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37-019-00660

Well Details

Well ID: 37-019-00660
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Country: United States
State: Pennsylvania
County: Butler
Municipality: Winfield Township
Operator Name: REDMILL DRILLING
Well Pad ID:
Farm/Lease Name: ELIZABETH HOAK ET AL 10301
License Status: ACTIVE
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.777590
Longitude: -79.703460

For data sources see[1][2][3]

Well History

Date Event
1901-01-01 Drilling Completion
1987-01-01 OLD WELL

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1990 DAMSON OIL CORP 1424.00 365 0.00 0 0.00 0
1991 PARKER & PARSLEY DEV LP 1370.00 364 0.00 0 0.00 0
1992 PARKER & PARSLEY DEV LP 1363.00 368 0.00 0 0.00 0
1993 PARKER & PARSLEY DEV LP 1349.00 364 0.00 0 0.00 0
1994 PARKER & PARSLEY DEV LP 1186.00 344 0.00 0 0.00 0
1995 RANGE OPR CO 562.00 153 0.00 0 0.00 0
1996 RANGE OPR CO 1219 365 0.00 0 0.00 0
1999 BLX INC 884 365 0.00 0 0.00 0
2000 BLX INC 497 305 0.00 0 0.00 0
2001 BLX INC 741 335 0.00 0 0.00 0
2002 BLX INC 856.17 333 0.00 0 0.00 0
2003 BLX INC 710.73 334 0.00 0 0.00 0
2004 BLX INC 432.71 339 0.00 0 0.00 0
2005 BLX INC 770.63 333 0.00 0 0.00 0
2006 BLX INC 697.00 362 0.00 0 0.00 0
2007 BLX INC 556.00 365 0.00 0 0.00 0
2008 BLX INC 560.00 343 0.00 0 0.00 0
2010 BLX INC 265.33 152 0.00 0 0.00 0
2011 BLX INC 125.49 188 0.00 0 0.00 0
2012 BLX INC 4.5 61 0.00 0 0.00 0
2013 REDMILL DRILLING 8.62 38 0.00 0 0.00 0
2014 REDMILL DRILLING 18.09 119 0.00 0 0.00 0
2015 REDMILL DRILLING 172.48 183 0.00 0 0.00 0
2016 REDMILL DRILLING 267.61 335 0.00 0 0.00 0
2017 REDMILL DRILLING 631.66 365 0.00 0 0.00 0
2018 REDMILL DRILLING 683.04 365 0.00 0 0.00 0
2019 SME WELL SVC INC 710.85 365 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2727656 Primary Facility 2018-05-02 Routine/Partial Inspection No Violations Noted At the time of inspection, well was producing. Well integrity appeared to be in good condition, with no signs of any leaks. There was some superficial corrosion in the form of rust on the 4 7/8" casing. The outer 7" had moderate corrosion near ground level. The well was properly labeled. There was a small meter hooked up at the well. Production was reported for 2017 as 631 mcf for 365 days.

For data sources see[6]

References