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Well ID: 34-083-20374 | Loading map...
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Country: United States | |
State: Ohio | |
County: Knox | |
Municipality: Jackson Township | |
Operator Name: VALLEY PETROLEUM MANAGEMENT | |
Well Pad ID: | |
Farm/Lease Name: ROBERT & ELLA TROYER | |
License Status: Producing | |
License Date: | |
Spud Date: 1943-05-04 | |
Spud Drilling Contractor: | |
Final Drill Date: 1943-06-15 | |
Well Total Depth: 3029 ft | |
Configuration: Vertical | |
Latitude: 40.305968557 | |
Longitude: -82.22746597 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1801-01-02 | 2936 COLUMBIA NATURAL RES INC |
Original Spud | 1943-05-04 | GL=1043.9 I.P. NAT. GAS 0.05 PER. |
Completed | 1943-06-15 | GL=1043.9 I.P. NAT. GAS 0.05 PER. |
Reached Total Depth | 1943-06-15 | GL=1043.9 I.P. NAT. GAS 0.05 PER. |
CO | 1991-07-31 | 360 RELIANCE ENERGY INC GeoDate |
Change of Owner | 1999-07-06 | Operator changed from 360, RELIANCE ENERGY INC to 231, VALLEY PETROLEUM MANAGMNT |
Record Last Modified | 2014-12-30 | GL=1043.9 I.P. NAT. GAS 0.05 PER. |
Correction to Well | 2015-01-02 | UPDATE OF LEASE NAME, UNIT SIZE, X,Y COORDINATES AND FOOTAGE FROM NEW PLAT. NO PREVIOUS PLAT ON FILE. |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
Not Treated | 0 | 120 Qts | 0 |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
1361997838 | 2013-02-27 | Production Wells | Violations Noted | I received a call from Denny Dugan, Valley Petroleum Management stating that he had a production line leak that had contaminated a stream with an estimated 10 gallon combination of Crude oil and brine. During my inspection I found that there was sheen on the water down a feeder stream and down Wakatomika Creek a total of 3800 feet. Chris Holmes from EPA is on site conducting an inspection and overseeing the clean up of the stream. Inspectors Jeff Fry, Tom Zacharyasz, and Will Ziegler were also present on site. Talked with the land owner and he stated that he had reported the leak earlier that morning. The company needs to clean up any stain and contamination around the leak by 2/27/2013, and repair or replace the line before the well is placed back into production. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1361997838 | US-OH-110542 | 2013-03-08 | Well operation causing pollution and contamination |
For data sources see[8]