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34-169-23924

Well Details

Well ID: 34-169-23924
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1985-02-01
Unconventional:
Horizontal:
Producing: No
Violations: 1
Latitude: 40.7043832002
Longitude: -81.7629907689

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1107318195 2013-04-11 Appears to be in compliance.
-1117448615 2011-08-04 Check well today and found that well is not in operation. I checked production records and found that well has not been produced since 1998 . Contact Operator and issue Notice to plug or produce. NONE18
-1458970200 2013-07-26 NOV 1117448615 resolved with plugging of this well.
-1845682673 2011-08-04 FOLLOW UP TO NOV # 1298999867 FOLLOW UP TO NOV # -1117448615 Check well today and found that well is not in operation. I checked production records and found that well has not been produced since 1998 . Contact Operator and issue Notice to plug or produce.
-875521369 2012-01-25 I checked for any leaks and to see if cement is at surface. I did not find gas leaking and cement was only down a few feet. The casing can be cut off and area graded and seeded. The pits are closed.
1037077508 2012-01-23 Finish plugging well today with Chipco Well and Cemenco. Taged plug at 2620' but could not get 4.5" casing to rip. Tried for hours and got casing to rip at 1915'. They pulled up to 1000' and set the next plug thru 4.5" casing, on way out. They also set cement plugs at the bottom of the 8.675"casing and then from 200' to surface.
1242991303 2013-04-11 Appears to be in compliance.
1298999867 2011-08-04 FOLLOW UP TO NOV # -1117448615 Check well today and found that well is not in operation. I checked production records and found that well has not been produced since 1998 . Contact Operator and issue Notice to plug or produce.
1631188910 2011-08-04 FOLLOW UP TO NOV # -1117448615 Check well today and found that well is not in operation. I checked production records and found that well has not been produced since 1998 . Contact Operator and issue Notice to plug or produce.
2089896175 2012-01-20 This well had a hole in the 4.5" casing. Chipco Well service and Cemenco Cementing service set the bottom cement plug thru 2.375" upset tubing. They had to shoot holes in 4.5" casing to set the second combo plug because the casing could not be ripped. They shot holes from 2939' to 2926' and also set that plug thru 2.375" tubing. The water trucks and rig froze up 4 to 5 times during the job due to the inclement weather.
28378780 2002-10-10 Well is in production. Equipped with pumpjack, rods and tubing. Well is producing gas only to landowner. Tank battery has one 210 barrel tank, separator. And concrete vault for brine storage.Cloudy, 60 degrees.
548846542 2013-03-06 Appears to be in compliance.
PL618 Preliminary Restoration done information from Data Point