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Well ID: 115-20258 | Loading map...
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County: Susquehanna | |
Municipality: Rush Township | |
Operator Name: STONE ENERGY CORP | |
Farm/Lease Name: LOOMIS 2H | |
First Permit Date: 2010-02-02 | |
Last Permit Date: 2010-02-02 | |
Spud Date: 2010-08-27 | |
Unconventional: Yes | |
Horizontal: Yes | |
Producing: Yes | |
Violations: 2 | |
Latitude: 41.76608 | |
Longitude: -76.103799 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
1912888 | 2010-09-02 | Violation(s) Noted | 595222 | |
1912888 | 2010-09-02 | Violation(s) Noted | 595223 | |
1912901 | 2010-09-13 | No Violations Noted | Follow up on repair of cementing job on 13 3/8" string. Set a plug at 240-310' on 9/6 at 18:00hrs and let sit for 24 hrs. At 18:00 hrs tonight will tag TOC. Plan to perf and squeeze addtional cement around 190' zone. Bubbling observed in between 20" and 13 3/8". NOV written on 9/2 addressing violation. | |
1952107 | 2011-02-18 | No Violations Noted | On site with DEP WQS, Matt Shope to conduct an inspection of the pit. I observed that the pit has been completely filled in. Company Man, Dan Williams, informed me that the pit had been backfilled and encapsulated between 2-11 and 2-13-11. The drill cuttings were solidified the week of 2-7-11. There were no violations observed during the inspection. Please feel free to contact me if there are any questions at 570-346-5533 or jsassi@state.pa.us | |
1965420 | 2011-04-06 | No Violations Noted | Routine inspection. No activity on site. Well is shut in. When standing near well head, can hear gas venting. Could not determine source. Temporary fence around well heads. Freshwater impoundment on location. Fence in place and maintained around impoundment. Liner appears to be in good condition. Freeboard @5'. DEP will follow up with Operator on venting observed. | |
2005390 | 2011-09-14 | No Violations Noted |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2012-2 | 298617.0 | 180.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2012-1 | 373950.0 | 165.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-2 | 374904.0 | 128.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-1 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-1 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2010-2 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2010-3 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2012-2 | PRODUCED FLUID | 550.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR119 | EUREKA RESOURCES (WILLIAMSPORT WATER TREATMENT) | WILLIAMSPORT | PA |
2010-2 | FRACING FLUID WASTE | 14556.6 | Bbl | REUSE OTHER THAN ROAD SPREADING | FRAC WATER REUSE | PA | ||
2010-2 | FRACING FLUID WASTE | 851.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0027057 | WILLIAMSPORT SAN AUTH - CENTRAL STP | WILLIAMSPORT | PA |
2011-1 | DRILL CUTTINGS | 998.0 | Tons | LANDFILL | 31346244 | CASELLA WASTE SYSTEMS | PAINTED POST | NY |
2011-1 | DRILLING FLUID WASTE | 347.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0101508 | PA BRINE TRT INC - FRANKLIN PLT - VENANGO CO | FRANKLIN | PA |
2011-1 | PRODUCED FLUID | 119.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0101508 | PA BRINE TRT INC - FRANKLIN PLT - VENANGO CO | FRANKLIN | PA |
2011-1 | DRILLING FLUID WASTE | 3533.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0008451 | SUNBURY GENERATION WASTE WATER TRMT FAC | SHAMOKIN DAM | PA |
2012-1 | PRODUCED FLUID | 734.0 | Bbl | INJECTION DISPOSAL WELL | 34-099-23127 | NORTH STAR BRINE DISPOSAL | YOUNGSTOWN | OH |