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+ | [[Category:Wells]] |
Well ID: 37-015-21986 | Loading map...
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County: Bradford | |
Municipality: Albany Township | |
Operator Name: CHESAPEAKE APPALACHIA LLC | |
Well Pad ID: 148861 | |
Farm/Lease Name: MCGROARTY S BRA 2H | |
First Permit Date: 2011-10-13 | |
Last Permit Date: 2011-10-13 | |
Spud Date: 2011-12-04 | |
Unconventional: Yes | |
Horizontal: Yes | |
Producing: Yes | |
Violations: 1 | |
Latitude: 41.586422 | |
Longitude: -76.410794 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
2031971 | 2011-12-21 | No Violations Noted | NOMAC 44 Comp. Man - Buzz Glover checked drillers log - at 1711'
10' - water running in 80' - rock, above 80' - clay with chunks gravel or shale BOP test 12/19/2011 good cellar checked - no bubbles need to label all tanks 20" @ 84' w/ 210 sx Cl A, 15.6 ppg 12/5/2011 O-Tex 13 3/8" @ 552' w/ 450 sx stand. cement w/ gas block, 15.6 ppg, 100 sx Cl a 15.6 ppg, 8 bbls back to surf. Halliburton 12/18/2011 , will run bond log. |
|
2033249 | 2012-01-11 | Pending | NOMAC 44, Comp. Man - Russ White, Checked drillers log - at 12856'.
BOP test - 12/23/11, some drop-off - ? Comp. Man wasn't worried about it. 9 5/8" @ 2000' w/ 870 sx Stand, Cement w/ Gas Block, 15.6 ppg, 60 bbls back to surf, no packers. Discussed need to patch a few holes in plastic containment, keep 2' freeboard in waste tanks, and check on flare unit, light is not flashing- is it working? Checked cellar. Saw bubbles, 1 bubble every 1 to 2 seconds. Need to investigate further. |
|
2033885 | 2012-01-12 | No Violations Noted | NOMAC 44, Comp. Man - Russ White
On site to check if bubbles in cellar are still present and if they are methane. No bubbles are present. Flare light is flashing, it was unplugged. Holes in containment have been patched. Comp. Man wil continue to monitor the cellar for bubbles and will let us know if he sees any further bubbling. |
|
2039326 | 2012-01-31 | Pending | While inspecting the N BRA 2H, saw bubbling in cellar - full of water. Checked w/ Altair 5x gas meter - high CO(1000+ppm), about 40 ppm H2S, 100 comb gas. Had them pump out cellar. Hvy bubbling was from open valve on 5 1/2" x 9 5/8" annulus. However, I then noticed areas of less bubbling, in particular, at the spot where bubbles were previously seen while drilling, as noted in inspection report. Not sure where the bubbles were coming from, possibly from inside the 20" conductor. Will need to revisit the site after rig has moved. | |
2047143 | 2012-02-28 | Violation(s) Noted | 633156 | |
2054672 | 2012-03-28 | Outstanding Violations - No Viols Req'd | Conductor has been capped and monitoring device installed(see photo)
0 psi on 13 3/8 X 20" vent guage. Cellar is not backfilled, couple inches of water. |
|
2136524 | 2013-01-31 | No Violations Noted | Cellar is full of dirty water. Vents on 5 1/2" prod(not open) csg and 5 1/2 X 9 5/8" annulus(open) have pressure guages w/ 0 psi.
The 9 5/8 X 13 3/8" annulus is vented - comb = 20% LEL, Meth = 0 The 20 x 13 3/8" is capped and vented - Comb = 0, Meth = 0 Guage on top of wellhead (5 1/") has 340 psi. |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2012-2 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2012-1 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-2 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2012-1 | DRILLING FLUID WASTE | 25.0 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR HYDRAULIC FRACTURING | |||
2012-1 | PRODUCED FLUID | 508.5 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR HYDRAULIC FRACTURING |