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Difference between revisions of "37-003-01032"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-003-01032
 
| Well ID: 37-003-01032
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.518272, -79.843939 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.518272, -79.843939 | width=100% | height=100% }}
 
|-
 
|-
 
| Country: United States
 
| Country: United States
Line 19: Line 19:
 
| Farm/Lease Name: SCAIFE 1
 
| Farm/Lease Name: SCAIFE 1
 
|-
 
|-
| License Status: Active
+
| License Status: ACTIVE
 
|-
 
|-
| Spud Date: 1800-01-01
+
| Spud Date:  
 
|-
 
|-
 
| Permit Date:  
 
| Permit Date:  
 +
|-
 +
| Well Type: GAS
 
|-
 
|-
 
| Unconventional Well: N
 
| Unconventional Well: N
 
|-
 
|-
 
| Configuration: Vertical Well
 
| Configuration: Vertical Well
 +
|-
 +
| Conservation: No
 
|-
 
|-
 
| Latitude: 40.518272
 
| Latitude: 40.518272
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  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | accessdate = 2019-05-21 }}</ref>
 
  | accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Date
 +
!scope="col" | Event
 +
|-
 +
| 1901-01-01
 +
| Drilling Completion
 +
|-
 +
| 1993-01-01
 +
| OLD WELL
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Compiled from multiple data sources - see Pennsylvania Oil and Gas Data Sources
 +
| date = 2020-02-27
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-02-27 }}</ref>
 
<!--== Fracking Activities ==
 
<!--== Fracking Activities ==
 
==== Fracking Jobs ====
 
==== Fracking Jobs ====
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!scope="col" | Job Percentage by Mass
 
!scope="col" | Job Percentage by Mass
 
!scope="col" | Mass Used (lb)
 
!scope="col" | Mass Used (lb)
 +
|-
 +
|}-->
 +
 +
<!--== Stimulation Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Stimulation Date
 +
!scope="col" | Phase Number
 +
!scope="col" | Chemical Agent
 +
!scope="col" | Volume (gal)
 +
!scope="col" | Treating Pressure (psi)
 +
!scope="col" | Breakdown Pressure (psi)
 
|-
 
|-
 
|}-->
 
|}-->
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| 1998
 
| 1998
 
| [[VERNARD L SHUMAKER]]
 
| [[VERNARD L SHUMAKER]]
| style="text-align: right;" | 34,243.00
+
| style="text-align: right;" | 34243
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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| 1999
 
| 1999
 
| [[VERNARD L SHUMAKER]]
 
| [[VERNARD L SHUMAKER]]
| style="text-align: right;" | 44,975.00
+
| style="text-align: right;" | 44975
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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| 2000
 
| 2000
 
| [[VERNARD L SHUMAKER]]
 
| [[VERNARD L SHUMAKER]]
| style="text-align: right;" | 42,671.00
+
| style="text-align: right;" | 42671
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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| 2001
 
| 2001
 
| [[VERNARD L SHUMAKER]]
 
| [[VERNARD L SHUMAKER]]
| style="text-align: right;" | 18,865.00
+
| style="text-align: right;" | 18865
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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| 2002
 
| 2002
 
| [[VERNARD L SHUMAKER]]
 
| [[VERNARD L SHUMAKER]]
| style="text-align: right;" | 20,076.00
+
| style="text-align: right;" | 20076
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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| 2003
 
| 2003
 
| [[VERNARD L SHUMAKER]]
 
| [[VERNARD L SHUMAKER]]
| style="text-align: right;" | 17,646.00
+
| style="text-align: right;" | 17646
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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| 2004
 
| 2004
 
| [[VERNARD L SHUMAKER]]
 
| [[VERNARD L SHUMAKER]]
| style="text-align: right;" | 18,560.00
+
| style="text-align: right;" | 18560
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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| 2005
 
| 2005
 
| [[VERNARD L SHUMAKER]]
 
| [[VERNARD L SHUMAKER]]
| style="text-align: right;" | 18,795.00
+
| style="text-align: right;" | 18795
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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| 2007
 
| 2007
 
| [[VERNARD L SHUMAKER]]
 
| [[VERNARD L SHUMAKER]]
| style="text-align: right;" | 17,467.00
+
| style="text-align: right;" | 17467.00
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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| 2009
 
| 2009
 
| [[VERNARD L SHUMAKER]]
 
| [[VERNARD L SHUMAKER]]
| style="text-align: right;" | 14,947.00
+
| style="text-align: right;" | 14947.00
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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|-
 
|-
 
|}
 
|}
==== Penalties Applied ====
+
<!--==== Penalties Applied ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | Violation ID
 
!scope="col" | Violation ID
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!scope="col" | Amount Collected
 
!scope="col" | Amount Collected
 
|-
 
|-
| 841263
+
|}-->
| 372132
 
| NOV - Notice of Violation
 
|
 
|
 
|
 
| style="text-align: right;" |
 
| style="text-align: right;" |
 
|-
 
| 841264
 
| 372132
 
| NOV - Notice of Violation
 
|
 
|
 
|
 
| style="text-align: right;" |
 
| style="text-align: right;" |
 
|-
 
|}
 
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
 
  | title =Oil and Gas Compliance Report
 
  | title =Oil and Gas Compliance Report

Latest revision as of 10:13, 20 May 2020

Well Details

Well ID: 37-003-01032
Loading map...
Country: United States
State: Pennsylvania
County: Allegheny
Municipality: Oakmont Borough
Operator Name: VERNARD L SHUMAKER
Well Pad ID:
Farm/Lease Name: SCAIFE 1
License Status: ACTIVE
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.518272
Longitude: -79.843939

For data sources see[1][2][3]

Well History

Date Event
1901-01-01 Drilling Completion
1993-01-01 OLD WELL

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1998 VERNARD L SHUMAKER 34243 365 0.00 0 0.00 0
1999 VERNARD L SHUMAKER 44975 365 0.00 0 0.00 0
2000 VERNARD L SHUMAKER 42671 365 0.00 0 0.00 0
2001 VERNARD L SHUMAKER 18865 365 0.00 0 0.00 0
2002 VERNARD L SHUMAKER 20076 365 0.00 0 0.00 0
2003 VERNARD L SHUMAKER 17646 365 0.00 0 0.00 0
2004 VERNARD L SHUMAKER 18560 365 0.00 0 0.00 0
2005 VERNARD L SHUMAKER 18795 365 0.00 0 0.00 0
2007 VERNARD L SHUMAKER 17467.00 365 0.00 0 0.00 0
2009 VERNARD L SHUMAKER 14947.00 365 0.00 0 0.00 0
2010 VERNARD L SHUMAKER 32,514.00 365 0.00 0 0.00 0
2012 VERNARD L SHUMAKER 14,861.00 365 0.00 0 0.00 0
2013 VERNARD L SHUMAKER 28,929.00 365 0.00 0 0.00 0
2014 VERNARD L SHUMAKER 27,426.00 365 0.00 0 0.00 0
2015 VERNARD L SHUMAKER 27,906.00 365 0.00 0 0.00 0
2016 VERNARD L SHUMAKER 25,935.00 365 0.00 0 0.00 0
2017 VERNARD L SHUMAKER 16,963.00 365 0.00 0 0.00 0
2018 VERNARD L SHUMAKER 19,227.00 365 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
1999 VERNARD L SHUMAKER Brine 0.01 Bbl Other UNK
2000 VERNARD L SHUMAKER Brine 0.01 Bbl Other
2002 VERNARD L SHUMAKER Brine 0.01 Bbl Brine or Industrial Waste Treatment Plt PA0091472
2003 VERNARD L SHUMAKER Brine 0.25 Bbl Brine or Industrial Waste Treatment Plt
2004 VERNARD L SHUMAKER Brine 0.04 Bbl Brine or Industrial Waste Treatment Plt
2005 VERNARD L SHUMAKER Brine 0.04 Bbl Brine or Industrial Waste Treatment Plt

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
217274 Primary Facility 1995-11-30 Routine/Complete Inspection No Violations Noted OPERATING WELL; NO TANKS
221819 Primary Facility 1999-07-21 Routine/Complete Inspection No Violations Noted OPERATING WELL
2826139 Primary Facility 2018-12-07 Routine/Complete Inspection Pending Visited site after report of possible abandoned well across alley behind Oakmont Bakery. Well is 2 3/8" tubing, ~2 feet high, teed to side with capped valve, topped with valve, swaged to 1/2" valve with plug. Disconnected from sales line. Equitable Gas line is 10' from wellhead. Wellhead has a few minor gas leaks, maximum Bascom Turner reading was 340 PPM.

Wellsite is ~ 15' X 25', flat, grassy area. Well is about 5' from small parking lot, 10' from corner of nearest building. Power lines extend to nearby building overhead and are offset ~5' from wellhead.

2836937 Primary Facility 2019-02-07 Administrative/File Review Violation(s) Noted In response to Inspection 2826139 Pending. The well is disconnected from production.
2840707 Primary Facility 2019-02-15 Routine/Complete Inspection Pending Visited site to take additional gas readings. Weather is 54 degrees, sunny and breezy. No gas detected in ambient air. Small, variable gas leak detected at ground level from tubing at tubing head: 7020 PPM maximum.
2841491 Primary Facility 2019-02-11 Routine/Partial Inspection Pending Met operator at well site to go over plans for this shut-in gas well. The operator stated that he was going to test the well and decide by the end of the week if he can produce the well. If the well is not able to be put back into production he said he would start the paper work to plug it.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2836937 841263 2018-12-07 OGA3220(A) Environmental Health & Safety
2836937 841264 2018-12-07 78.91(a) Environmental Health & Safety

For data sources see[7]

References