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Difference between revisions of "34-019-22629"

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__TOC__
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__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-019-22629
 
| Well ID: 34-019-22629
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.57241321, -81.01005246 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.572350768, -81.01023699 | width=100% | height=100% }}
 
|-
 
|-
| County:  
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 
|-
 
|-
| Operator Name:  
+
| County: [[Carroll_County,_Ohio|Carroll]]
 
|-
 
|-
| Well Pad ID:  
+
| Municipality: [[Washington_Township,_Carroll_County,_Ohio|Washington Township]]
 
|-
 
|-
| Farm/Lease Name:  
+
| Operator Name: [[CHESAPEAKE EXPLORATION LLC]]
 
|-
 
|-
| First Permit Date:  
+
| Well Pad ID: [[US-OH-001167]]
 
|-
 
|-
| Last Permit Date:  
+
| Farm/Lease Name: DEAN OTT 7-14-5
 +
|-
 +
| License Status: Producing
 +
|-
 +
| License Date: 2015-01-14
 
|-
 
|-
 
| Spud Date: 2015-01-07
 
| Spud Date: 2015-01-07
 
|-
 
|-
| Unconventional:
+
| Spud Drilling Contractor: [[NOMAC DRILLING CORP]]
|-
 
| Configuration:  
 
 
|-
 
|-
| Well Status: Well Drilled
+
| Final Drill Date: 2015-01-31
 
|-
 
|-
| Violations: 0
+
| Well Total Depth: 15859 ft
 
|-
 
|-
| Latitude: 40.57241321
+
| Configuration: Horizontal
 
|-
 
|-
| Longitude: -81.01005246
+
| Latitude: 40.572350768
 
|-
 
|-
 +
| Longitude: -81.01023699
 
|}
 
|}
== Inspection Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Well Status
!scope="col" | DATE
+
!scope="col" style="width: 15%;text-align: center"| Well Status Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Comment
!scope="col" | COMMENT
+
|-
!scope="col" | VIOLATION ID
+
| APP
!scope="col" | VIOLATION CODE
+
| 2014-11-04
!scope="col" | VIOLATION COMMENT
+
| Proposed Formations:TRENTON-BLACK RIVER, Issued Date:11/4/2014, Expired Date:11/3/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT
 +
|-
 +
| APP
 +
| 2015-01-14
 +
| Proposed Formations:POINT PLEASANT, Issued Date:1/14/2015, Expired Date:1/13/2017 12:00:00 PM, Drilling unit acres:585.485, Proposed Well Type:OG, Proposed Well Class:POOL
 +
|-
 +
| Reached Total Depth
 +
| 2015-01-31
 +
|
 +
|-
 +
| Correction to Well
 +
| 2015-10-02
 +
| UPDATE TO SURFACE, TARGET AND TAKE-POINT INFORMATION (FOOTAGES AND COORDINATES) FROM NEW PLAT.  UNIT SIZE UPDATED.
 
|-
 
|-
| 1566938426
+
| Completion Report Received
| 2015-01-24
+
| 2015-12-17
 +
|
 +
|-
 +
| Construction Permit Expires
 +
| 2017-01-13
 
|  
 
|  
| I was on location to witness the cementing of the 13.375 surface casing.  Nomac Rig #71 spudded the surface hole on 1/23/15 and drilled a 17.5 hole to a depth of 636'.  Wyoming Casing rigged up and ran  casing to a depth of 628'.  The rig was losing circulation (municipal water) of approximately 20 barrels per hour at a depth of 170'.  Schlumberger rigged up the cement head, tested the lines, and pumped 25 barrels of gel and 10 barrels of water ahead of the slurry.  They then mixed and pumped 126 barrels of cement slurry, dropped the plug, and displaced the plug to the collar with 90.4 barrels of water.  The plug landed at 316psi and the pressure was increased and held for 5 minutes at 975psi.  The pressure was released and the floats held with 0.25 barrels flowing back to the truck.  28 barrels of cement circulated to surface.  There were no circulation issues during the job and the cement held at surface.  See casing ticket for more details on this job.  No violations.
+
|-
 +
| Record Last Modified
 +
| 2017-10-23
 
|  
 
|  
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
| 2015-12-17
 +
| style="text-align: right;" | 8309
 +
| style="text-align: right;" | 15706
 +
| style="text-align: right;" | 835
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Perfs Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
| 1
 +
| 05/23/2015
 +
| 06/09/2015
 +
| style="text-align: right;" | 7984
 +
| style="text-align: right;" | 6,447,420.0
 +
| style="text-align: right;" | 522306
 +
|-
 +
|}
 +
==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|- valign="top"
 +
| rowspan="28"| 1
 +
| rowspan="1"| 100 Mesh Sand
 +
| rowspan="1"| HEARTLAND SOLUTIONS
 +
| rowspan="1"| Proppant - Natural
 +
| Crystalline Silica (Quartz Sand, Silicon Dioxide)
 +
| 014808-60-7
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 0.55798
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| Recycled Produced Water
 +
| rowspan="1"| CHESAPEAKE ENERGY
 +
| rowspan="1"| Carrier/Base Fluid
 +
| Water
 +
| 007732-18-5
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 0.59271
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| PTLGL240
 +
| rowspan="1"| PERFORMANCE TECHNOLOGIES
 +
| rowspan="1"| Gelling Agent
 +
| No Hazardous Components
 +
| NONE
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="2"| PTLFR200
 +
| rowspan="2"| PERFORMANCE TECHNOLOGIES
 +
| rowspan="2"| Friction Reducer
 +
| Proprietary Aliphatic Hydrocarbon
 +
| TRADE SECRET
 +
| style="text-align: right;" | 30
 +
| style="text-align: right;" | 0.00912
 +
| style="text-align: right;" | 0
 +
|-
 +
| Proprietary Oxyalkylated Alcohol
 +
| TRADE SECRET
 +
| style="text-align: right;" | 5
 +
| style="text-align: right;" | 0.00152
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="2"| OilSafe AR (Acid Replacement) 1:2 Dilution
 +
| rowspan="2"| HEARTLAND SOLUTIONS
 +
| rowspan="2"| Acid
 +
| Water
 +
| 007732-18-5
 +
| style="text-align: right;" | 67
 +
| style="text-align: right;" | 0.11569
 +
| style="text-align: right;" | 0
 +
|-
 +
| Patented Synthetic Acid
 +
| TRADE SECRET
 +
| style="text-align: right;" | 33
 +
| style="text-align: right;" | 0.05698
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="12"| PTLBW112, PTLFR200, PTLGL240
 +
| rowspan="12"| PERFORMANCE TECHNOLOGIES
 +
| rowspan="12"| Breaker, Friction Reducer, Gelling Agent
 +
| Proprietary Aliphatic Alcohol
 +
| TRADE SECRET
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.03247
 +
| style="text-align: right;" | 0
 +
|-
 +
| Copper Sulfate
 +
| 007758-98-7
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00036
 +
| style="text-align: right;" | 0
 +
|-
 +
| Guar Gum
 +
| 009000-30-0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.2022
 +
| style="text-align: right;" | 0
 +
|-
 +
| Proprietary Clay
 +
| TRADE SECRET
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.2022
 +
| style="text-align: right;" | 0
 +
|-
 +
| Proprietary Vinyl Copolymer
 +
| TRADE SECRET
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.03381
 +
| style="text-align: right;" | 0
 +
|-
 +
| Tetrasodium Ethylenediaminetetraacetate
 +
| 000064-02-8
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.03247
 +
| style="text-align: right;" | 0
 +
|-
 +
| Sodium Chloride
 +
| 007647-14-5
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.03247
 +
| style="text-align: right;" | 0
 +
|-
 +
| Petroleum Distillate Hydrotreated Light
 +
| 064742-47-8
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.2022
 +
| style="text-align: right;" | 0
 +
|-
 +
| Proprietary Substituted Fatty Acid Ester
 +
| TRADE SECRET
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.03247
 +
| style="text-align: right;" | 0
 +
|-
 +
| Proprietary Oxyalkylated Fatty Acid Derivative
 +
| TRADE SECRET
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.03247
 +
| style="text-align: right;" | 0
 +
|-
 +
| Proprietary Surfactant
 +
| TRADE SECRET
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.2022
 +
| style="text-align: right;" | 0
 +
|-
 +
| Water
 +
| 007732-18-5
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.03247
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="3"| PTLCA102
 +
| rowspan="3"| PERFORMANCE TECHNOLOGIES
 +
| rowspan="3"| Cross Linker
 +
| Proprietary Inorganic Salt
 +
| TRADE SECRET
 +
| style="text-align: right;" | 30
 +
| style="text-align: right;" | 0.01299
 +
| style="text-align: right;" | 0
 +
|-
 +
| Sodium Hydroxide
 +
| 001310-73-2
 +
| style="text-align: right;" | 60
 +
| style="text-align: right;" | 0.02598
 +
| style="text-align: right;" | 0
 +
|-
 +
| Proprietary Alkyl Alcohol
 +
| TRADE SECRET
 +
| style="text-align: right;" | 60
 +
| style="text-align: right;" | 0.02598
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| Chlorine Dioxide
 +
| rowspan="1"| TERRA SERVICES
 +
| rowspan="1"| Anti-Bacterial Agent
 +
| Chlorine Dioxide
 +
| 010049-04-4
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 0.00837
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="2"| TS-30
 +
| rowspan="2"| X CHEM
 +
| rowspan="2"| Scale Inhibitor
 +
| Proprietary Sodium Polycarboxylate
 +
| TRADE SECRET
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 0.00953
 +
| style="text-align: right;" | 0
 +
|-
 +
| Water
 +
| 007732-18-5
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.01145
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| Fresh Water
 +
| rowspan="1"| CHESAPEAKE ENERGY
 +
| rowspan="1"| Carrier/Base Fluid
 +
| Water
 +
| 007732-18-5
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 82.2732
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| PTLBW112
 +
| rowspan="1"| PERFORMANCE TECHNOLOGIES
 +
| rowspan="1"| Breaker
 +
| Ammonium Persulfate
 +
| 007727-54-0
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 0.00279
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| Northern White Sand
 +
| rowspan="1"| HEARTLAND SOLUTIONS
 +
| rowspan="1"| Proppant - Natural
 +
| Crystalline Silica (Quartz Sand, Silicon Dioxide)
 +
| 014808-60-7
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 16.1407
 +
| style="text-align: right;" | 0
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = FracFocus Fracking Chemicals Database
 +
| date = 2019-04-02
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-06-19 }}</ref>
 +
== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
| 2015-05-23
 +
| H2O
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 3917 Bbl
 +
| style="text-align: right;" | 330200
 
|  
 
|  
 +
| STAGE 33/33
 +
|-
 +
| 2015-05-23
 +
| H2O
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 1515 Bbl
 +
| style="text-align: right;" | 329780
 
|  
 
|  
 +
| STAGE 1/33
 +
25 SHOTS
 +
STAGES 2-32 SEE IMAGES
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 2015
 +
| [[CHESAPEAKE EXPLORATION LLC]]
 +
| style="text-align: right;" | 454055
 +
| style="text-align: right;" | 15162
 +
| style="text-align: right;" | 114
 +
|-
 +
| 2016
 +
| [[CHESAPEAKE EXPLORATION LLC]]
 +
| style="text-align: right;" | 843796
 +
| style="text-align: right;" | 8609
 +
| style="text-align: right;" | 366
 +
|-
 +
| 2017
 +
| [[CHESAPEAKE EXPLORATION LLC]]
 +
| style="text-align: right;" | 448309
 +
| style="text-align: right;" | 2269
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2018
 +
| [[CHESAPEAKE EXPLORATION LLC]]
 +
| style="text-align: right;" | 324278
 +
| style="text-align: right;" | 1272
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2019
 +
| [[CHESAPEAKE EXPLORATION LLC]]
 +
| style="text-align: right;" | 67902
 +
| style="text-align: right;" | 254
 +
| style="text-align: right;" | 90
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 2015
 +
| [[CHESAPEAKE EXPLORATION LLC]]
 +
| Brine
 +
| style="text-align: right;" | 18343
 +
| style="text-align: right;" | 114
 +
|-
 +
| 2016
 +
| [[CHESAPEAKE EXPLORATION LLC]]
 +
| Brine
 +
| style="text-align: right;" | 8887
 +
| style="text-align: right;" | 366
 +
|-
 +
| 2017
 +
| [[CHESAPEAKE EXPLORATION LLC]]
 +
| Brine
 +
| style="text-align: right;" | 3937
 +
| style="text-align: right;" | 365
 
|-
 
|-
 +
| 2018
 +
| [[CHESAPEAKE EXPLORATION LLC]]
 +
| Brine
 +
| style="text-align: right;" | 3278
 +
| style="text-align: right;" | 365
 
|-
 
|-
| -1875471865
+
| 2019
 +
| [[CHESAPEAKE EXPLORATION LLC]]
 +
| Brine
 +
| style="text-align: right;" | 656
 +
| style="text-align: right;" | 90
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Inspection Data ==
 +
==== Inspections Performed ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Inspection Date
 +
!scope="col" style="text-align: center"| Inspection Type
 +
!scope="col" style="text-align: center"| Inspection Result
 +
!scope="col" style="text-align: center"| Inspection Comments
 +
|-
 +
| 1566938426
 +
| 2015-01-24
 +
| Casing String Witnessed
 +
| No Violations
 +
| I was on location to witness the cementing of the 13.375 surface casing.  Nomac Rig #71 spudded the surface hole on 1/23/15 and drilled a 17.5 hole to a depth of 636.  Wyoming Casing rigged up and ran  casing to a depth of 628.  The rig was losing circulation (municipal water) of approximately 20 barrels per hour at a depth of 170.  Schlumberger rigged up the cement head, tested the lines, and pumped 25 barrels of gel and 10 barrels of water ahead of the slurry.  They then mixed and pumped 126 barrels of cement slurry, dropped the plug, and displaced the plug to the collar with 90.4 barrels of water.  The plug landed at 316psi and the pressure was increased and held for 5 minutes at 975psi.  The pressure was released and the floats held with 0.25 barrels flowing back to the truck.  28 barrels of cement circulated to surface.  There were no circulation issues during the job and the cement held at surface.  See casing ticket for more details on this job.  No violations.
 +
|-
 +
| 1875471865
 
| 2014-10-22
 
| 2014-10-22
|  
+
| Administrative Inspection
 +
| No Violations
 
| I was on location with Chesapeake representatives Steven Rybicki, Matt Garrison, Seth Wehr, and landowner Dean Ott to conduct Pre-Construction site inspection #s APATT026047 and APATT026051 for the Dean Ott Pad and the Donna Ott Pad.  See Pre-Site inspection reports for site specific details on construction.
 
| I was on location with Chesapeake representatives Steven Rybicki, Matt Garrison, Seth Wehr, and landowner Dean Ott to conduct Pre-Construction site inspection #s APATT026047 and APATT026051 for the Dean Ott Pad and the Donna Ott Pad.  See Pre-Site inspection reports for site specific details on construction.
|  
+
|-
|  
+
| 2021917913
|  
+
| 2015-11-10
 +
| Preliminary Restoration
 +
| No Violations
 +
| I was on location to conduct a preliminary restoration inspection.  The well is open flow with a wellhead Christmas tree assembly.  Jersey barriers were installed around the wellhead.  The well is properly identified with a clear, legibly-marked well identification sign.  The tank battery consisted of eight, 400 BBL production tanks and was diked. The tanks are located within a spray-lined and sealed secondary containment.  There are e-stops outside the barriers, and the tanks are grounded, and have static dissipators.  There is a truck grounding area for trucks collecting condensate and/or produced water.  Lightning protection and a windsock are installed on top of the production tanks.  Other production equipment on the well pad consisted of:
 +
 
 +
 
 +
 
 +
 
 +
 
 +
Jersey barriers are installed around the production equipment.  The entire well pad is enclosed with a six-foot high, chain link fence with three-strand barbed wire and the man doors were locked.  Along the interior of the chain link fence there is an earthen berm and it was stable. The soil stockpile is well-stabilized with vegetation.  Drainage and erosion controls at the pad are in place and functioning.  A closed-loop, above-ground drilling pit system was used, so there are no earthen pits requiring closure.  The pad has a crushed limestone surface, and is in good repair.  The lease road is stable and drivable.  The well was in production at the time of this inspection, and the status needs changed in RBDMS from DR to PR.  Preliminary restoration passed.
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]
 +
[[Category:FracFocus]]

Revision as of 09:37, 31 July 2019

Well Details

Well ID: 34-019-22629
Loading map...
Country: United States
State: Ohio
County: Carroll
Municipality: Washington Township
Operator Name: CHESAPEAKE EXPLORATION LLC
Well Pad ID: US-OH-001167
Farm/Lease Name: DEAN OTT 7-14-5
License Status: Producing
License Date: 2015-01-14
Spud Date: 2015-01-07
Spud Drilling Contractor: NOMAC DRILLING CORP
Final Drill Date: 2015-01-31
Well Total Depth: 15859 ft
Configuration: Horizontal
Latitude: 40.572350768
Longitude: -81.01023699

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2014-11-04 Proposed Formations:TRENTON-BLACK RIVER, Issued Date:11/4/2014, Expired Date:11/3/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT
APP 2015-01-14 Proposed Formations:POINT PLEASANT, Issued Date:1/14/2015, Expired Date:1/13/2017 12:00:00 PM, Drilling unit acres:585.485, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2015-01-31
Correction to Well 2015-10-02 UPDATE TO SURFACE, TARGET AND TAKE-POINT INFORMATION (FOOTAGES AND COORDINATES) FROM NEW PLAT. UNIT SIZE UPDATED.
Completion Report Received 2015-12-17
Construction Permit Expires 2017-01-13
Record Last Modified 2017-10-23

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2015-12-17 8309 15706 835

For data sources see[3]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 05/23/2015 06/09/2015 7984 6,447,420.0 522306

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 100 Mesh Sand HEARTLAND SOLUTIONS Proppant - Natural Crystalline Silica (Quartz Sand, Silicon Dioxide) 014808-60-7 100 0.55798 0
Recycled Produced Water CHESAPEAKE ENERGY Carrier/Base Fluid Water 007732-18-5 100 0.59271 0
PTLGL240 PERFORMANCE TECHNOLOGIES Gelling Agent No Hazardous Components NONE 0 0 0
PTLFR200 PERFORMANCE TECHNOLOGIES Friction Reducer Proprietary Aliphatic Hydrocarbon TRADE SECRET 30 0.00912 0
Proprietary Oxyalkylated Alcohol TRADE SECRET 5 0.00152 0
OilSafe AR (Acid Replacement) 1:2 Dilution HEARTLAND SOLUTIONS Acid Water 007732-18-5 67 0.11569 0
Patented Synthetic Acid TRADE SECRET 33 0.05698 0
PTLBW112, PTLFR200, PTLGL240 PERFORMANCE TECHNOLOGIES Breaker, Friction Reducer, Gelling Agent Proprietary Aliphatic Alcohol TRADE SECRET 0 0.03247 0
Copper Sulfate 007758-98-7 0 0.00036 0
Guar Gum 009000-30-0 0 0.2022 0
Proprietary Clay TRADE SECRET 0 0.2022 0
Proprietary Vinyl Copolymer TRADE SECRET 0 0.03381 0
Tetrasodium Ethylenediaminetetraacetate 000064-02-8 0 0.03247 0
Sodium Chloride 007647-14-5 0 0.03247 0
Petroleum Distillate Hydrotreated Light 064742-47-8 0 0.2022 0
Proprietary Substituted Fatty Acid Ester TRADE SECRET 0 0.03247 0
Proprietary Oxyalkylated Fatty Acid Derivative TRADE SECRET 0 0.03247 0
Proprietary Surfactant TRADE SECRET 0 0.2022 0
Water 007732-18-5 0 0.03247 0
PTLCA102 PERFORMANCE TECHNOLOGIES Cross Linker Proprietary Inorganic Salt TRADE SECRET 30 0.01299 0
Sodium Hydroxide 001310-73-2 60 0.02598 0
Proprietary Alkyl Alcohol TRADE SECRET 60 0.02598 0
Chlorine Dioxide TERRA SERVICES Anti-Bacterial Agent Chlorine Dioxide 010049-04-4 100 0.00837 0
TS-30 X CHEM Scale Inhibitor Proprietary Sodium Polycarboxylate TRADE SECRET 100 0.00953 0
Water 007732-18-5 0 0.01145 0
Fresh Water CHESAPEAKE ENERGY Carrier/Base Fluid Water 007732-18-5 100 82.2732 0
PTLBW112 PERFORMANCE TECHNOLOGIES Breaker Ammonium Persulfate 007727-54-0 100 0.00279 0
Northern White Sand HEARTLAND SOLUTIONS Proppant - Natural Crystalline Silica (Quartz Sand, Silicon Dioxide) 014808-60-7 100 16.1407 0

For data sources see[4]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2015-05-23 H2O 0 3917 Bbl 330200 STAGE 33/33
2015-05-23 H2O 0 1515 Bbl 329780 STAGE 1/33

25 SHOTS STAGES 2-32 SEE IMAGES

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2015 CHESAPEAKE EXPLORATION LLC 454055 15162 114
2016 CHESAPEAKE EXPLORATION LLC 843796 8609 366
2017 CHESAPEAKE EXPLORATION LLC 448309 2269 365
2018 CHESAPEAKE EXPLORATION LLC 324278 1272 365
2019 CHESAPEAKE EXPLORATION LLC 67902 254 90

For data sources see[6] [7]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2015 CHESAPEAKE EXPLORATION LLC Brine 18343 114
2016 CHESAPEAKE EXPLORATION LLC Brine 8887 366
2017 CHESAPEAKE EXPLORATION LLC Brine 3937 365
2018 CHESAPEAKE EXPLORATION LLC Brine 3278 365
2019 CHESAPEAKE EXPLORATION LLC Brine 656 90

For data sources see[8] [9]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1566938426 2015-01-24 Casing String Witnessed No Violations I was on location to witness the cementing of the 13.375 surface casing. Nomac Rig #71 spudded the surface hole on 1/23/15 and drilled a 17.5 hole to a depth of 636. Wyoming Casing rigged up and ran casing to a depth of 628. The rig was losing circulation (municipal water) of approximately 20 barrels per hour at a depth of 170. Schlumberger rigged up the cement head, tested the lines, and pumped 25 barrels of gel and 10 barrels of water ahead of the slurry. They then mixed and pumped 126 barrels of cement slurry, dropped the plug, and displaced the plug to the collar with 90.4 barrels of water. The plug landed at 316psi and the pressure was increased and held for 5 minutes at 975psi. The pressure was released and the floats held with 0.25 barrels flowing back to the truck. 28 barrels of cement circulated to surface. There were no circulation issues during the job and the cement held at surface. See casing ticket for more details on this job. No violations.
1875471865 2014-10-22 Administrative Inspection No Violations I was on location with Chesapeake representatives Steven Rybicki, Matt Garrison, Seth Wehr, and landowner Dean Ott to conduct Pre-Construction site inspection #s APATT026047 and APATT026051 for the Dean Ott Pad and the Donna Ott Pad. See Pre-Site inspection reports for site specific details on construction.
2021917913 2015-11-10 Preliminary Restoration No Violations I was on location to conduct a preliminary restoration inspection. The well is open flow with a wellhead Christmas tree assembly. Jersey barriers were installed around the wellhead. The well is properly identified with a clear, legibly-marked well identification sign. The tank battery consisted of eight, 400 BBL production tanks and was diked. The tanks are located within a spray-lined and sealed secondary containment. There are e-stops outside the barriers, and the tanks are grounded, and have static dissipators. There is a truck grounding area for trucks collecting condensate and/or produced water. Lightning protection and a windsock are installed on top of the production tanks. Other production equipment on the well pad consisted of:



Jersey barriers are installed around the production equipment. The entire well pad is enclosed with a six-foot high, chain link fence with three-strand barbed wire and the man doors were locked. Along the interior of the chain link fence there is an earthen berm and it was stable. The soil stockpile is well-stabilized with vegetation. Drainage and erosion controls at the pad are in place and functioning. A closed-loop, above-ground drilling pit system was used, so there are no earthen pits requiring closure. The pad has a crushed limestone surface, and is in good repair. The lease road is stable and drivable. The well was in production at the time of this inspection, and the status needs changed in RBDMS from DR to PR. Preliminary restoration passed.

For data sources see[10]

References