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37-039-22009

Well Details

Well ID: 37-039-22009
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Operator Name: MITCH WELL ENERGY INC
First Permit Date: 1983-08-17
Last Permit Date: 1983-08-17
Spud Date: 1800-01-01
Unconventional: No
Horizontal: No
Violations: 3
Latitude: 41.794234
Longitude: -79.801138

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2012-0 100.0 365.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2012-0 PRODUCED FLUID 1.0 Bbl STORAGE PENDING DISPOSAL OR REUSE STORAGE PENDING DISPOSAL OR REUSE PA
2012-0 PRODUCED FLUID 1.0 Bbl STORAGE PENDING DISPOSAL OR REUSE STORAGE PENDING DISPOSAL OR REUSE PA

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
357117 1988-06-08 No Violations Noted
2037233 2012-01-24 Violation(s) Noted Upon inspection today Scott Lux and I found a abandon well that is unplugged. The well was tagged and shut-in. The casing was very rusty and consisted of a 13" conductor -10" surface and 4" & 2 " production strings.The production equipment consist of one steel stock tank plumbed to tthe separator- several holes are rusted through the tank; one 70 bbl poly tank (not plumbed). The regulator coming into separator was leaking a signifcant amount of gas. The production chart was last calibrated in 1986.No E&S problems.Patches of snow on the ground. 630476
2037233 2012-01-24 Violation(s) Noted Upon inspection today Scott Lux and I found a abandon well that is unplugged. The well was tagged and shut-in. The casing was very rusty and consisted of a 13" conductor -10" surface and 4" & 2 " production strings.The production equipment consist of one steel stock tank plumbed to tthe separator- several holes are rusted through the tank; one 70 bbl poly tank (not plumbed). The regulator coming into separator was leaking a signifcant amount of gas. The production chart was last calibrated in 1986.No E&S problems.Patches of snow on the ground. 630476
2075454 2012-06-13 Violation(s) Noted 642298
2075454 2012-06-13 Violation(s) Noted 642298
2076263 2012-06-13 Violation(s) Noted 641848
2076263 2012-06-13 Violation(s) Noted 641848
2076263 2012-06-13 Violation(s) Noted 641848
2118601 2012-11-20 Outstanding Violations - No Viols Req'd
2162554 2013-04-29 Crawford Bloomfield Twp Outstanding Violations - No Viols Req'd

References