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Difference between revisions of "37-049-22960"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-049-22960
 
| Well ID: 37-049-22960
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.909126, -80.006005 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.909126, -80.006005 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Erie County, Pennsylvania|Erie]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Pennsylvania
 
|-
 
|-
| Operator Name: [[MITCH WELL ENERGY INC]]
+
| County: [[Erie_County,_Pennsylvania|Erie]]
 +
|-
 +
| Municipality: [[Le Boeuf Township,_Erie_County,_Pennsylvania|Le Boeuf Township]]
 +
|-
 +
| Operator Name:
 
|-
 
|-
 
| Well Pad ID:  
 
| Well Pad ID:  
Line 15: Line 19:
 
| Farm/Lease Name: WALTER K & AINO RINNE 3
 
| Farm/Lease Name: WALTER K & AINO RINNE 3
 
|-
 
|-
| First Permit Date: 1983-05-12
+
| License Status: PLUGGED & ABANDONED
 
|-
 
|-
| Last Permit Date: 1983-05-12
+
| Spud Date:  
 
|-
 
|-
| Spud Date: 1983-12-19
+
| Permit Date: 1983-05-12
 
|-
 
|-
| Unconventional: No
+
| Well Type: GAS
 
|-
 
|-
| Horizontal: No
+
| Unconventional Well: N
 
|-
 
|-
| Well Status:
+
| Configuration: Vertical Well
 
|-
 
|-
| Violations: 2
+
| Conservation: Yes
 
|-
 
|-
 
| Latitude: 41.909126
 
| Latitude: 41.909126
 
|-
 
|-
 
| Longitude: -80.006005
 
| Longitude: -80.006005
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Permits Issued Detail Report
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-05-20
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref><ref>{{cite web
 +
| title = Spud Data Report
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-04-30
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-16 }}</ref><ref>{{cite web
 +
| title = Oil and Gas Well Pad Report
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-05-20
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Date
 +
!scope="col" | Event
 +
|-
 +
| 1983-05-12
 +
| New Permit Application
 +
|-
 +
| 1983-12-19
 +
| Performed Spud Operation
 +
|-
 +
| 1983-12-24
 +
| Drilling Completion
 +
|-
 +
| 1983-12-28
 +
| Perforation
 +
|-
 +
| 1983-12-29
 +
| Performed Stimulation 
 +
|-
 +
| 1984-06-13
 +
| NEWLY DRILLED
 +
|-
 +
| 1989-12-14
 +
| Drilling Completion
 +
|-
 +
| 1989-12-14
 +
| FULLY PLUGGED
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Compiled from multiple data sources - see Pennsylvania Oil and Gas Data Sources
 +
| date = 2020-02-27
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-02-27 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Job Number
 +
!scope="col" | Job Start Date
 +
!scope="col" | Job End Date
 +
!scope="col" | True Vertical Depth (ft)
 +
!scope="col" | Total Water Volume (gal)
 +
!scope="col" | Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" | Job Number
!scope="col" | GAS QUANTITY
+
!scope="col" | Trade Name
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" | Supplier
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" | Purpose
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" | Ingredient Name
!scope="col" | OIL QUANTITY
+
!scope="col" | CAS Number
!scope="col" | OIL PRODUCTION DAYS
+
!scope="col" | Additive Percentage by Mass
 +
!scope="col" | Job Percentage by Mass
 +
!scope="col" | Mass Used (lb)
 
|-
 
|-
| 1984-0
+
|}-->
| style="text-align:right;" | 8794.0
+
 
| style="text-align:right;" | 0.0
+
== Stimulation Data ==
| style="text-align:right;" | 0.0
+
{| class="wikitable sortable" width="95%"
| style="text-align:right;" | 0.0
+
!scope="col" | Stimulation Date
| style="text-align:right;" | 0.0
+
!scope="col" | Phase Number
| style="text-align:right;" | 0.0
+
!scope="col" | Chemical Agent
 +
!scope="col" | Volume (gal)
 +
!scope="col" | Treating Pressure (psi)
 +
!scope="col" | Breakdown Pressure (psi)
 +
|-
 +
| 1983-12-29
 +
| style="text-align: right;" |  
 +
 
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Oil and Gas Historical Production Report
+
  | title = Completion Reports - Stimulations
  | publisher = [[Pennsylvania Department of Environmental Protection]]
+
  | publisher = Pennsylvania Department of Conservation and Natural Resources
| date = 2015-05-26
+
| date = 2020-03-02
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources#Production
+
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
  | accessdate = 2015-05-27 }}</ref>
+
  | accessdate = 2020-03-02 }}</ref>
== Waste Data ==
+
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" | Period
!scope="col" | TYPE
+
!scope="col" | Operator Name
!scope="col" | QUANTITY
+
!scope="col" | Gas Quantity (mcf)
!scope="col" | UNITS
+
!scope="col" | Gas Production Days
!scope="col" | DISPOSAL METHOD
+
!scope="col" | Oil Quantity (bbl)
!scope="col" | WASTE FACILITY PERMIT ID
+
!scope="col" | Oil Production Days
!scope="col" | WASTE FACILITY NAME
+
!scope="col" | Water Quantity (bbl)
!scope="col" | FACILITY CITY
+
!scope="col" | Water Production Days
!scope="col" | FACILITY STATE
+
|-
 +
| 1984
 +
| [[MITCH WELL ENERGY INC]]
 +
| style="text-align: right;" | 8,794.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Oil and Gas Historical Waste Report
+
  | title =Oil and Gas Production Reports
| publisher = [[Pennsylvania Department of Environmental Protection]]
+
|publisher = [[Pennsylvania Department of Environmental Protection]]
| date = 2015-05-26
+
| date = 2019-03-31
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources#Waste
+
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
  | accessdate = 2015-05-26 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
 +
<!--== Waste Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Period
 +
!scope="col" | Operator
 +
!scope="col" | Waste Type
 +
!scope="col" | Quantity
 +
!scope="col" | Disposal Method
 +
!scope="col" | Waste Facility ID
 +
|-
 +
|}-->
 +
 
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" | Inspection ID
!scope="col" | DATE
+
!scope="col" | Inspection Category
!scope="col" | DESCRIPTION
+
!scope="col" | Inspection Date
!scope="col" | COMMENT
+
!scope="col" | Inspection Type
!scope="col" | VIOLATION ID
+
!scope="col" | Inspection Result
!scope="col" | VIOLATION CODE
+
!scope="col" | Inspection Comments
!scope="col" | VIOLATION_COMMENT
+
|-
 +
| 1833051
 +
| Primary Facility
 +
| 2009-09-17
 +
| Routine/Complete Inspection
 +
| No Violations Noted
 +
|
 +
|-
 +
| 1964783
 +
| Primary Facility
 +
| 2011-04-11
 +
| Routine/Complete Inspection
 +
| Violation(s) Noted
 +
| Today Scott Lux and I inspected this gas well and found a 10" casing , protruding up from the grown about 18". The casing was open and filled to the surface with clear water. There was no production equipment on-site.
 
|-
 
|-
 
| 362236
 
| 362236
 +
| Primary Facility
 
| 1989-12-13
 
| 1989-12-13
 +
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
|
 
|
 
|
 
 
|  
 
|  
|-
 
 
|-
 
|-
 
| 362237
 
| 362237
 +
| Primary Facility
 
| 1989-12-14
 
| 1989-12-14
 +
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
 
|  
 
|  
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 364989
 
| 364989
 +
| Primary Facility
 
| 1990-03-08
 
| 1990-03-08
 +
| Routine/Complete Inspection
 
| Violation(s) Noted
 
| Violation(s) Noted
|
 
| 89267
 
| 201TAG - Failure to install, in a permanent manner, the permit number on a completed well
 
 
|  
 
|  
 
|-
 
|-
 +
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Inspection ID
 +
!scope="col" | Violation ID
 +
!scope="col" | Violation Date
 +
!scope="col" | Date Resolved
 +
!scope="col" | Violation Code
 +
!scope="col" | Violation Type
 +
!scope="col" | Violation Comments
 
|-
 
|-
| 1833051
+
| 1964783
| 2009-09-17
+
| 608624
| No Violations Noted
+
| 04/11/2011
|  
+
| 2011-04-11
|  
+
| 210UNPLUG - Failure to plug a well upon abandonment
 +
| Administrative
 
|  
 
|  
 +
|-
 +
| 364989
 +
| 89267
 +
| 03/08/1990
 +
| 1990-03-08
 +
| 201TAG - Failure to install, in a permanent manner, the permit number on a completed well
 +
| Administrative
 
|  
 
|  
 
|-
 
|-
 +
|}
 +
==== Penalties Applied ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Violation ID
 +
!scope="col" | Penalty ID
 +
!scope="col" | Penalty Code
 +
!scope="col" | Penalty Status
 +
!scope="col" | Penalty Date
 +
!scope="col" | Enforcement Date
 +
!scope="col" | Penalty Amount
 +
!scope="col" | Amount Collected
 
|-
 
|-
| 1964783
 
| 2011-04-11
 
| Violation(s) Noted
 
| Today Scott Lux and I inspected this gas well and found a 10" casing , protruding up from the grown about 18". The casing was open and filled to the surface with clear water. There was no production equipment on-site.
 
 
This abandon well is a vilation 210UNPlUGGED. A NOV will be sent.
 
 
| 608624
 
| 608624
| 210UNPLUG - Failure to plug a well upon abandonment
+
| 269756
 +
| NOV - Notice of Violation
 +
| Superseded
 
|  
 
|  
 +
| 2013-01-29
 +
| style="text-align: right;" |
 +
| style="text-align: right;" |
 
|-
 
|-
|-
 
| 1964783
 
| 2011-04-11
 
| Violation(s) Noted
 
| Today Scott Lux and I inspected this gas well and found a 10" casing , protruding up from the grown about 18". The casing was open and filled to the surface with clear water. There was no production equipment on-site.
 
 
This abandon well is a vilation 210UNPlUGGED. A NOV will be sent.
 
 
| 608624
 
| 608624
| 210UNPLUG - Failure to plug a well upon abandonment
+
| 292029
 +
| ADORD - Administrative Order
 +
| Superseded
 
|  
 
|  
 +
| 2013-01-29
 +
| style="text-align: right;" |
 +
| style="text-align: right;" |
 
|-
 
|-
|-
 
| 1964783
 
| 2011-04-11
 
| Violation(s) Noted
 
| Today Scott Lux and I inspected this gas well and found a 10" casing , protruding up from the grown about 18". The casing was open and filled to the surface with clear water. There was no production equipment on-site.
 
 
This abandon well is a vilation 210UNPlUGGED. A NOV will be sent.
 
 
| 608624
 
| 608624
| 210UNPLUG - Failure to plug a well upon abandonment
+
| 294448
 +
| ADORD - Administrative Order
 +
|
 +
|
 
|  
 
|  
 +
| style="text-align: right;" |
 +
| style="text-align: right;" |
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Oil and Gas Historical Inspection Report
+
  | title =Oil and Gas Compliance Report
| publisher = [[Pennsylvania Department of Environmental Protection]]
+
|publisher = [[Pennsylvania Department of Environmental Protection]]
| date = 2015-05-26
+
| date = 2019-05-20
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources#Inspections
+
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
  | accessdate = 2015-05-27 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Pennsylvania Wells]]

Latest revision as of 14:15, 2 June 2020

Well Details

Well ID: 37-049-22960
Loading map...
Country: United States
State: Pennsylvania
County: Erie
Municipality: Le Boeuf Township
Operator Name:
Well Pad ID:
Farm/Lease Name: WALTER K & AINO RINNE 3
License Status: PLUGGED & ABANDONED
Spud Date:
Permit Date: 1983-05-12
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: Yes
Latitude: 41.909126
Longitude: -80.006005

For data sources see[1][2][3]

Well History

Date Event
1983-05-12 New Permit Application
1983-12-19 Performed Spud Operation
1983-12-24 Drilling Completion
1983-12-28 Perforation
1983-12-29 Performed Stimulation
1984-06-13 NEWLY DRILLED
1989-12-14 Drilling Completion
1989-12-14 FULLY PLUGGED

For data sources see[4]

Stimulation Data

Stimulation Date Phase Number Chemical Agent Volume (gal) Treating Pressure (psi) Breakdown Pressure (psi)
1983-12-29 0 0 0

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1984 MITCH WELL ENERGY INC 8,794.00 0 0.00 0 0.00 0

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1833051 Primary Facility 2009-09-17 Routine/Complete Inspection No Violations Noted
1964783 Primary Facility 2011-04-11 Routine/Complete Inspection Violation(s) Noted Today Scott Lux and I inspected this gas well and found a 10" casing , protruding up from the grown about 18". The casing was open and filled to the surface with clear water. There was no production equipment on-site.
362236 Primary Facility 1989-12-13 Plugging(Includes Plugged/Mined Through) No Violations Noted
362237 Primary Facility 1989-12-14 Plugging(Includes Plugged/Mined Through) No Violations Noted
364989 Primary Facility 1990-03-08 Routine/Complete Inspection Violation(s) Noted

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
1964783 608624 04/11/2011 2011-04-11 210UNPLUG - Failure to plug a well upon abandonment Administrative
364989 89267 03/08/1990 1990-03-08 201TAG - Failure to install, in a permanent manner, the permit number on a completed well Administrative

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
608624 269756 NOV - Notice of Violation Superseded 2013-01-29
608624 292029 ADORD - Administrative Order Superseded 2013-01-29
608624 294448 ADORD - Administrative Order

For data sources see[7]

References