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34-121-24466

Well Details

Well ID: 34-121-24466
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2014-01-23
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 39.8799236366
Longitude: -81.4085491047

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1130141162 2014-07-09 My inspection today finds the well meets the preliminary restoration requirements. The tank battery consists of eight 400 barrel tanks set in a liquid tight containment and is shared by another well on the pad.
-170219777 2014-03-31 My inspection today finds the drilling rig, Patterson 343, has reached a total depth of 14228'. The rig is preparing to run 5.5" casing.
-2018606639 2014-02-10 My inspection finds the bottom hole assembly is being put together. The rig is preparing to drill the surface section of the well.
1390486182 2014-01-23 My inspection today finds Express Energy ran 100' of 26" conductor. Express Energy is also cementing the casing in place. 330 sks of Class A cement was circulated into place. A test of the water with a Quantab indicated the water did not contain high levels of chlorides.
1392179984 2014-02-11 The drilling rig, Patterson 343, ran 385' of 18.625" casing. Allied circulated 744 sks of class A cement into place.