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34-167-23796

Well Details

Well ID: 34-167-23796
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1977-06-25
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 39.4019540505
Longitude: -81.6525780657

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1132615930 2010-08-30
-122429985 2010-01-19
-1579556951 2011-10-18 Inspection this day requested by landowner and lawyer to verify well still not producing. At jack, line disconnected running to house for house gas (this done 3/11). 2" steel line also still severed in garden area between tank and well when, in Spring 2010, landowner cut line plowing garden - oil leak at that time which I witnessed. In 7/11, line to tanks was cut in another spot while owner was mowing pasture. These 3 breaks make it impossible for well to produce. Landowner reports valves were shut at well @ 11/08 yet company reports 204 mcf for 2009 - they must be mistaken or report gas on the wrong well - this is not correct. Valves have not been open at well since that time (11/08) except when attempting to sell gas and discovered severed lines. This well has been idle for 3 years now yet operator continues to send royalty checks. Pictures taken.
1292596578 2010-12-16 Request from Dave Eichorn, thru Beth Wilson, for inspections to give to attorney to break lease. She sent inspections over last 2 years.
1300986524 2011-03-24
1352990834 2012-11-14 Service rig Matheney on location and have run tubing in well, to prepare for bottom plug tomorrow. Crew still digging pit but rig crew has gone home.
1382940281 2004-01-16 Inspection this day found no violations, well producing with jack, current meter, tank area clean, dry, no dike, good ID's
487545192 2012-11-19 Matheney finished plugging this well for Stonebridge this day, setting top plug 350-0'. They could not get telegraph on the 4.5" casing and records show well cemented to surface with no surface casing. They dug down around the outside and found cement - put a 350' plug inside 4.5" and cut off 30" below ground where there was cement on the outside of the casing.