If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 37-125-27081 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.074597,"lon":-80.346744,"icon":""}]} |
Operator Name: CNX GAS CO LLC | |
First Permit Date: 2013-09-04 | |
Last Permit Date: 2013-09-04 | |
Spud Date: 2013-11-02 | |
Unconventional: Yes | |
Horizontal: No | |
Violations: None | |
Latitude: 40.074597 | |
Longitude: -80.346744 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2013-2 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2013-2 | DRILL CUTTINGS | 6.21 | Tons | RESIDUAL WASTE TRANSFER FACILITY | PAD004835146 | MAX ENVIRONMENTAL TECHNOLOGIES INC YUKON FACILITY | YUKON | PA |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
2235646 | 2013-01-06 | Washington | East Finley Twp | No Violations Noted |
2243999 | 2014-02-05 | No Violations Noted | ||
2244018 | 2014-02-06 | No Violations Noted | Yost drilling for CNX using closed loop system and flare stack. On 2/5/2014 a call came in at 10:10pm that Allied was having trouble with the cement job. Pumped 200bbls or fresh water and 35bbls of gel, then 10bbls of fresh water. Next they started pumpling cement. At 95bbls of cement pumped, the pressure spiked to 2500psi while pumping at 4.5 bbls/min. Decided to bleed off pressure and try again. Pumpled 1.4 to 1.5 bbls/min. and pressure began to build again. CNX terminated cement job. 02/06/2014 CNX decided to grout casing to surface.using a 1" pour string. On 2/7/2014, 84bbls of cement was pumped throught pour string and got 1bbl to returns. |