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Well ID: 34-119-28740 | Loading map...
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Spud Date: 2011-07-18 | |
Unconventional: | |
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Producing: No | |
Violations: 0 | |
Latitude: 39.7728337022 | |
Longitude: -81.970814867 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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1001469119 | 2011-10-25 | Inspection conducted by Dan Goins and Pat Shreve. Kilbarger rig was running rods in the well and dealing with a down hole pump problem. | ||||
11863484 | 2011-07-27 | Rig was shut down. Schlumberger directional group decided to pull tools. They will check down hole drill motor and bit. They are using Varel #57 tricone. They have 7 7/8" tools and will go to slim hole. The depth is at 1660' and they are at the end of the curve.They will drill a 1000' lateral hole. | ||||
1311182624 | 2011-07-19 | On day of inspection G&L Drilling set 424' of 23 pound 8 5/8" surface casing. Formation Cementing is doing the cement work. | ||||
1311693159 | 2011-07-26 | G&L Drilling is at a total vertical depth of 1198'. The present TD is 1448'. The bit is going due east at 70 degrees. The end of curve is at 1674'. Then there is 1000' leg to drill. The rate of penetration is 13.5' per hour. The weight on bit is at 71.4 lbs/ft. Pump rate is at 7 bbl /min. | ||||
1312219431 | 2011-08-01 | G&L Drilling is running 4.5casing in with Weatherford cementing equipment. Ran J-55, Range 3 pipe. Ran spiral 4.5 x 5.75" from curve to the end point of lateral approximately every 22'. That is a total of 53. Then in the vertical ran 14 regular single bow or b-type. Universal will be cementing the casing in place. | ||||
1406461018 | 2011-07-21 | G&L was shut down and repairing fluid pump that Kilbarger dropped off. | ||||
246097083 | 2011-10-11 | Preliminary Restoration passed on 10-11-11 by Patrick Shreve. |