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Well ID: 34-031-25529 | Loading map...
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Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Tuscarawas Township | |
Operator Name: M & R INVESTMENTS OHIO LLC | |
Well Pad ID: | |
Farm/Lease Name: WILKINS JAMES | |
License Status: Producing | |
License Date: 1984-11-30 | |
Spud Date: 1985-01-02 | |
Spud Drilling Contractor: MID ATLANTC DRLG | |
Final Drill Date: 1985-01-06 | |
Well Total Depth: 4213 ft | |
Configuration: Vertical | |
Latitude: 40.286546895 | |
Longitude: -81.83222660 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1984-11-30 | Issued Date 11/30/84 Expired Date 11/30/85 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 04213 Proposed Drill Depth 04213 |
Original Spud | 1985-01-02 | CHG ACREAGE 4-2-94 |
Completed | 1985-01-06 | CHG ACREAGE 4-2-94 |
Reached Total Depth | 1985-01-06 | CHG ACREAGE 4-2-94 |
CO | 1985-01-30 | 98 NGO DEVELOPMENT CORP. GeoDate 11/30/84 |
Completion Report Received | 1985-03-14 | CHG ACREAGE 4-2-94 |
Construction Permit Expires | 1985-11-30 | CHG ACREAGE 4-2-94 |
Change of Owner | 2018-03-07 | Operator changed from 98, NGO DEVELOPMENT CORP. to 8685, M & R INVESTMENTS OHIO LLC |
Record Last Modified | 2018-03-08 | CHG ACREAGE 4-2-94 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 3978 | 4055 | 0 |
2006-09-11 | 4046 | 4055 | 1 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1400 Bbl | 350000 | FRAC;H2O,SAND | ||
ACID | 0 | 294 Gal | 0 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0553492748 | 2018-08-06 | Production Wells | Violations Noted | On the day of my inspection I found that the well was equipped with a plunger lift. There was a loud audible hiss from a gas leak at the wellhead. There was a clamp on the casing, but it was still leaking gas. I called Dale Smith to report the gas leak. This well shares the production equipment with the Wilkins 1, permit 4824. There was no identification at the wellhead and the updated ID sign on the tank was only labeled for the Wilkins 1. The production equipment consisted of one 210 barrel steel tank, one 100 barrel steel tank and two separators in an earthen dike. There were no leaks or spills around the tanks. The gas leak at the wellhead must be repaired, and identification must be posted at the wellhead and tanks. |
1161273354 | 2006-10-19 | Production Wells | No Violations | Well in production . |
1229858380 | 2018-08-28 | Production Wells | No Violations | I was contacted by Diversified to notify me that the compliance issues at this well had been resolved. On the day of my inspection I found that there was a man at the well, installing new fittings and reconnecting the lines. There were tracks from a service rig leading to the wellhead. There was a new joint of 4.5 inch diameter casing in the top of the well. The gas leak had been repaired. I also found that correct, legible identification had been posted for the well. The compliance notice is resolved. |
1327261524 | 2005-03-28 | Production Wells | No Violations | Well in production . |
2071585384 | 2003-02-06 | Production Wells | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0553492748 | US-OH-126099 | 2018-11-28 | 9-9-05(A)1 | Well insufficiently equipped to prevent escape of oil and gas |
0553492748 | US-OH-126100 | 2018-11-28 | 9-9-05(A)10 | Failure to legibly identify well |
For data sources see[9]