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Well ID: 42-015-20865 | Loading map...
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County: Bradford | |
Municipality: Orwell Township | |
Operator Name: CHESAPEAKE APPALACHIA LLC | |
Farm/Lease Name: REXFORD 5H | |
First Permit Date: 2010-05-06 | |
Last Permit Date: 2010-05-06 | |
Spud Date: 2010-06-07 | |
Unconventional: Yes | |
Horizontal: Yes | |
Producing: Yes | |
Violations: 1 | |
Latitude: 41.877794 | |
Longitude: -76.309322 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
1976895 | 2011-05-18 | Violation(s) Noted | 22% LEL combustible gas off of 13 5/8 vent port | 612379 |
1987627 | 2011-07-14 | Outstanding Violations - No Viols Req'd | 20 3 pressure on 13 3/8. 2 1/2% combustible gas being vented to atomosphere. | |
2001690 | 2011-08-25 | Outstanding Violations - No Viols Req'd | 40% combustible gas off of 13 3/8. 2% comb gas off of 9 5/8. Not vented to tank. No bubbles in cellar. | |
2024141 | 2011-12-05 | No Violations Noted | Visible bubbling in the cellar. Cannot determine where gas is coming from as cellar is filled with water. Bubbling may be from communication with the 2H. | |
2032643 | 2012-01-05 | Outstanding Violations - No Viols Req'd | 13 3/8' x 20' annulus leaking gas | |
2033422 | 2012-01-11 | Outstanding Violations - No Viols Req'd | drilling out frac plugs and are at 9606 at present | |
2049353 | 2012-03-05 | No Violations Noted | workover rig onsite. Crew onsite monitoring pressures
13 3/8 - 0 psi 9 5/8 7 psi 5 1/2 180 psi |
|
2049371 | 2012-01-18 | No Violations Noted | Flowback crew onsite monitoring pressures. Wireline run this AM. Logs run 1/17 and 1/18. Logs to be reviewed by engineers 1/19 | |
2063654 | 2012-03-12 | No Violations Noted | 13 3/8 vent - 0% combustible gas, 0 psi
9 5/8 vent - no vent 5 1/2 - 250 psi on gague./no vent |
|
2098741 | 2012-09-10 | No Violations Noted | 13 3/8 casing pressure - gauge reads 0 psi, 0% combustible gas off of vent.
9 5/8 casing pressure - gauge reads 0 psi - not vented 5 1/2 casing pressure - gauge reads 0 psi Cellar pumped down - no visible bubbling |
|
2098742 | 2012-09-05 | No Violations Noted | 13 3/8 casing pressure - gauge reads 0 psi, .5% combustible gas off of vent. Meter holds at
.25% combustible gas 9 5/8 casing pressure - gauge reads 0 psi - not vented 5 1/2 casing pressure - gauge reads 0 psi Cellar pumped down - no visible bubbling |
|
2098743 | 2012-08-27 | No Violations Noted | 13 3/8 casing pressure - gauge reads 0 psi, 1% combustible gas spike off of vent. Meter holds at .5% combustible gas
9 5/8 casing pressure - gauge reads 0 psi - not vented 5 1/2 casing pressure - gauge reads 0 psi Cellar pumped down - no visible bubbling |
|
2098744 | 2012-08-22 | No Violations Noted | 13 3/8 casing pressure - gauge reads 0 psi, 1% combustible gas spike off of vent. Meter holds at .5% combustible gas
9 5/8 casing pressure - gauge reads 0 psi - not vented 5 1/2 casing pressure - gauge reads 0 psi Cellar pumped down - no visible bubbling |
|
2098745 | 2012-08-16 | No Violations Noted | 13 3/8 X 9 5/8 casing pressure - gauge reads 0 psi, 0% combustible gas off of vent.
9 5/8 X 5 1/2 casing pressure - gauge reads 0 psi - not vented 5 1/2 casing pressure - gauge reads 0 psi Cellar pumped down - no visible bubbling |
|
2098746 | 2012-07-05 | No Violations Noted | 13 3/8 X 9 5/8 casing pressure - gauge reads 0 psi, 0% combustible gas off of vent.
9 5/8 X 5 1/2 casing pressure - gauge reads 0 psi - not vented 5 1/2 casing pressure - gauge reads 0 psi Cellar pumped down - no visible bubbling |
|
2120031 | 2012-10-10 | No Violations Noted | Back pressure vavle installed. Performing 48 hour shut-in tests. Well currently shut-in. 13 3/8 - 0 psi. 9 5/8 - 0 psi (pop-off valve installed). 5 1/2 - 275 psi. | |
2120677 | 2012-10-03 | No Violations Noted | 13 X 9 - 0 psi 0.2 %spike comb gas
9 X 5 - (not vented) 0psi 5 1/2 - 330 psi |
|
2120685 | 2012-09-25 | No Violations Noted | 13 X 9 -(vented) - 0psi - 2% combustible gas spike
9 X 5 (not vented) - 0 psi 5 1/2 production casing 190 psi |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2012-2 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2012-1 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-2 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-1 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2010-2 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2010-3 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2012-2 | PRODUCED FLUID | 55.0 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR HYDRAULIC FRACTURING | |||
2012-1 | PRODUCED FLUID | 4910.0 | Bbl | REUSE OTHER THAN ROAD SPREADING | REUSE FOR HYDRAULIC FRACTURING |