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Well ID: 37-065-00161 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Jefferson | |
Municipality: Porter Township | |
Operator Name: EQT PROD CO | |
Well Pad ID: | |
Farm/Lease Name: WG SHICK 1 | |
License Status: Plugged OG Well | |
Spud Date: 1800-01-01 | |
Permit Date: | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Latitude: 40.941183 | |
Longitude: -79.203272 |
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1986 | APOLLO GAS CO | 674 | 279 | 0.00 | 0 | 0.00 | 0 |
1987 | APOLLO GAS CO | 549 | 362 | 0.00 | 0 | 0.00 | 0 |
1988 | APOLLO GAS CO | 691 | 374 | 0.00 | 0 | 0.00 | 0 |
1989 | APOLLO GAS CO | 1,397.00 | 372 | 0.00 | 0 | 0.00 | 0 |
1991 | APOLLO GAS CO | 833.00 | 329 | 0.00 | 0 | 0.00 | 0 |
1997 | CARNEGIE PROD CO | 712.00 | 365 | 0.00 | 0 | 0.00 | 0 |
1998 | CARNEGIE PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1999 | CARNEGIE PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2000 | EQUITRANS INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2001 | EQUITABLE PROD EASTERN STATES EXPLORATION INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2003 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2004 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2005 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2006 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2007 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2008 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2009 | EQT PROD CO | 161.00 | 61 | 0.00 | 0 | 0.00 | 0 |
2010 | EQT PROD CO | 156.00 | 59 | 0.00 | 0 | 0.00 | 0 |
2011 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2018 | EQT PROD CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[4]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2579772 | Primary Facility | 2017-04-06 | Administrative/File Review | No Violations Noted | |
2601043 | Primary Facility | 2017-05-23 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | |
2601144 | Primary Facility | 2017-06-02 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | |
2607776 | Primary Facility | 2017-06-20 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | |
2670795 | Primary Facility | 2017-12-14 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Dawn Energy Services rig on location. They have run 7" and 4 1/2" casing. 3" appears to be inside the 4 1/2" according to the camera run. Planning on running a tapered mill to open top of stub. |
2681382 | Primary Facility | 2018-01-11 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Dawn Energy Services rig on location. They have run 7" and 4 1/2" casing. Ran 1" tubing to 227' and tagged out. Pulled 1" and are preparing to run 1 1/2" with a mill. |
2689102 | Primary Facility | 2018-01-31 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Currently running a concave mill. Are losing hole. Lost approximately 10" while I was on location. |
2708206 | Primary Facility | 2018-03-08 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Made to 421' yesterday. Set overnight and mill plugged off. Tripped in to 1420'. Tubbing was setting off several times per joint and stopped moving at current depth. |
2708214 | Primary Facility | 2018-03-12 | Administrative/File Review | No Violations Noted | Phone call with Beau Fry. Discussed video ran on 3/9. Camera run showed that the tubing went outside the 3 1/2" casing at approximately 267'. The intact 3 1/2" casing was then seen on the side of the video. |
2708217 | Primary Facility | 2018-03-21 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Currently setting up to run spear. |
2714848 | Primary Facility | 2018-04-05 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Attainable bottom was given at '. 2 3/8" tubing was run down between the 3 1/2" production casing. And 8 5/8" surface casing. Perforation gun (37 shots- 6' gun) was run inside 2 3/8" tubing and used to perforate both the 2 3/8" and 3 1/2". 2 3/8" tubing will be left in the well to ensure cement is able to be pumped without risk of well caving or having issues at the 3 1/2" stub. 4.7 Bbl pumped and tagged cement this morning at 1086'. Ran another perforation gun (1056' 30 shots). Pumped 4.7 Bbl and will tag cement this afternoon after 5 hours. |
2732973 | Primary Facility | 2018-05-22 | Administrative/File Review | No Violations Noted | Reviewed alternate method and plugging certificate |
For data sources see[5]