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34-111-22477

Well Details

Well ID: 34-111-22477
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1981-07-25
Unconventional:
Horizontal:
Producing: No
Violations: 5
Latitude: 39.8545099271
Longitude: -81.1258051591

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1082963784 2013-12-10 Compliance agreement # 1393718879 & 2108127806 follow up inspection found the well idle with only 4.5 production casing present with no production equipment hooked up or present and no current gas sales chart in the meter. Production records show no reported production in the Database. Instructions are as follows- File for a plugging permit within 30 days. ODNR contact- Monroe Co Inspector Bill Stolarik 1-740-507-6592. NONE
-1393718879 2010-01-04 FOLLOW UP TO NOV # -2108127806 Well is idle and not capable. I called and talked to Bill Arnholt of Northwood Energy.No production reports filed.
-1628218038 2013-12-11 On this day I spoke with Bill Arnholt with Northwood energy and He confirmed that the well 4.5 production casing has a hole in it up high possibly from a coal seam, They will file for a plugging permit.
-186975000 2010-01-04 FOLLOW UP TO NOV # -2108127806 Well is idle and not capable. I called and talked to Bill Arnholt of Northwood Energy.No production reports filed.
-2108127806 2010-01-04 Well is idle and not capable. I called and talked to Bill Arnholt of Northwood Energy.No production reports filed. NONE
-2108127806 2010-01-04 Well is idle and not capable. I called and talked to Bill Arnholt of Northwood Energy.No production reports filed. NONEC
-2117874206 2014-05-27 Glen Davis rig is plugging well with Cemenco placing the plugs. Well circulated good. Set bottom plug thru 2.375upset 8 round tubing.
-659286123 2010-01-04 FOLLOW UP TO NOV # -1393718879 FOLLOW UP TO NOV # -2108127806 Well is idle and not capable. I called and talked to Bill Arnholt of Northwood Energy.No production reports filed.
1181162750 2007-06-05 No violations noted, well is equipped with pump jack and tubing&rods and 1-100 bbl tank,tank site will need better dike construction when SPCC rules go into effect.
1235063472 2009-02-05 WELL HAD RODS AND TUBING AND PUMP JACK AT ONE TIME .RODS WERE PULLED OUT.PUMPJACK REMOVED.WELL IS IDLE AT PRESENT TIME.WILL CALL MIKE CORP.
1268851680 2010-03-15 Called Mike Corp on this NOV.There was a swab rig in the location. There are two 300bbl frac tanks that are 1/2 full. One is leaking. I told mike to get water truck in and remove brine out of tanks and get them back on Jr. Burkhart's farm. Put well into working order as the location dries up.No id at tank or wellhead. 9-9-05(A)10
1268851680 2010-03-15 Called Mike Corp on this NOV.There was a swab rig in the location. There are two 300bbl frac tanks that are 1/2 full. One is leaking. I told mike to get water truck in and remove brine out of tanks and get them back on Jr. Burkhart's farm. Put well into working order as the location dries up.No id at tank or wellhead. NONE
1389107407 2014-01-07 Administrative Inspection to document that contact has been made with Bill Arnholt with Northwood energy in regards to the well being idle and the 2 unresolved violations numbering 208127806 & 1393718879, Mr. Arnholt says they will apply for a plugging permit.
1402266643 2014-06-08 The said well plugging took place on 05/27/2014 with Davis Well Svc rig on the hole and Cemennco cement services, the bottom was tagged at 2,285' by the rig's wireline tools and 2 tubing was ran into 2,270' and a bottom plug was set using 30 sacks of class A cement, the 4.5 production casing was ripped at 610' and pulled to a free point at 484' , a solid plug was set covering the bottom of the surface pipe to surface from 484' to surface with the casing cut off 30 below the ground surface and a permanent marker installed. Contractors were on site removing the production equipment.