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Difference between revisions of "37-015-20416"

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== Well Details ==
 
== Well Details ==
{| class="wikitable" width="95%"
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{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-015-20416
 
| Well ID: 37-015-20416
| style="width: 50%; height=100%; align=center" rowspan="14" | {{#display_map: 41.658044, -76.286719 | width=100% | height=100% }}  
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| style="height=100%; align=center" rowspan="14" | {{#display_map: 41.658044, -76.286719 | width=100% | height=100% }}  
 
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| County: [[Bradford County, Pennsylvania|Bradford]]
 
| County: [[Bradford County, Pennsylvania|Bradford]]

Revision as of 16:55, 26 June 2014

Well Details

Well ID: 37-015-20416
Loading map...
County: Bradford
Municipality: Terry Township
Operator Name: CHESAPEAKE APPALACHIA LLC
Well Pad ID: 149713
Farm/Lease Name: WELLES 4 2H
First Permit Date: 2009-09-02
Last Permit Date: 2009-09-02
Spud Date: 2009-12-29
Unconventional: Yes
Horizontal: Yes
Producing: Yes
Violations: 5
Latitude: 41.658044
Longitude: -76.286719

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
1878399 2010-04-14 Violation(s) Noted Copied to Chapter 105 Permit file No. GP0708160904 585465
1878399 2010-04-14 Violation(s) Noted Copied to Chapter 105 Permit file No. GP0708160904 585466
1878399 2010-04-14 Violation(s) Noted Copied to Chapter 105 Permit file No. GP0708160904 585467
1878399 2010-04-14 Violation(s) Noted Copied to Chapter 105 Permit file No. GP0708160904 585468
1878399 2010-04-14 Violation(s) Noted Copied to Chapter 105 Permit file No. GP0708160904 585469
1911356 2010-09-08 No Violations Noted sept 6th 2010 perfs @ 4650-4651 7 shots pumped 42 bbl of cement behind pipe. 75 lbs on 9 5/8 casing
1912075 2010-09-10 No Violations Noted 9 5/8 open 0 psi venting gas perf @1900-1902 6 shots per ft going to pump 80 bbl cement behind pipe.
1913748 2010-09-15 No Violations Noted sept 14th perfed @ 3292-3293 6 shots per ft pumped 64 bbl cement behind pipe/// sept 15th 6 shots @ 2450 ft pumped 39 bbl cement behind pipe
1915422 2010-09-21 No Violations Noted sept 16th did 2 squeeze jobs 1@4450 ft pumped 42 bbl cement 2nd @ 2000 ft pumped 42 bbl cement
2063471 2012-04-25 No Violations Noted Rig - Longhorn 37 Comp. Man - Matt Duncan

Did a squeeze @ 3292' on 5 1/2" csg. Pressure tested yesterday and held.

2123170 2012-12-10 No Violations Noted

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2012-2 0.0 0.0 0.0 0.0 0.0 0.0
2012-1 0.0 0.0 0.0 0.0 0.0 0.0
2011-2 0.0 0.0 0.0 0.0 0.0 0.0
2011-1 0.0 0.0 0.0 0.0 0.0 0.0
2010-2 0.0 0.0 0.0 0.0 0.0 0.0
2010-3 0.0 0.0 0.0 0.0 0.0 0.0
2009-0 0.0 0.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2012-2 PRODUCED FLUID 105.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2012-1 PRODUCED FLUID 1743.5 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING

References