, and the working barrel excluding the mud anchor have now been removed from the wellbore.
1371752753 2013-06-19 Plug / Plug Back No Violations I witnessed plugging operations today. The wellbore was filled solid with approx 7.8 yards of 9 sack grout mix from a total depth of 1230 to the surface. Prior to cementing, the contractor bailed the hole dry on 6/18/2013 and 6/19/2013. The contractor was instructed to leave the wellbore open to allow for settling and to ensure no leakage had occurred.
1374062072 2013-07-16 Final Restoration No Violations An inspection of the Final Restoration revealed compliance with Ohio Revised Code 1509.072. The well site was situated on a location designated as pasture field. At the conclusion of the inspections conducted on Permit Numbers 60214 and 60215, the results were discussed with the landowner, Mr. Tim Sautter, at his residence. Mr. Sautter confirmed that he was satisfied with the restoration work on this property and the additional wells also plugged and abandoned but located within field crop.
1591383471 2013-06-07 Plug / Plug Back No Violations

For data sources see[3]

References