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Well ID: 34-115-24120 | Loading map...
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Country: United States | |
State: Ohio | |
County: Morgan | |
Municipality: Bristol | |
Operator Name: STONEBRIDGE OPERATING CO LLC | |
Well Pad ID: | |
Farm/Lease Name: CUNNINGHAM | |
License Status: Producing | |
License Date: 1990-12-26 | |
Spud Date: 1990-01-24 | |
Spud Drilling Contractor: R WOLFE DRLG | |
Final Drill Date: 1991-01-31 | |
Well Total Depth: 1475 ft | |
Configuration: Vertical | |
Latitude: 39.695018271 | |
Longitude: -81.80915890 |
For data sources see[1]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 1303 | 1335 | 0 |
2006-09-11 | 1320 | 1330 | 2 |
For data sources see[1]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1996 | BT ENERGY CORP | 0 | 0 | 0 |
1997 | BT ENERGY CORP | 0 | 0 | 0 |
1998 | STONEBRIDGE OPERATING CO LLC | 0 | 0 | 0 |
2000 | STONEBRIDGE OPERATING CO LLC | 0 | 0 | 0 |
2005 | BT ENERGY CORP | 0 | 0 | 0 |
2006 | STONEBRIDGE OPERATING CO LLC | 571 | 0 | 365 |
2007 | STONEBRIDGE OPERATING CO LLC | 235 | 0 | 365 |
2008 | STONEBRIDGE OPERATING CO LLC | 185 | 0 | 365 |
2009 | STONEBRIDGE OPERATING CO LLC | 538 | 0 | 365 |
2010 | STONEBRIDGE OPERATING CO LLC | 143 | 0 | 365 |
2011 | STONEBRIDGE OPERATING CO LLC | 0 | 0 | 0 |
2012 | STONEBRIDGE OPERATING CO LLC | 0 | 0 | 357 |
2013 | STONEBRIDGE OPERATING CO LLC | 0 | 0 | 365 |
2014 | STONEBRIDGE OPERATING CO LLC | 0 | 0 | 365 |
2015 | STONEBRIDGE OPERATING CO LLC | 0 | 0 | 357 |
2016 | STONEBRIDGE OPERATING CO LLC | 0 | 0 | 350 |
2017 | STONEBRIDGE OPERATING CO LLC | 0 | 0 | 315 |
2018 | STONEBRIDGE OPERATING CO LLC | 0 | 0 | 280 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1996 | BT ENERGY CORP | Brine | 0 | 0 |
1997 | BT ENERGY CORP | Brine | 0 | 0 |
1998 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 0 |
2000 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 0 |
2005 | BT ENERGY CORP | Brine | 0 | 0 |
2006 | BT ENERGY CORP | Brine | 0 | 0 |
2007 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 365 |
2008 | STONEBRIDGE OPERATING CO LLC | Brine | 43 | 365 |
2009 | STONEBRIDGE OPERATING CO LLC | Brine | 20 | 365 |
2010 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 365 |
2011 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | |
2012 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 357 |
2013 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 365 |
2014 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 365 |
2015 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 357 |
2016 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 350 |
2017 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 315 |
2018 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 280 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0000006322 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 6/28/91 INSPECTOR TOM HALL DATE 06/2819/91 DATA FROM OLD VAX INFO | |
0000136944 | 2019-04-02 | Production Wells | No Violations | I was back on location today to do a follow-up inspection on this well. There has been no change in the status of this well. I spoke with the field supervisor John Schneider about their plan for this well and he stated they plan on plugging this well this year. |
0371871597 | 2012-02-02 | Production Wells | No Violations | FOLLOW UP TO NOV # -696653351 My inspection this day due to request from the landowner, Doug Emrick, to verify if the well is in production. I found gas well with valves shut, not capable of production. A small, 65 bbl tank is nearby and is not connected to the well. No identification was present. Northwood Energy has turned in production for 2010 and Stonebridge Operating has also turned in production for 2010 of 0 - only one operator needs to turn in production and which one is correct? Well needs plugged or put on TI list, identification needs posted and well needs placed on correct owners bond. I will give them a call and find out who owns the well. 2/24/12 - Enervest says they do not own well. |
0416758618 | 2017-01-09 | Production Wells | No Violations | The inspection today revealed that this well is equipped with a plunger lift system, a 8 5/8 inch diameter well surface casing at the surface, a 4 1/2 inch diameter wellhead, 1 1/2 inch diameter production tubing, and 2 inch diameter steel and plastic production lines. The valve on the wellhead is closed at the time of inspection. There are no associated tank with this well at the time of inspection. The well is idle at the time of inspection and there has been no resolution to the issue on this well. |
0444013045 | 2012-12-27 | Administrative Inspection | No Violations | I talked with Dave Crippen and he confirmed that they were going to bring in fill dirt to complete the removal of the dike sometime in the near future. He also said Stonebridge was talking of sending in a permit to plug this well. |
0649210225 | 2014-03-13 | Administrative Inspection | No Violations | Eddie Biehl asked the state for an extension of time until April 25 to evaluate this well and legal situation. In this time they will apply for either a permit to plug back and re-complete or to plug and abandon. He asked to then be allowed to utilize up to the full term of the permit to resolve outstanding legal issues including any pending or potential litigation in the local Court of Common Pleas. Once they are able to clear the legal issues, they will safely perform the work in the field. |
0696653351 | 2012-02-02 | Production Wells | Violations Noted | My inspection this day due to request from the landowner, Doug Emrick, to verify if the well is in production. I found gas well with valves shut, not capable of production. A small, 65 bbl tank is nearby and is not connected to the well. No identification was present. Northwood Energy has turned in production for 2010 and Stonebridge Operating has also turned in production for 2010 of 0 - only one operator needs to turn in production and which one is correct? Well needs plugged or put on TI list, identification needs posted and well needs placed on correct owners bond. I will give them a call and find out who owns the well. 2/24/12 - Enervest says they do not own well. |
0779045021 | 2010-09-28 | Production Wells | No Violations | Follow-up on NOV, In-Compliance. |
0846949401 | 2018-03-13 | Production Wells | No Violations | I was on location today to do a follow-up inspection on this well for being idle and incapable of production. Stonebridge was issued a compliance notice on 12/19/2013 for the violations on this well. At this time the well is still idle and incapable of production. All of the production valves are shut at the wellhead and all of the production equipment has been removed. No production has been reported on this well since 2010. |
0912041264 | 2014-03-13 | Production Wells | No Violations | Compliance Action Follow-up -2136013100: Identification has been posted at the wellhead and production has been reported as zero to the state. The well is still idle and there are no tanks or separators. |
0931077478 | 2013-09-04 | Production Wells | No Violations | Compliance Action Follow-up -2136013100: Well is still idle. There still has been no resolution to any of the issues. |
0990980113 | 2012-12-27 | Production Wells | No Violations | Well was not inspected. The dike, however has been cleared of all production equipment. Tenant said company came out and cleared small truckload of contamination and was going to be bringing back so fill dirt to finish job. They did not say when they were going to complete the removal of dike area. He said the landowner expressed concern over the dike area and believed contamination was more extensive than what they hauled away. I called Dave Crippen, Stonebridge well pumper, and left a message in regards to their plans. Dike is currently filled with water and ice. |
1331507957 | 2011-06-15 | Production Wells | No Violations | Inspection this day found well with rabbit, not in production. No IDs on tank. Landowner says well has not produced, Northwood had worked on it and set tank. I said Enervest is the operator of record. E-- waiting for a call back. |
1345664058 | 2012-08-22 | Administrative Inspection | No Violations | I received call today from Doug Emrick, Jr. saying lease had been broke and would like well plugged. When I asked who was operator, he thought it was Enervest. RBDMS shows very conflicting information and when NOV was mailed to Enervest, they called and said it was not their well. I explained that well already a citation and they had no time deadlines for plugging it. |
1352149205 | 2012-10-17 | Production Wells | Violations Noted | Well was not inspected. Tank Battery was inspected and ID was labeled as Cunninham 5-B. Diked area still exists with production equipment tangled in overgrown vegetation. Diked area also has oil and water contamination on surface all around and beyond the 1 100 barrel tank. Tank is empty and all flow lines have been disconnected. Meter is still hooked up but inactive and landowners renter stated he no longer receives house gas. All production equipment needs to be removed and diked area needs to be cleaned of contamination followed by restoration. I called Northwood and talked to Bill and he said the well equipment is not Northwoods. I called Enervest and Alan Tartlton stated the well was never in Enervests possession. Production is being reported by both Stonebridge and Northwood. I have told both Alan and Bill they need to correct their involvement in this situation with Columbus. Stonebridge has been contacted with no return call. Failure to comply may result in a forfeiture of Bond. |
1355333310 | 2012-12-12 | Administrative Inspection | No Violations | John Schneider left me a message today to inform me he was sending field worker to tank battery location today to remove remaining fluid from tank. He also stated in message that either this Thursday or Friday they would be out to remove the tank and production equipment. |
1387486957 | 2013-12-19 | Production Wells | Violations Noted | I received paperwork from the Doug Emrick, the landowner, showing a canceled lease filed by his attorney at the Morgan County Courthouse. The inspection revealed an idle well with 8 and 4 1/2 casing. All valves were shut at well head and there are flow lines, however Stonebridge removed the tank and separator from the dike. They also removed and restored the dike location. Operator must produce well within 30 days or plug the well within 90 days. |
1387812805 | 2013-12-19 | Production Wells | No Violations | Compliance Action Follow-up -2136013100: The operator has removed the tank and separator from the dike and cleaned up the contamination. They have also removed and restored the dike location. The compliance action -2136013100 is now void and a new produce or plug compliance action (1387486957) has been issued to Stonebridge. |
1392998665 | 2014-02-21 | Production Wells | No Violations | Compliance Action Follow-up -2136013100: The well is still idle and overgrown with sawbriar. The tank and separator have all been removed and Stonebridge has restored the dike, which is now being used as feeding area for cattle. Doug Emerick stated they receive no house gas from the well and they are in the process of breaking the lease with their attorney. I called and left a message with John Schneider in regards to the well issues. |
1398695916 | 2014-04-28 | Production Wells | No Violations | Compliance Action Follow-up -2136013100: The inspection revealed an idle well with 8 and 4 1/2 casing. All valves were shut at well head and there are flow lines, however Stonebridge removed the tank and separator from the dike. They also removed and restored the dike location. |
1449717831 | 2012-11-06 | Administrative Inspection | No Violations | Jim Schneider with Stonebridge called and left a message stating the pumper went out and looked at the dike issue and that they will start on cleanup. Only the tank battery was inspected for the Cunningham 5-B. I returned the call to Jim and left a voicemail stating the well was still showing up as Enervests and that needed to be corrected ASAP. |
1501129413 | 2018-08-22 | Production Wells | No Violations | I have returned to this well today to do a follow-up inspection on it. At this time the well is still sitting idle and incapable of production. The production valves on the well are currently closed making the well incapable of any type of production. The well is still in violation at this time. |
1769645899 | 2012-11-13 | Production Wells | No Violations | Stonebridge has recently been out to tank battery and cleared it of vegetation. Production equipment still on location and visible contamination still exists within dike. Valves are all shut off and there is no chart or meter. There is a house meter and one 100 barrel tank. Well head inspection revealed 8 and 4 1/2 casing. All valves were shut at well head. I called and left a message for John Schneider with Stonebridge to discuss cleanup and ownership discrepancy. |
1913795995 | 2018-01-24 | Production Wells | No Violations | I was on location today to do a follow-up inspection on this well. At this time the well is still idle and incapable of production. All of the production valves are shut at the wellhead and all of the production equipment has been removed. |
1946092474 | 2013-04-30 | Production Wells | No Violations | Compliance Action Follow-up -2136013100: There still has been no resolution to any of the issues. Well is still in non-compliance. |
2036960463 | 2010-03-15 | Production Wells | Violations Noted | An inspection of the well revealed no ID at the well or on storage tank, all producing leases shall be legibly identified in a conspicuous place on or near the well-head or the storage tank (s) as to owner, lease name, well number, permit number, county, and an emergency telephone number. |
2124413286 | 2018-12-13 | Production Wells | No Violations | I was back on location today to do a follow-up on this well. At this time the well is still idle and is not in production. I called John Schneider and am just waiting on a phone call back at this time. |
2136013100 | 2012-12-06 | Production Wells | Violations Noted | I called John Schneider with Stonebridge and left message this morning in regards to getting production equipment removed from area. John had left a message stating Enervest was working on the paperwork for the well. He left me a number for an Enervest representative named Amber. I called her and she told me ODNR DOGRM had corrected the ownership from Enervest to Stonebridge. RBDMS confirms this correction. She also stated that John Schneider had told her the well was in fact a Stonebridge well. I called John back and left a message that Stonebridge is now fully responsible for the well and production equipment and he needs to have it all removed and restored to original grade. I also explained that the actual well is incapable of producing and needs to be plugged. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0696653351 | US-OH-127890 | 2014-04-10 | Failure to legibly identify well | |
0696653351 | US-OH-127891 | 2014-04-10 | Nonproduction; well shall be plugged or placed in temporary inactive status | |
1352149205 | US-OH-110189 | 2013-10-22 | Forfeiture of bond | |
1352149205 | US-OH-110190 | 2013-10-22 | Non urban - failure to meet tank battery setbacks from an inhabited structure | |
1387486957 | US-OH-111486 | 2014-04-10 | Well shall be plugged | |
1387486957 | US-OH-111487 | 2014-04-10 | Nonproduction; well shall be plugged or placed in temporary inactive status | |
2036960463 | US-OH-120634 | 2010-03-16 | Failure to legibly identify well | |
2136013100 | US-OH-121900 | 2014-01-28 | Forfeiture of bond | |
2136013100 | US-OH-121901 | 2014-01-28 | Failure to legibly identify well | |
2136013100 | US-OH-121902 | 2014-01-28 | Well shall be plugged | |
2136013100 | US-OH-121903 | 2014-01-28 | Failure to keep dike or pit free of brine or other wastes |
For data sources see[1]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
FOAM | 0 | 600 Bbl | 10000 | FOAM FRAC |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1988-12-23 | 471 EAGLE MOUNTAIN ENERGY GeoDate 12/23/88 |
Oil and Gas | 1988-12-23 | Issued Date 12/23/88 Expired Date 12/23/89 Acres 0010000 Tool Type RTA Proposed Formation BEREA Proposed Depth 00000 Proposed Drill Depth 00000 |
CO | 1990-12-26 | 471 EAGLE MOUNTAIN ENERGY GeoDate 12/26/90 |
Oil and Gas | 1990-12-26 | Issued Date 12/26/90 Expired Date 12/26/91 Acres 0010000 Tool Type RTA Proposed Formation BEREA Proposed Depth 01475 Proposed Drill Depth 01475 |
Original Spud | 1991-01-30 | RI 12-29-90 |
Completed | 1991-01-31 | RI 12-29-90 |
Reached Total Depth | 1991-01-31 | RI 12-29-90 |
Completion Report Received | 1991-02-12 | RI 12-29-90 |
Construction Permit Expires | 1991-12-26 | RI 12-29-90 |
Change of Owner | 2003-08-11 | Operator changed from 471, EAGLE MOUNTAIN ENERGY to 28, CGAS EXPLORATION |
Change of Owner | 2003-09-08 | Operator changed from 471, EAGLE MOUNTAIN ENERGY to 28, CGAS EXPLORATION |
Change of Owner | 2007-04-27 | Operator changed from 28, CGAS EXPLORATION to 7578, ENERVEST OPERATING LLC |
Record Last Modified | 2017-02-15 | RI 12-29-90 |
For data sources see[1]