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34-067-21307

Well Details

Well ID: 34-067-21307
County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional:
Horizontal:
Producing:
Violations:
Latitude:
Longitude:

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
1396354639 2014-03-27 HAD Drilling Rig # 680 is on site drilling a 30" inch diameter conductor hole and setting 30" inch diameter casing. The permit requirements are for 100ft of casing and no cementing is required using the concentric drilling method.
1399302949 2014-05-05 I am checking the drilling status of HAD Drilling and found that they are no longer on site. The conductor casing appeats to be set. I was advised that they would set 200 ft but nobody on site to confirm that.
1400092117 2014-05-12 H &P Drilling Rig # 287 is moving from the Athens B pad to this well. They are not very far along and will be several days before drilling begins.
1400680137 2014-05-20 Met Ron Trivisonno on site along with Beth Pratt and Hess Company Man R.L. went over the site stability information and why H & P Drilling Rig # 287 had to rig down and move off the site. Review my concerns on the conductor angular stability. If the section of the pad and toe of the bottom fill move will it move the conductor as well. I need to contact Hess Ohio to find out who is to take over the updates needed to repair the site.
1404139024 2014-06-30 On the date of inspection I accompanied ODNR Inspector Chris Grimm to witness a surface cement string. Refer to Chris Grimm's report for further details.
1404233807 2014-06-30 On the day of my inspection I found that HAD Drilling ran new 24" casing to a depth of 310'. Halliburton cemented the casing to surface with 570 sacks of class A cement. Good circulation was maintained throughout the job with 15 barrels of cement returns.
1666888425 2014-03-25 HAD Drilling is on site moving equipment in place to drill the conductor hole. They are not drilling at this time.
568875471 2014-04-28 I am on site today to witness the running of the 30" inch diameter casing string. The rig has shut down due to mechanical problems and another rig is now scheduled to move on in its place. They have casing at 68 ft and now will need to reduce the casing size and set 24" inch casing.
666432122 2014-06-25 On the date of inspection I accompanied ODNR Inspector Randy Akins and ODNR District Supervisor Brent Bear to witness the current drilling status of the well. Refer to Randy Akins report for further details.