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Difference between revisions of "34-029-21633"

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| County: [[Columbiana_County,_Ohio|Columbiana]]
 
| County: [[Columbiana_County,_Ohio|Columbiana]]
 
|-
 
|-
| Municipality: [[Madison_Township,_Columbiana_County,_Ohio|Madison Township]]
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| Municipality: [[Madison Township,_Columbiana_County,_Ohio|Madison Township]]
 
|-
 
|-
 
| Operator Name: [[WILKES ENERGY INC]]
 
| Operator Name: [[WILKES ENERGY INC]]
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| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Latitude: 40.674307017
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| Latitude: <Latitude>
 
|-
 
|-
 
| Longitude: -80.66385191
 
| Longitude: -80.66385191

Revision as of 18:17, 12 August 2019

Well Details

Well ID: 34-029-21633
Loading map...
Country: United States
State: Ohio
County: Columbiana
Municipality: Madison Township
Operator Name: WILKES ENERGY INC
Well Pad ID:
Farm/Lease Name: STEVENS UNIT
License Status: Producing
License Date: 2005-02-23
Spud Date: 2005-02-28
Spud Drilling Contractor: LAND & SHORE DRILLING, LTD
Final Drill Date: 2005-03-04
Well Total Depth: 904 ft
Configuration: Vertical
Latitude: <Latitude>
Longitude: -80.66385191

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2004-11-30 Proposed Formations:BEREA, Issued Date:11/30/2004, Expired Date:11/30/2005 6:00:00 AM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:POOL
APP 2005-02-23 Proposed Formations:BEREA, Issued Date:2/23/2005, Expired Date:2/23/2006 6:00:00 AM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:POOL
Original Spud 2005-02-28
Completed 2005-03-04
Reached Total Depth 2005-03-04
Construction Permit Expires 2006-02-23
Completion Report Received 2006-05-30
Change of Owner 2011-10-11 Operator changed from 7528, E SERVICES to 6805, GAS ACQUISITION COMPANY LTD
Change of Owner 2012-05-10 Operator changed from 6805, GAS ACQUISITION COMPANY LTD to 3954, WILKES ENERGY INC
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-08-15 726 750 98

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 15 1000 Gal 0 1500 GALLONS FE ACID

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2011 WILKES ENERGY INC 186 0 90
2012 WILKES ENERGY INC 656 0 90
2013 WILKES ENERGY INC 184 0 90
2014 WILKES ENERGY INC 123 0 90
2015 WILKES ENERGY INC 38 0 90
2016 WILKES ENERGY INC 3 0 90
2017 WILKES ENERGY INC 0 0 90

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2011 WILKES ENERGY INC Brine 0 90
2012 WILKES ENERGY INC Brine 0 90
2013 WILKES ENERGY INC Brine 0 90
2014 WILKES ENERGY INC Brine 0 90
2015 WILKES ENERGY INC Brine 0 90
2016 WILKES ENERGY INC Brine 0 90
2017 WILKES ENERGY INC Brine 0 90

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0701170563 2009-04-09 Preliminary Restoration No Violations Inspection revealed that the preliminary restoration can be approved at this time. No violations at this time.
1110385292 2005-03-02 Drill / Deepen / Reopen No Violations Arrived for a surface job. Difficulty drilling. Departed and returned 1.5 hours later. Observed the surface job.
1336117747 2016-11-17 Production Wells No Violations The purpose of my inspection was to conduct a status check on well # 2-1633. RBDMS indicates the operator is current with reporting production. The well is located in the backyard of a residence. Correct and legible identification is present at the well head. The 8.625 surface casing head is above grade and contains a plug in one side and a valve open to atmosphere on the other. The 4.5 production casing is swaged down to 2 and produced open flow. No audible or visual leaks were observed. A domestic supply connection is present. Production equipment consists of a line drip and digital sales meter. A gauge on the drip indicated 27#/ The drip was plumbed to a 305 gallon poly tank that contained production fluid. The tank remained in good repair with cracks or leaks. A plug was installed in the bottom of the tank. No violations were observed during this inspection.
1546007843 2006-05-31 Preliminary Restoration No Violations Meets requirements for preliminary restoration.

For data sources see[9]

References