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Difference between revisions of "37-115-20205"

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__TOC__
 
== Well Details ==
 
== Well Details ==
{| class="wikitable" width="95%"
+
{| class="wikitable welldetails" width="95%"
| Well ID: 42-115-20205
+
| Well ID: 37-115-20205
| style="width: 50%; height=100%; align=center" rowspan="14" | {{#display_map: 41.976791, -75.779855 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.976792, -75.779855 | width=100% | height=100% }}
 +
|-
 +
| Country: United States
 +
|-
 +
| State: Pennsylvania
 +
|-
 +
| County: [[Susquehanna_County,_Pennsylvania|Susquehanna]]
 +
|-
 +
| Municipality: [[Liberty Township,_Susquehanna_County,_Pennsylvania|Liberty Township]]
 +
|-
 +
| Operator Name: [[XPR RESOURCES LLC]]
 
|-
 
|-
| County: [[Susquehanna County, Pennsylvania|Susquehanna]]
+
| Well Pad ID:  
 
|-
 
|-
| Municipality: [[Liberty Township, Susquehanna County, Pennsylvania|Liberty Township]]
+
| Farm/Lease Name: CARTY 1H
 
|-
 
|-
| Operator Name: [[WPX ENERGY APPALACHIA LLC|WPX ENERGY APPALACHIA LLC]]
+
| License Status:  
 
|-
 
|-
| First Permit Date: 2009-08-24
+
| Spud Date:  
 
|-
 
|-
| Last Permit Date: 2009-08-24
+
| Permit Date: 2009-08-24
 
|-
 
|-
| Spud Date: None
+
| Well Type: GAS
 
|-
 
|-
| Unconventional: Yes
+
| Unconventional Well: Y
 
|-
 
|-
| Horizontal: Yes
+
| Configuration: Horizontal Well
 
|-
 
|-
| Violations: 1
+
| Conservation: No
 
|-
 
|-
| Latitude: 41.976791
+
| Latitude: 41.976792
 
|-
 
|-
 
| Longitude: -75.779855
 
| Longitude: -75.779855
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Permits Issued Detail Report
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-05-20
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref><ref>{{cite web
 +
| title = Spud Data Report
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-04-30
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-16 }}</ref><ref>{{cite web
 +
| title = Oil and Gas Well Pad Report
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-05-20
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Date
 +
!scope="col" | Event
 +
|-
 +
| 2009-08-24
 +
| New Permit Application
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Compiled from multiple data sources - see Pennsylvania Oil and Gas Data Sources
 +
| date = 2020-02-27
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-02-27 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Job Number
 +
!scope="col" | Job Start Date
 +
!scope="col" | Job End Date
 +
!scope="col" | True Vertical Depth (ft)
 +
!scope="col" | Total Water Volume (gal)
 +
!scope="col" | Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Job Number
 +
!scope="col" | Trade Name
 +
!scope="col" | Supplier
 +
!scope="col" | Purpose
 +
!scope="col" | Ingredient Name
 +
!scope="col" | CAS Number
 +
!scope="col" | Additive Percentage by Mass
 +
!scope="col" | Job Percentage by Mass
 +
!scope="col" | Mass Used (lb)
 +
|-
 +
|}-->
 +
 +
<!--== Stimulation Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Stimulation Date
 +
!scope="col" | Phase Number
 +
!scope="col" | Chemical Agent
 +
!scope="col" | Volume (gal)
 +
!scope="col" | Treating Pressure (psi)
 +
!scope="col" | Breakdown Pressure (psi)
 +
|-
 +
|}-->
 +
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Period
 +
!scope="col" | Operator Name
 +
!scope="col" | Gas Quantity (mcf)
 +
!scope="col" | Gas Production Days
 +
!scope="col" | Oil Quantity (bbl)
 +
!scope="col" | Oil Production Days
 +
!scope="col" | Water Quantity (bbl)
 +
!scope="col" | Water Production Days
 +
|-
 +
| 2010
 +
| [[XPR RESOURCES LLC]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
 
|}
 
|}
__TOC__
+
For data sources see<ref>{{cite web
== Well Inspection Data ==
+
| title =Oil and Gas Production Reports
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-03-31
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Waste Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Period
 +
!scope="col" | Operator
 +
!scope="col" | Waste Type
 +
!scope="col" | Quantity
 +
!scope="col" | Disposal Method
 +
!scope="col" | Waste Facility ID
 +
|-
 +
|}-->
 +
 
 +
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" | Inspection ID
!scope="col" | DATE
+
!scope="col" | Inspection Category
!scope="col" | DESCRIPTION
+
!scope="col" | Inspection Date
!scope="col" | COMMENT
+
!scope="col" | Inspection Type
!scope="col" | VIOLATION ID
+
!scope="col" | Inspection Result
 +
!scope="col" | Inspection Comments
 
|-
 
|-
 
| 2002311
 
| 2002311
 +
| Primary Facility
 
| 2011-09-13
 
| 2011-09-13
 +
| Drilling/Alteration
 
| Violation(s) Noted
 
| Violation(s) Noted
 
| At the time of inspection, I inspected the cellar of the well.  Standing fluid was present in the cellar up around the base of the well head.  Consistent bubbling was observed between the 9 x 13 annulus.  The Operator did not report the defect to the Department.
 
| At the time of inspection, I inspected the cellar of the well.  Standing fluid was present in the cellar up around the base of the well head.  Consistent bubbling was observed between the 9 x 13 annulus.  The Operator did not report the defect to the Department.
| 620052
+
|-
 +
| 2625142
 +
| Primary Facility
 +
| 2017-08-11
 +
| Routine/Complete Inspection
 +
| No Violations Noted
 +
| The Department arrived on site at the WR 77- Carty Well Site to conduct a Routine Complete Inspection.  A review of the E&S Inspection Log indicated that the most recent inspection was conducted on 8/7/17 with the note "monitor rills".
 +
 
 +
The status of this well is "Operator Reported Not Drilled".
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
==== Violations Commited ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" | Inspection ID
!scope="col" | GAS QUANTITY
+
!scope="col" | Violation ID
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" | Violation Date
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" | Date Resolved
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" | Violation Code
!scope="col" | OIL QUANTITY
+
!scope="col" | Violation Type
!scope="col" | OIL PRODUCTION DAYS
+
!scope="col" | Violation Comments
 
|-
 
|-
| 2010-2
+
| 2002311
| style="text-align:right;" | 0.0
+
| 620052
| style="text-align:right;" | 0.0
+
| 09/13/2011
| style="text-align:right;" | 0.0
+
| 2011-09-13
| style="text-align:right;" | 0.0
+
| 78.86* - Failure to report defective, insufficient, or improperly cemented casing w/in 24 hrs or submit plan to correct w/in 30 days
| style="text-align:right;" | 0.0
+
| Administrative
| style="text-align:right;" | 0.0
+
|  
|-
 
|-
 
| 2010-3
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
 
|-
 
|-
 
|}
 
|}
== Waste Data ==
+
<!--==== Penalties Applied ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" | Violation ID
!scope="col" | TYPE
+
!scope="col" | Penalty ID
!scope="col" | QUANTITY
+
!scope="col" | Penalty Code
!scope="col" | UNITS
+
!scope="col" | Penalty Status
!scope="col" | DISPOSAL METHOD
+
!scope="col" | Penalty Date
!scope="col" | WASTE FACILITY PERMIT ID
+
!scope="col" | Enforcement Date
!scope="col" | WASTE FACILITY NAME
+
!scope="col" | Penalty Amount
!scope="col" | FACILITY CITY
+
!scope="col" | Amount Collected
!scope="col" | FACILITY STATE
+
|-
|}
+
|}-->
 +
For data sources see<ref>{{cite web
 +
| title =Oil and Gas Compliance Report
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-05-20
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 
==References==
 
==References==
{{Reflist}}
+
<references/>
 
 
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 +
[[Category:Pennsylvania Wells]]

Latest revision as of 14:19, 2 June 2020

Well Details

Well ID: 37-115-20205
Loading map...
Country: United States
State: Pennsylvania
County: Susquehanna
Municipality: Liberty Township
Operator Name: XPR RESOURCES LLC
Well Pad ID:
Farm/Lease Name: CARTY 1H
License Status:
Spud Date:
Permit Date: 2009-08-24
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 41.976792
Longitude: -75.779855

For data sources see[1][2][3]

Well History

Date Event
2009-08-24 New Permit Application

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2010 XPR RESOURCES LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2002311 Primary Facility 2011-09-13 Drilling/Alteration Violation(s) Noted At the time of inspection, I inspected the cellar of the well. Standing fluid was present in the cellar up around the base of the well head. Consistent bubbling was observed between the 9 x 13 annulus. The Operator did not report the defect to the Department.
2625142 Primary Facility 2017-08-11 Routine/Complete Inspection No Violations Noted The Department arrived on site at the WR 77- Carty Well Site to conduct a Routine Complete Inspection. A review of the E&S Inspection Log indicated that the most recent inspection was conducted on 8/7/17 with the note "monitor rills".

The status of this well is "Operator Reported Not Drilled".

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2002311 620052 09/13/2011 2011-09-13 78.86* - Failure to report defective, insufficient, or improperly cemented casing w/in 24 hrs or submit plan to correct w/in 30 days Administrative

For data sources see[6]

References