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| County: [[Noble_County,_Ohio|Noble]] | | County: [[Noble_County,_Ohio|Noble]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Wayne Township,_Noble_County,_Ohio|Wayne Township]] |
|- | |- | ||
| Operator Name: [[ENERVEST OPERATING LLC]] | | Operator Name: [[ENERVEST OPERATING LLC]] |
Well ID: 34-121-22101 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Wayne Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: BEHM A | |
License Status: Final Restoration | |
License Date: 2012-12-06 | |
Spud Date: 1979-08-13 | |
Spud Drilling Contractor: | |
Final Drill Date: 1979-08-28 | |
Well Total Depth: 5653 ft | |
Configuration: Vertical | |
Latitude: 39.914103551 | |
Longitude: -81.45629671 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1979-04-25 | 2143 CARLESS RESOURCES INC GeoDate 4/25/79 |
Original Spud | 1979-08-13 | R.I. 5-2-79 |
Completed | 1979-08-28 | R.I. 5-2-79 |
Reached Total Depth | 1979-08-28 | R.I. 5-2-79 |
Change of Owner | 1998-07-06 | Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2012-12-06 | Proposed Formations:CLINTON, Issued Date:12/6/2012, Expired Date:12/6/2014 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2013-09-12 | R.I. 5-2-79 |
Record Last Modified | 2014-07-25 | R.I. 5-2-79 |
Construction Permit Expires | 2014-12-06 | R.I. 5-2-79 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5563 | 5591 | 1 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1300 Bbl | 55000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0056479493 | 2013-12-19 | Final Restoration | No Violations | The final restoration has been completed. All equipment has been removed. |
0259793562 | 2013-04-11 | Production Wells | No Violations | Follow up to Compliance Notice #1350909565. The status of the well has not changed. The operator was issued a permit to plug on 12/6/2012. |
0500047517 | 2013-09-09 | Plug / Plug Back | No Violations | Chipco ran six drill collars and a tooth bit. The service rig ran to a depth of 3790 and began to run the swivel. The rig crew drilled down to a depth of 3980, they pulled up to 3760 and shut the well in. |
1072157192 | 2013-09-04 | Plug / Plug Back | No Violations | My inspection today finds the plugging contractor, Chipco, ran a 4.5 spear and pulled on the casing. The casing moved up two inches and gave them enough room to weld a new piece of pipe on. |
1338807403 | 2012-06-04 | Production Wells | No Violations | Inspection of the well found 8.625 casing -4.5 production casing with a 4 to 2 swage on the casing and the well shut in at the time of inspection with no reported production since 2002. A separator is present and the production tank has been removed . |
1350909565 | 2012-10-22 | Production Wells | Violations Noted | My inspection today finds the well is equipped with 4.5 casing reduced to 2. All valves at the well are closed. The well has not produced gas in commercial quantities since 2003. RETURN THE WELL TO PRODUCTION OR PLUG. Failure to comply may lead to forfeiture of bond. |
1377690106 | 2013-08-26 | Plug / Plug Back | No Violations | My inspection today finds Chipco is attempting to get their tools down the well. They casing is tight at 690. Chipco attempted to circulate but was unable to pump any volume of fluid. They then attempted to pump down the 8.625 to free the casing and could not pump any fluid away. |
1378690069 | 2013-09-06 | Plug / Plug Back | No Violations | My inspection today finds Chipco is using a power swivel and mud pump to drill through the obstruction at 690. The bit was ran to 915. The rig crew pulled the tubing. The wire line tools sat down at 3830. The tubing swab tools ran to a depth of 3950 before stopping. |
1379422634 | 2013-09-12 | Plug / Plug Back | No Violations | Chipco set a 60 sk rip plug at 3430. They then pulled up to 1400 and set a 60 sk plug. A 200 sixty sk plug was set from 630 up to 430. The surface plug was placed from 200 up to surface. I asked the plugging contractor reclaim the site according to ORC 1509:072. |
1447033000 | 2013-09-11 | Plug / Plug Back | No Violations | The rig crew ran tubing to 3970. Chipco spotted a 72 sk plug. The well circulated. The rig crew pulled the tubing and ripped casing at 3430. |
1525686098 | 2013-09-05 | Plug / Plug Back | No Violations | My inspection today finds Chipco is running six drill collars, a bit sub, and a tooth bit on 2.375 tubing. The rig crew ran to a depth of 615 and packed the well off. A power swivel and mud pump were brought to location and being put in place. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1350909565 | US-OH-110163 | 2013-12-11 | Nonproduction; well shall be plugged or placed in temporary inactive status |
For data sources see[9]