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Difference between revisions of "34-173-61121"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-173-61121
 
| Well ID: 34-173-61121
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.22328775, -83.64210746 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.223341183, -83.64203869 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Wood County, Ohio|Wood]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Wood_County,_Ohio|Wood]]
 +
|-
 +
| Municipality: [[Bloom_Township,_Wood_County,_Ohio|Bloom Township]]
 
|-
 
|-
 
| Operator Name: [[LANDOWNER GRANT PROGRAM 2009]]
 
| Operator Name: [[LANDOWNER GRANT PROGRAM 2009]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: ZIEGLER DALLAS
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2011-07-26
 
|-
 
|-
 
| Spud Date:  
 
| Spud Date:  
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:
 +
|-
 +
| Final Drill Date:
 +
|-
 +
| Well Total Depth:  
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Final Restoration
+
| Latitude: 41.223341183
 
|-
 
|-
| Violations: 0
+
| Longitude: -83.64203869
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| Change of Owner
 +
| 2006-03-23
 +
| Operator changed from 9999, UNKNOWN OWNER to 7952, LANDOWNER GRANT PROGRAM 2006
 
|-
 
|-
| Latitude: 41.22328775
+
| APP
 +
| 2006-03-24
 +
| Proposed Formations:TRENTON, Issued Date:3/24/2006, Expired Date:3/24/2007 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
 
|-
 
|-
| Longitude: -83.64210746
+
| Change of Owner
 +
| 2008-11-06
 +
| Operator changed from 7952, LANDOWNER GRANT PROGRAM 2006 to 8389, LANDOWNER GRANT PROGRAM 2008
 +
|-
 +
| APP
 +
| 2009-04-08
 +
| Proposed Formations:TRENTON, Issued Date:4/8/2009, Expired Date:4/8/2010 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
 +
|-
 +
| Change of Owner
 +
| 2009-04-08
 +
| Operator changed from 8389, LANDOWNER GRANT PROGRAM 2008 to 8483, LANDOWNER GRANT PROGRAM 2009
 +
|-
 +
| Plugged by Orphan Well Program
 +
| 2009-05-13
 +
| Plugged by Orphan Well Program
 +
|-
 +
| Plugged/Abandoned
 +
| 2009-05-13
 +
| INSPECTED BY KEN PIISPANEN ON 10/07/04. REQUESTED BY LANDOWNER DALLAS ZIEGLER WHO NOTED OIL IN FIELD.  A BACKHOE EXCAVATION FOUND AN OLD STEEL CASING APPROXIMATELY 2 FEET BELOW THE GROUND.
 +
|-
 +
| Construction Permit Expires
 +
| 2010-04-08
 +
| INSPECTED BY KEN PIISPANEN ON 10/07/04. REQUESTED BY LANDOWNER DALLAS ZIEGLER WHO NOTED OIL IN FIELD.  A BACKHOE EXCAVATION FOUND AN OLD STEEL CASING APPROXIMATELY 2 FEET BELOW THE GROUND.
 +
|-
 +
| Record Last Modified
 +
| 2013-03-14
 +
| INSPECTED BY KEN PIISPANEN ON 10/07/04. REQUESTED BY LANDOWNER DALLAS ZIEGLER WHO NOTED OIL IN FIELD.  A BACKHOE EXCAVATION FOUND AN OLD STEEL CASING APPROXIMATELY 2 FEET BELOW THE GROUND.
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 +
<!--== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 +
<!--== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
| -1079431239
+
| 1079431239
 
| 2011-07-26
 
| 2011-07-26
|  
+
| Final Restoration
 +
| No Violations
 
| Well was located in farm field. Field and access road graded and planted. Grass on access lane and crops in field. Final Restoration Passed.
 
| Well was located in farm field. Field and access road graded and planted. Grass on access lane and crops in field. Final Restoration Passed.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1098896315
 
| 1098896315
 
| 2004-10-07
 
| 2004-10-07
|  
+
| Orphan
 +
| No Violations
 
| Request by landowner Dallas Ziegler to check 2 wells found in farm field. Field is on Tank Farm Road and is adjacent to BP Oil property which has large storage/distribution tanks. There are 2 pipelines crossing the field. Landowner noted oil in field and contacted BP Oil. A backhoe was brought in to excavate to check if there was a leak from the pipeline or tanks. An old steel well casing was found approximately 2 feet below ground. A vac truck removed oil from the site and a 12 inch pipe was installed to contain discharge from the well.
 
| Request by landowner Dallas Ziegler to check 2 wells found in farm field. Field is on Tank Farm Road and is adjacent to BP Oil property which has large storage/distribution tanks. There are 2 pipelines crossing the field. Landowner noted oil in field and contacted BP Oil. A backhoe was brought in to excavate to check if there was a leak from the pipeline or tanks. An old steel well casing was found approximately 2 feet below ground. A vac truck removed oil from the site and a 12 inch pipe was installed to contain discharge from the well.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1242059955
 
| 1242059955
 
| 2009-05-11
 
| 2009-05-11
|  
+
| Orphan
 +
| No Violations
 
| Operator pumped cement into the well through 1050 feet of tubing. After pumpming most of cement from truck, cisculation was lost and pump would not pump cement into well. Tubing will be pulled and will check depth to cement in the morning.
 
| Operator pumped cement into the well through 1050 feet of tubing. After pumpming most of cement from truck, cisculation was lost and pump would not pump cement into well. Tubing will be pulled and will check depth to cement in the morning.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1242138435
 
| 1242138435
 
| 2009-05-12
 
| 2009-05-12
|  
+
| Plug / Plug Back
 +
| No Violations
 
| Cement set up at 650 feet. Pumped 110 bags of cement into the well. Cement did not return to surface although there was circulation. Will check depth to cement in the morning.
 
| Cement set up at 650 feet. Pumped 110 bags of cement into the well. Cement did not return to surface although there was circulation. Will check depth to cement in the morning.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1242312086
 
| 1242312086
 
| 2009-05-13
 
| 2009-05-13
|  
+
| Plug / Plug Back
 +
| No Violations
 
| Cement set up at 66 feet depth. Operator filled remaining well casing with 13 bags of hand mix cement. ID plate being made. Pit  open around well to cut off top of casing and attach plate.
 
| Cement set up at 66 feet depth. Operator filled remaining well casing with 13 bags of hand mix cement. ID plate being made. Pit  open around well to cut off top of casing and attach plate.
|
 
|
 
|
 
|-
 
 
|-
 
|-
| -1249169683
+
| 1249169683
 
| 2009-06-08
 
| 2009-06-08
|  
+
| Orphan
 +
| No Violations
 
| Spoke to Bob Harpster and Dallas Ziegler about final restoration of site. Bob is waiting on OK from Mr. Ziegler to complete work. Another I&O well has been located in the farm field and will be docmented and submitted to the Orphan Well program. Access road to well will be disced after well data collected.
 
| Spoke to Bob Harpster and Dallas Ziegler about final restoration of site. Bob is waiting on OK from Mr. Ziegler to complete work. Another I&O well has been located in the farm field and will be docmented and submitted to the Orphan Well program. Access road to well will be disced after well data collected.
|
 
|
 
|
 
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 23:40, 24 July 2019

Well Details

Well ID: 34-173-61121
Loading map...
Country: United States
State: Ohio
County: Wood
Municipality: Bloom Township
Operator Name: LANDOWNER GRANT PROGRAM 2009
Well Pad ID:
Farm/Lease Name: ZIEGLER DALLAS
License Status: Final Restoration
License Date: 2011-07-26
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 41.223341183
Longitude: -83.64203869

For data sources see[1]

Well History

Well Status Well Status Date Comment
Change of Owner 2006-03-23 Operator changed from 9999, UNKNOWN OWNER to 7952, LANDOWNER GRANT PROGRAM 2006
APP 2006-03-24 Proposed Formations:TRENTON, Issued Date:3/24/2006, Expired Date:3/24/2007 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2008-11-06 Operator changed from 7952, LANDOWNER GRANT PROGRAM 2006 to 8389, LANDOWNER GRANT PROGRAM 2008
APP 2009-04-08 Proposed Formations:TRENTON, Issued Date:4/8/2009, Expired Date:4/8/2010 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2009-04-08 Operator changed from 8389, LANDOWNER GRANT PROGRAM 2008 to 8483, LANDOWNER GRANT PROGRAM 2009
Plugged by Orphan Well Program 2009-05-13 Plugged by Orphan Well Program
Plugged/Abandoned 2009-05-13 INSPECTED BY KEN PIISPANEN ON 10/07/04. REQUESTED BY LANDOWNER DALLAS ZIEGLER WHO NOTED OIL IN FIELD. A BACKHOE EXCAVATION FOUND AN OLD STEEL CASING APPROXIMATELY 2 FEET BELOW THE GROUND.
Construction Permit Expires 2010-04-08 INSPECTED BY KEN PIISPANEN ON 10/07/04. REQUESTED BY LANDOWNER DALLAS ZIEGLER WHO NOTED OIL IN FIELD. A BACKHOE EXCAVATION FOUND AN OLD STEEL CASING APPROXIMATELY 2 FEET BELOW THE GROUND.
Record Last Modified 2013-03-14 INSPECTED BY KEN PIISPANEN ON 10/07/04. REQUESTED BY LANDOWNER DALLAS ZIEGLER WHO NOTED OIL IN FIELD. A BACKHOE EXCAVATION FOUND AN OLD STEEL CASING APPROXIMATELY 2 FEET BELOW THE GROUND.

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1079431239 2011-07-26 Final Restoration No Violations Well was located in farm field. Field and access road graded and planted. Grass on access lane and crops in field. Final Restoration Passed.
1098896315 2004-10-07 Orphan No Violations Request by landowner Dallas Ziegler to check 2 wells found in farm field. Field is on Tank Farm Road and is adjacent to BP Oil property which has large storage/distribution tanks. There are 2 pipelines crossing the field. Landowner noted oil in field and contacted BP Oil. A backhoe was brought in to excavate to check if there was a leak from the pipeline or tanks. An old steel well casing was found approximately 2 feet below ground. A vac truck removed oil from the site and a 12 inch pipe was installed to contain discharge from the well.
1242059955 2009-05-11 Orphan No Violations Operator pumped cement into the well through 1050 feet of tubing. After pumpming most of cement from truck, cisculation was lost and pump would not pump cement into well. Tubing will be pulled and will check depth to cement in the morning.
1242138435 2009-05-12 Plug / Plug Back No Violations Cement set up at 650 feet. Pumped 110 bags of cement into the well. Cement did not return to surface although there was circulation. Will check depth to cement in the morning.
1242312086 2009-05-13 Plug / Plug Back No Violations Cement set up at 66 feet depth. Operator filled remaining well casing with 13 bags of hand mix cement. ID plate being made. Pit open around well to cut off top of casing and attach plate.
1249169683 2009-06-08 Orphan No Violations Spoke to Bob Harpster and Dallas Ziegler about final restoration of site. Bob is waiting on OK from Mr. Ziegler to complete work. Another I&O well has been located in the farm field and will be docmented and submitted to the Orphan Well program. Access road to well will be disced after well data collected.

For data sources see[3]

References