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37-065-00161

Well Details

Well ID: 37-065-00161
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Country: United States
State: Pennsylvania
County: Jefferson
Municipality: Porter Township
Operator Name: EQT PROD CO
Well Pad ID:
Farm/Lease Name: WG SHICK 1
License Status: Plugged OG Well
Spud Date: 1800-01-01
Permit Date:
Unconventional Well: N
Configuration: Vertical Well
Latitude: 40.941183
Longitude: -79.203272

For data sources see[1][2][3]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1986 APOLLO GAS CO 674 279 0.00 0 0.00 0
1987 APOLLO GAS CO 549 362 0.00 0 0.00 0
1988 APOLLO GAS CO 691 374 0.00 0 0.00 0
1989 APOLLO GAS CO 1,397.00 372 0.00 0 0.00 0
1991 APOLLO GAS CO 833.00 329 0.00 0 0.00 0
1997 CARNEGIE PROD CO 712.00 365 0.00 0 0.00 0
1998 CARNEGIE PROD CO 0.00 0 0.00 0 0.00 0
1999 CARNEGIE PROD CO 0.00 0 0.00 0 0.00 0
2000 EQUITRANS INC 0.00 0 0.00 0 0.00 0
2001 EQUITABLE PROD EASTERN STATES EXPLORATION INC 0.00 0 0.00 0 0.00 0
2003 EQT PROD CO 0.00 0 0.00 0 0.00 0
2004 EQT PROD CO 0.00 0 0.00 0 0.00 0
2005 EQT PROD CO 0.00 0 0.00 0 0.00 0
2006 EQT PROD CO 0.00 0 0.00 0 0.00 0
2007 EQT PROD CO 0.00 0 0.00 0 0.00 0
2008 EQT PROD CO 0.00 0 0.00 0 0.00 0
2009 EQT PROD CO 161.00 61 0.00 0 0.00 0
2010 EQT PROD CO 156.00 59 0.00 0 0.00 0
2011 EQT PROD CO 0.00 0 0.00 0 0.00 0
2012 EQT PROD CO 0.00 0 0.00 0 0.00 0
2013 EQT PROD CO 0.00 0 0.00 0 0.00 0
2014 EQT PROD CO 0.00 0 0.00 0 0.00 0
2015 EQT PROD CO 0.00 0 0.00 0 0.00 0
2016 EQT PROD CO 0.00 0 0.00 0 0.00 0
2017 EQT PROD CO 0.00 0 0.00 0 0.00 0
2018 EQT PROD CO 0.00 0 0.00 0 0.00 0

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2579772 Primary Facility 2017-04-06 Administrative/File Review No Violations Noted
2601043 Primary Facility 2017-05-23 Plugging(Includes Plugged/Mined Through) No Violations Noted
2601144 Primary Facility 2017-06-02 Plugging(Includes Plugged/Mined Through) No Violations Noted
2607776 Primary Facility 2017-06-20 Plugging(Includes Plugged/Mined Through) No Violations Noted
2670795 Primary Facility 2017-12-14 Plugging(Includes Plugged/Mined Through) No Violations Noted Dawn Energy Services rig on location. They have run 7" and 4 1/2" casing. 3" appears to be inside the 4 1/2" according to the camera run. Planning on running a tapered mill to open top of stub.
2681382 Primary Facility 2018-01-11 Plugging(Includes Plugged/Mined Through) No Violations Noted Dawn Energy Services rig on location. They have run 7" and 4 1/2" casing. Ran 1" tubing to 227' and tagged out. Pulled 1" and are preparing to run 1 1/2" with a mill.
2689102 Primary Facility 2018-01-31 Plugging(Includes Plugged/Mined Through) No Violations Noted Currently running a concave mill. Are losing hole. Lost approximately 10" while I was on location.
2708206 Primary Facility 2018-03-08 Plugging(Includes Plugged/Mined Through) No Violations Noted Made to 421' yesterday. Set overnight and mill plugged off. Tripped in to 1420'. Tubbing was setting off several times per joint and stopped moving at current depth.
2708214 Primary Facility 2018-03-12 Administrative/File Review No Violations Noted Phone call with Beau Fry. Discussed video ran on 3/9. Camera run showed that the tubing went outside the 3 1/2" casing at approximately 267'. The intact 3 1/2" casing was then seen on the side of the video.
2708217 Primary Facility 2018-03-21 Plugging(Includes Plugged/Mined Through) No Violations Noted Currently setting up to run spear.
2714848 Primary Facility 2018-04-05 Plugging(Includes Plugged/Mined Through) No Violations Noted Attainable bottom was given at '. 2 3/8" tubing was run down between the 3 1/2" production casing. And 8 5/8" surface casing. Perforation gun (37 shots- 6' gun) was run inside 2 3/8" tubing and used to perforate both the 2 3/8" and 3 1/2". 2 3/8" tubing will be left in the well to ensure cement is able to be pumped without risk of well caving or having issues at the 3 1/2" stub. 4.7 Bbl pumped and tagged cement this morning at 1086'. Ran another perforation gun (1056' 30 shots). Pumped 4.7 Bbl and will tag cement this afternoon after 5 hours.
2732973 Primary Facility 2018-05-22 Administrative/File Review No Violations Noted Reviewed alternate method and plugging certificate

For data sources see[5]

References