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(Created page with "== Well Details == {{131-20156-Details}} __TOC__ == Well Inspection Data == {{131-20156-inspection}} == Production Data == {{131-20156-production}} == Waste Data == {{131-2015...") |
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== Well Details == | == Well Details == | ||
− | { | + | {| class="wikitable" width="95%" |
+ | | Well ID: 131-20156 | ||
+ | | style="width: 50%; height=100%; align=center" rowspan="14" | {{#display_map: 41.640783, -75.811002 | width=100% | height=100% }} | ||
+ | |- | ||
+ | | County: [[Wyoming County, Pennsylvania|Wyoming]] | ||
+ | |- | ||
+ | | Municipality: [[Nicholson Township, Wyoming County, Pennsylvania|Nicholson Township]] | ||
+ | |- | ||
+ | | Operator Name: [[CHIEF OIL & GAS LLC]] | ||
+ | |- | ||
+ | | Farm/Lease Name: POLOVITCH UNIT 1H | ||
+ | |- | ||
+ | | First Permit Date: 2011-03-22 | ||
+ | |- | ||
+ | | Last Permit Date: 2011-03-22 | ||
+ | |- | ||
+ | | Spud Date: 2011-03-28 | ||
+ | |- | ||
+ | | Unconventional: Yes | ||
+ | |- | ||
+ | | Horizontal: Yes | ||
+ | |- | ||
+ | | Producing: Yes | ||
+ | |- | ||
+ | | Violations: 1 | ||
+ | |- | ||
+ | | Latitude: 41.640783 | ||
+ | |- | ||
+ | | Longitude: -75.811002 | ||
+ | |- | ||
+ | |} | ||
__TOC__ | __TOC__ | ||
== Well Inspection Data == | == Well Inspection Data == | ||
− | { | + | {| class="wikitable sortable" width="95%" |
+ | !scope="col" | INSPECTION ID | ||
+ | !scope="col" | DATE | ||
+ | !scope="col" | DESCRIPTION | ||
+ | !scope="col" | COMMENT | ||
+ | !scope="col" | VIOLATION ID | ||
+ | |- | ||
+ | | 1960667 | ||
+ | | 2011-03-28 | ||
+ | | No Violations Noted | ||
+ | | big rig- probably Thurs, still laying plastic, etc,getting ready to spud, have permit on site | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1965039 | ||
+ | | 2011-04-11 | ||
+ | | No Violations Noted | ||
+ | | AT 1823' drilling to 1825' then set csg and cement- probably tonight, using Universal | ||
+ | UDI Rig 58 | ||
+ | Drillers log - good | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1965671 | ||
+ | | 2011-04-14 | ||
+ | | No Violations Noted | ||
+ | | UDI Rig 58 | ||
+ | got copy of cement and csg report | ||
+ | BOP tested 4/14/2011 1500/2500lbs for 5 min | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1968964 | ||
+ | | 2011-04-28 | ||
+ | | No Violations Noted | ||
+ | | UDI 58 | ||
+ | TD @ 6:45 AM 4/28/2011 | ||
+ | discussed containment, BOP testing - put in drillers log | ||
+ | checked drillers log | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1969661 | ||
+ | | 2011-05-02 | ||
+ | | No Violations Noted | ||
+ | | 5 1/2" csg set @ 10026' with 1180 sx cement report attached | ||
+ | Well is done. Cleaning up rig and site. Will skid rig and drill another well at site. | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1990412 | ||
+ | | 2011-07-25 | ||
+ | | No Violations Noted | ||
+ | | All 3 annuli have a vent pipe running to a frac tank. | ||
+ | No containment under pipes. | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1996398 | ||
+ | | 2011-08-17 | ||
+ | | No Violations Noted | ||
+ | | Comp. Man - Max Lee, Fracing, hoping to get started this afternoon. Planning 5 stages - BJ. Need to get permits on site. | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1997192 | ||
+ | | 2011-08-19 | ||
+ | | No Violations Noted | ||
+ | | fracing, on stage 1 of 5 - just finished as I got here. | ||
+ | 1530 - shut down job because of lightning( didn't start second stage ) | ||
+ | Have permits. | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2026320 | ||
+ | | 2011-12-09 | ||
+ | | No Violations Noted | ||
+ | | Well is in production - 1076 psi. | ||
+ | 36 annular vents - cellar is filled in. | ||
+ | Black Beauty Abrasive on ground - empty bags on site. | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2029279 | ||
+ | | 2011-12-15 | ||
+ | | Pending | ||
+ | | On site with Eric Rooney to gather isotopic samples from annuli. Chief O&G reps on site -Rich Adams, Ralph Larson, and Jon Hafer. There are 3 annular vents, but cellar is filled in. Cellar will be dug out to confirm which annulus the vents go to. | ||
+ | blue - 5 1/2" X 9 5/8" - 169 psi , 100% comb. gas | ||
+ | A = ? 9 5/8 X 13 3/8" ? 68 psi, 100% comb. gas | ||
+ | B= ? 13 3/8 X 20" ? 35 psi, 100% comb. gas | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2029283 | ||
+ | | 2011-12-19 | ||
+ | | Violation(s) Noted | ||
+ | | On site with Kevin Costello. Met Rich Adams and Jon Hafer, Chief reps. Cellar has been dug up to determine which annuli the vents go to. | ||
+ | blue 9 5/8" X 5 1/2" This is what we | ||
+ | A 13 3/8 X 9 5/8" thought before they | ||
+ | B 20 X 13 3/8" were dug up. | ||
+ | | 627760 | ||
+ | |- | ||
+ | |- | ||
+ | | 2029309 | ||
+ | | 2011-12-22 | ||
+ | | Outstanding Violations - No Viols Req'd | ||
+ | | Onsite to take flow readings on csg annuli. Met w/ Ralph Larsen and Jon Hafer / Cheif Reps. Used the 1/4" plate on our oriface meter. | ||
+ | 13 3/8" X 9 5/8" annulus - 0" of water = 0 cf/day of gas | ||
+ | 20 X 13 3/8" annulus - 0" of water = 0 cf/day of gas | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2029315 | ||
+ | | 2011-12-15 | ||
+ | | Pending | ||
+ | | On site w/ Eric Rooney to gather isotopic samples from annuli. Also on site are Rich Adams, Ralph Larson, And Jon Hafer representing Chief Oil. There are 3 annular vents, but cellar is filled in. Will be dug out to confirm annuli. | ||
+ | blue 5 1/2" X 9 5/8" 169 psi, 100% comb. gas | ||
+ | A ? 9 5/8 X 13 3/8" ? 68 psi, 100% comb. gas | ||
+ | B ? 132 3/8 X 20" ? 35 psi, 100% comb. gas | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2051382 | ||
+ | | 2012-03-15 | ||
+ | | Outstanding Violations - No Viols Req'd | ||
+ | | Cellar dug out, small amount of water, no bubbles. | ||
+ | Need to put up orange fence( on ground) or barrier. | ||
+ | Prod. - 1150psi | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2062407 | ||
+ | | 2012-04-12 | ||
+ | | Outstanding Violations - No Viols Req'd | ||
+ | | Producing well. Cellar is dug out, small amount of water present, no bubbles. | ||
+ | 3 annular vents piped to tanks. | ||
+ | No change since last inspection. | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2062431 | ||
+ | | 2012-03-27 | ||
+ | | Outstanding Violations - No Viols Req'd | ||
+ | | Producing. Cellar dug out, some water, no bubbles, 3 vents from csg annuli. | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2064974 | ||
+ | | 2012-04-27 | ||
+ | | Outstanding Violations - No Viols Req'd | ||
+ | | Pressure recording devices have been installed on each of 3 annulus vents. Vents are shut in: 1150psi prod | ||
+ | 8 psi 20 X 13 3/8" annulus | ||
+ | 18 psi 13 3/8 X 9 5/8" | ||
+ | 100 psi 9 5/8" X 5 1/2" blue | ||
+ | Otherwise no change. Cellar dug out - no water. | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2067568 | ||
+ | | 2012-05-14 | ||
+ | | Outstanding Violations - No Viols Req'd | ||
+ | | Producing well. 3 annular vents - shut in with pressure and temp. recording device installed and press guages. Pressures are: 5 1/2" X 9 5/8" = 60 psi | ||
+ | 9 5/8 x 13 3/8" = 15.5 psi | ||
+ | 13 3/8 x 20" = 2 psi | ||
+ | Celar is dug out w/ small amount of water. | ||
+ | 1125 psi on prod. | ||
+ | Drop in pressures on annular vents since last inspection. | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2078711 | ||
+ | | 2012-06-18 | ||
+ | | Outstanding Violations - No Viols Req'd | ||
+ | | Concrete barriers have been placed around well heads. The cellar is dug out w/ water - no bubbles. | ||
+ | There are 3 annular vents - all open. | ||
+ | Well is producing - 1093 psi on prod. | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2084516 | ||
+ | | 2012-07-18 | ||
+ | | Outstanding Violations - No Viols Req'd | ||
+ | | Cellars are dug out. No water to 1/2" present. No changes since last inspection on 7/9/2012. | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2086703 | ||
+ | | 2012-07-24 | ||
+ | | Outstanding Violations - No Viols Req'd | ||
+ | | No change since last insp. Some water in cellar - no bubbles. 3 annular vents - all open, vented. | ||
+ | Prod has 1150 psi. | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2087775 | ||
+ | | 2012-07-30 | ||
+ | | Outstanding Violations - No Viols Req'd | ||
+ | | Producing well. Has 3 annular vents, open. Clean water in cellar, no bubbles. | ||
+ | 1205 psi on prod. No change since last insp. | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2097253 | ||
+ | | 2012-08-30 | ||
+ | | Outstanding Violations - No Viols Req'd | ||
+ | | On site w/ Kevin Costello(DEP), Ralph Larsen (Chief) & Jon Hafer(Chief consult.) to witness flow tests and pressure tests on annuli. Shut in all 3 annuli(20 x 13 3/8", 13 3/8 x 9 5/8", and 9 5/8 x 5 1/2") for 20 min. All pressures are 0 psi. Did not install orifice meter, flow is zero. | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2102755 | ||
+ | | 2012-09-14 | ||
+ | | Outstanding Violations - No Viols Req'd | ||
+ | | Cellar is dug out. Very small amount of water - no bubbles, 3 annular vents. Pressure guage on 9 5/8 x 5 1/2" annulus but all annuli are open, venting to tank. Producing well. | ||
+ | 1201 psi on production. | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2133525 | ||
+ | | 2013-01-15 | ||
+ | | Outstanding Violations - No Viols Req'd | ||
+ | | Company Man is Max Lee. IPS (was Warrior) coil tbg unit on site. Moved in yesterdeay. Had a problem with a valve when rigging up, held them up. Encountered an obstruction at 15'. Will try to push, or drill out if need, clean out hole before setting CIBP @ 7200'. Plastic containment is down, good. Will prob. finish cleaning out hole and setting plug and filling on Thurs. | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2137296 | ||
+ | | 2013-01-25 | ||
+ | | Outstanding Violations - No Viols Req'd | ||
+ | | CDK Wireline is rigging down and moving out. On the 23 rd, log was run w/ the 4H open, producing. Noise increased as logged up the hole. Shut in the 4H and ran noise again from about 4200' to surf w/ same results. Gary from GWB consulting (not on site) suspended logs. The annuli on 1H were shut in prior to logging, he wants them shut in for about 1 month so everything equalizes. Need to call Rich Adams Monday. | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2137302 | ||
+ | | 2013-01-23 | ||
+ | | Outstanding Violations - No Viols Req'd | ||
+ | | Here for noise and temp logging. CDK logging. 5 1/2" has 0 psi and is full of fluid. | ||
+ | Running temp log, almost to bottom. Will run noide coming back up hole. | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2141567 | ||
+ | | 2013-01-18 | ||
+ | | Outstanding Violations - No Viols Req'd | ||
+ | | Coil tbg rig has moved off site. No comp man present. | ||
+ | | | ||
+ | |- | ||
+ | |} | ||
== Production Data == | == Production Data == | ||
− | { | + | {| class="wikitable sortable" width="95%" |
+ | !scope="col" | PERIOD | ||
+ | !scope="col" | GAS QUANTITY | ||
+ | !scope="col" | GAS PRODUCTION DAYS | ||
+ | !scope="col" | CONDENSATE QUANTITY | ||
+ | !scope="col" | CONDENSATE PRODUCTION DAYS | ||
+ | !scope="col" | OIL QUANTITY | ||
+ | !scope="col" | OIL PRODUCTION DAYS | ||
+ | |- | ||
+ | | 2012-2 | ||
+ | | style="text-align:right;" | 197646.0 | ||
+ | | style="text-align:right;" | 184.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | |- | ||
+ | |- | ||
+ | | 2012-1 | ||
+ | | style="text-align:right;" | 201386.47 | ||
+ | | style="text-align:right;" | 182.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | |- | ||
+ | |- | ||
+ | | 2011-2 | ||
+ | | style="text-align:right;" | 101239.0 | ||
+ | | style="text-align:right;" | 63.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | |- | ||
+ | |- | ||
+ | | 2011-1 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | |- | ||
+ | |} | ||
== Waste Data == | == Waste Data == | ||
− | { | + | {| class="wikitable sortable" width="95%" |
+ | !scope="col" | PERIOD | ||
+ | !scope="col" | TYPE | ||
+ | !scope="col" | QUANTITY | ||
+ | !scope="col" | UNITS | ||
+ | !scope="col" | DISPOSAL METHOD | ||
+ | !scope="col" | WASTE FACILITY PERMIT ID | ||
+ | !scope="col" | WASTE FACILITY NAME | ||
+ | !scope="col" | FACILITY CITY | ||
+ | !scope="col" | FACILITY STATE | ||
+ | |- | ||
+ | | 2012-2 | ||
+ | | PRODUCED FLUID | ||
+ | | style="text-align:right;" | 656.3 | ||
+ | | Bbl | ||
+ | | REUSE OTHER THAN ROAD SPREADING | ||
+ | | | ||
+ | | REUSE FOR HYDRAULIC FRACTURING | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2011-1 | ||
+ | | FRACING FLUID WASTE | ||
+ | | style="text-align:right;" | 357.0 | ||
+ | | Bbl | ||
+ | | CENTRALIZED TREATMENT PLANT FOR RECYCLE | ||
+ | | PA0008451 | ||
+ | | SUNBURY GENERATION WASTE WATER TRMT FAC | ||
+ | | SHAMOKIN DAM | ||
+ | | PA | ||
+ | |- | ||
+ | |- | ||
+ | | 2011-1 | ||
+ | | DRILL CUTTINGS | ||
+ | | style="text-align:right;" | 1143.3 | ||
+ | | Tons | ||
+ | | LANDFILL | ||
+ | | 100955 | ||
+ | | WAYNE TOWNSHIP LANDFILL (CLINTON COUNTY) | ||
+ | | MC ELHATTAN | ||
+ | | PA | ||
+ | |- | ||
+ | |- | ||
+ | | 2011-1 | ||
+ | | DRILL CUTTINGS | ||
+ | | style="text-align:right;" | 659.38 | ||
+ | | Tons | ||
+ | | LANDFILL | ||
+ | | 301626 | ||
+ | | WHITE PINES LANDFILL | ||
+ | | MILLVILLE | ||
+ | | PA | ||
+ | |- | ||
+ | |- | ||
+ | | 2011-2 | ||
+ | | FRACING FLUID WASTE | ||
+ | | style="text-align:right;" | 3130.0 | ||
+ | | Bbl | ||
+ | | REUSE OTHER THAN ROAD SPREADING | ||
+ | | | ||
+ | | FRAC WATER REUSE | ||
+ | | | ||
+ | | PA | ||
+ | |- | ||
+ | |- | ||
+ | | 2011-2 | ||
+ | | DRILL CUTTINGS | ||
+ | | style="text-align:right;" | 1272.61 | ||
+ | | Tons | ||
+ | | LANDFILL | ||
+ | | 301626 | ||
+ | | WHITE PINES LANDFILL | ||
+ | | MILLVILLE | ||
+ | | PA | ||
+ | |- | ||
+ | |- | ||
+ | | 2012-1 | ||
+ | | PRODUCED FLUID | ||
+ | | style="text-align:right;" | 1722.0 | ||
+ | | Bbl | ||
+ | | REUSE OTHER THAN ROAD SPREADING | ||
+ | | | ||
+ | | REUSE FOR HYDRAULIC FRACTURING | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ |
Well ID: 131-20156 | Loading map...
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County: Wyoming | |
Municipality: Nicholson Township | |
Operator Name: CHIEF OIL & GAS LLC | |
Farm/Lease Name: POLOVITCH UNIT 1H | |
First Permit Date: 2011-03-22 | |
Last Permit Date: 2011-03-22 | |
Spud Date: 2011-03-28 | |
Unconventional: Yes | |
Horizontal: Yes | |
Producing: Yes | |
Violations: 1 | |
Latitude: 41.640783 | |
Longitude: -75.811002 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
1960667 | 2011-03-28 | No Violations Noted | big rig- probably Thurs, still laying plastic, etc,getting ready to spud, have permit on site | |
1965039 | 2011-04-11 | No Violations Noted | AT 1823' drilling to 1825' then set csg and cement- probably tonight, using Universal
UDI Rig 58 Drillers log - good |
|
1965671 | 2011-04-14 | No Violations Noted | UDI Rig 58
got copy of cement and csg report BOP tested 4/14/2011 1500/2500lbs for 5 min |
|
1968964 | 2011-04-28 | No Violations Noted | UDI 58
TD @ 6:45 AM 4/28/2011 discussed containment, BOP testing - put in drillers log checked drillers log |
|
1969661 | 2011-05-02 | No Violations Noted | 5 1/2" csg set @ 10026' with 1180 sx cement report attached
Well is done. Cleaning up rig and site. Will skid rig and drill another well at site. |
|
1990412 | 2011-07-25 | No Violations Noted | All 3 annuli have a vent pipe running to a frac tank.
No containment under pipes. |
|
1996398 | 2011-08-17 | No Violations Noted | Comp. Man - Max Lee, Fracing, hoping to get started this afternoon. Planning 5 stages - BJ. Need to get permits on site. | |
1997192 | 2011-08-19 | No Violations Noted | fracing, on stage 1 of 5 - just finished as I got here.
1530 - shut down job because of lightning( didn't start second stage ) Have permits. |
|
2026320 | 2011-12-09 | No Violations Noted | Well is in production - 1076 psi.
36 annular vents - cellar is filled in. Black Beauty Abrasive on ground - empty bags on site. |
|
2029279 | 2011-12-15 | Pending | On site with Eric Rooney to gather isotopic samples from annuli. Chief O&G reps on site -Rich Adams, Ralph Larson, and Jon Hafer. There are 3 annular vents, but cellar is filled in. Cellar will be dug out to confirm which annulus the vents go to.
blue - 5 1/2" X 9 5/8" - 169 psi , 100% comb. gas A = ? 9 5/8 X 13 3/8" ? 68 psi, 100% comb. gas B= ? 13 3/8 X 20" ? 35 psi, 100% comb. gas |
|
2029283 | 2011-12-19 | Violation(s) Noted | On site with Kevin Costello. Met Rich Adams and Jon Hafer, Chief reps. Cellar has been dug up to determine which annuli the vents go to.
blue 9 5/8" X 5 1/2" This is what we A 13 3/8 X 9 5/8" thought before they B 20 X 13 3/8" were dug up. |
627760 |
2029309 | 2011-12-22 | Outstanding Violations - No Viols Req'd | Onsite to take flow readings on csg annuli. Met w/ Ralph Larsen and Jon Hafer / Cheif Reps. Used the 1/4" plate on our oriface meter.
13 3/8" X 9 5/8" annulus - 0" of water = 0 cf/day of gas 20 X 13 3/8" annulus - 0" of water = 0 cf/day of gas |
|
2029315 | 2011-12-15 | Pending | On site w/ Eric Rooney to gather isotopic samples from annuli. Also on site are Rich Adams, Ralph Larson, And Jon Hafer representing Chief Oil. There are 3 annular vents, but cellar is filled in. Will be dug out to confirm annuli.
blue 5 1/2" X 9 5/8" 169 psi, 100% comb. gas A ? 9 5/8 X 13 3/8" ? 68 psi, 100% comb. gas B ? 132 3/8 X 20" ? 35 psi, 100% comb. gas |
|
2051382 | 2012-03-15 | Outstanding Violations - No Viols Req'd | Cellar dug out, small amount of water, no bubbles.
Need to put up orange fence( on ground) or barrier. Prod. - 1150psi |
|
2062407 | 2012-04-12 | Outstanding Violations - No Viols Req'd | Producing well. Cellar is dug out, small amount of water present, no bubbles.
3 annular vents piped to tanks. No change since last inspection. |
|
2062431 | 2012-03-27 | Outstanding Violations - No Viols Req'd | Producing. Cellar dug out, some water, no bubbles, 3 vents from csg annuli. | |
2064974 | 2012-04-27 | Outstanding Violations - No Viols Req'd | Pressure recording devices have been installed on each of 3 annulus vents. Vents are shut in: 1150psi prod
8 psi 20 X 13 3/8" annulus 18 psi 13 3/8 X 9 5/8" 100 psi 9 5/8" X 5 1/2" blue Otherwise no change. Cellar dug out - no water. |
|
2067568 | 2012-05-14 | Outstanding Violations - No Viols Req'd | Producing well. 3 annular vents - shut in with pressure and temp. recording device installed and press guages. Pressures are: 5 1/2" X 9 5/8" = 60 psi
9 5/8 x 13 3/8" = 15.5 psi 13 3/8 x 20" = 2 psi Celar is dug out w/ small amount of water. 1125 psi on prod. Drop in pressures on annular vents since last inspection. |
|
2078711 | 2012-06-18 | Outstanding Violations - No Viols Req'd | Concrete barriers have been placed around well heads. The cellar is dug out w/ water - no bubbles.
There are 3 annular vents - all open. Well is producing - 1093 psi on prod. |
|
2084516 | 2012-07-18 | Outstanding Violations - No Viols Req'd | Cellars are dug out. No water to 1/2" present. No changes since last inspection on 7/9/2012. | |
2086703 | 2012-07-24 | Outstanding Violations - No Viols Req'd | No change since last insp. Some water in cellar - no bubbles. 3 annular vents - all open, vented.
Prod has 1150 psi. |
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2087775 | 2012-07-30 | Outstanding Violations - No Viols Req'd | Producing well. Has 3 annular vents, open. Clean water in cellar, no bubbles.
1205 psi on prod. No change since last insp. |
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2097253 | 2012-08-30 | Outstanding Violations - No Viols Req'd | On site w/ Kevin Costello(DEP), Ralph Larsen (Chief) & Jon Hafer(Chief consult.) to witness flow tests and pressure tests on annuli. Shut in all 3 annuli(20 x 13 3/8", 13 3/8 x 9 5/8", and 9 5/8 x 5 1/2") for 20 min. All pressures are 0 psi. Did not install orifice meter, flow is zero. | |
2102755 | 2012-09-14 | Outstanding Violations - No Viols Req'd | Cellar is dug out. Very small amount of water - no bubbles, 3 annular vents. Pressure guage on 9 5/8 x 5 1/2" annulus but all annuli are open, venting to tank. Producing well.
1201 psi on production. |
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2133525 | 2013-01-15 | Outstanding Violations - No Viols Req'd | Company Man is Max Lee. IPS (was Warrior) coil tbg unit on site. Moved in yesterdeay. Had a problem with a valve when rigging up, held them up. Encountered an obstruction at 15'. Will try to push, or drill out if need, clean out hole before setting CIBP @ 7200'. Plastic containment is down, good. Will prob. finish cleaning out hole and setting plug and filling on Thurs. | |
2137296 | 2013-01-25 | Outstanding Violations - No Viols Req'd | CDK Wireline is rigging down and moving out. On the 23 rd, log was run w/ the 4H open, producing. Noise increased as logged up the hole. Shut in the 4H and ran noise again from about 4200' to surf w/ same results. Gary from GWB consulting (not on site) suspended logs. The annuli on 1H were shut in prior to logging, he wants them shut in for about 1 month so everything equalizes. Need to call Rich Adams Monday. | |
2137302 | 2013-01-23 | Outstanding Violations - No Viols Req'd | Here for noise and temp logging. CDK logging. 5 1/2" has 0 psi and is full of fluid.
Running temp log, almost to bottom. Will run noide coming back up hole. |
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2141567 | 2013-01-18 | Outstanding Violations - No Viols Req'd | Coil tbg rig has moved off site. No comp man present. |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2012-2 | 197646.0 | 184.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2012-1 | 201386.47 | 182.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-2 | 101239.0 | 63.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-1 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2012-2 | PRODUCED FLUID | 656.3 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR HYDRAULIC FRACTURING | |||
2011-1 | FRACING FLUID WASTE | 357.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0008451 | SUNBURY GENERATION WASTE WATER TRMT FAC | SHAMOKIN DAM | PA |
2011-1 | DRILL CUTTINGS | 1143.3 | Tons | LANDFILL | 100955 | WAYNE TOWNSHIP LANDFILL (CLINTON COUNTY) | MC ELHATTAN | PA |
2011-1 | DRILL CUTTINGS | 659.38 | Tons | LANDFILL | 301626 | WHITE PINES LANDFILL | MILLVILLE | PA |
2011-2 | FRACING FLUID WASTE | 3130.0 | Bbl | REUSE OTHER THAN ROAD SPREADING | FRAC WATER REUSE | PA | ||
2011-2 | DRILL CUTTINGS | 1272.61 | Tons | LANDFILL | 301626 | WHITE PINES LANDFILL | MILLVILLE | PA |
2012-1 | PRODUCED FLUID | 1722.0 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR HYDRAULIC FRACTURING |