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34-169-25648

Well Details

Well ID: 34-169-25648
County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional:
Horizontal:
Producing:
Violations:
Latitude:
Longitude:

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1222517989 2011-11-18 Ran 10 joints of R-3, 20 # 8.625" casing to 430' Petroset cemented with 200 sacks of Class A (100% excess) with 3 % CaCl2. Good cement returned to surface with no drop back. See casing ticket for details.
-1444877537 2014-05-22 Open flow well with no apparent problems at time of inspection.
-669542616 2012-01-25 This well was drilled while I was on leave. DNR Inspector Todd Miller covered the installation and cementing of the surface casing. The pits are closed.
1097173874 2011-12-07 Pits are being emptied.
1321962438 2011-11-21 Drilling ahead at 3050' and soaping.
1322048645 2011-11-22 Total depth was reached at 3675'. Open hole logs were not run. The rig ran 88 joints of 4.5", 10.5# production casing to 3650.6' and was set at 3660.6'. Petroset cemented the production casing with 150 sacks of regular Class A cement w/ 2% CaCl2. Plug down at 4:04 PM.
1323432713 2011-12-08 Reclaiming the pits.
1323774335 2011-12-12 Both the reserve and the working pit have been emptied and filled in. Well has not yet been fractured.
1361807297 2013-02-25 This is a producing constant feed gas well. There were no problems noted at the time of the inspection. Preliminary Restoration is passed.
1534697202 2013-03-15 Well is an open flow well. Tank battery consists of 1 100 barrel tank, seperator and no water tank. Signage is in place and legible. Equipment appears to be in good condition.
462276032 2011-11-18 Spud at 7:00 AM. Drilling at 150' on fluid. Anticipate setting 430' of surface casing this evening.
641878139 2011-12-05 The reserve pit is full to the point of overflowing. The working pit has 6" of freeboard. I called Andy King and he will have reserve pit built up to prevent overflow. Water removal and pit closing are scheduled for 12/7/11.