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__NOEDITSECTION__ | __NOEDITSECTION__ | ||
+ | [[Category:Wells]] |
Well ID: 37-021-21127 | Loading map...
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Operator Name: AMER NATURAL RESOURCES LLC | |
First Permit Date: 2009-03-12 | |
Last Permit Date: 2009-03-12 | |
Spud Date: 2009-03-24 | |
Unconventional: No | |
Horizontal: No | |
Violations: 3 | |
Latitude: 40.614654 | |
Longitude: -78.732337 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2013-0 | 5787.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2012-0 | 5242.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-0 | 15114.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2010-0 | 18813.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2010-0 | PRODUCED FLUID | 193.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 | PA BRINE TRT INC - JOSEPHINE PLT, INDIANA COUNTY | JOSEPHINE | PA |
2011-0 | PRODUCED FLUID | 230.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 | PA BRINE TRT INC - JOSEPHINE PLT, INDIANA COUNTY | JOSEPHINE | PA |
2013-0 | PRODUCED FLUID | 20.0 | Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 | FLUID RECOVERY SERVICE JOSEPHINE FACILITY | JOSEPHINE | PA |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
1846470 | 2009-11-18 | No Violations Noted | At the time of inspection, the well was in production. Drilling was completed on 03/30/2009. Well site was properly signed with E&S plan, but well tag was illegible and it is recommended it be replaced. Brine tank appeared sound. Well site was adequately and uniformly restored. Since adequate vegetative cover had been established it is recommended that the filter fabric fence be removed. No accelerated erosion or sedimentation issues were observed with well site. Access road was in stable condition, but noted that culvert pipes should be maintained to remove debris. | |
1949597 | 2011-02-14 | Violation(s) Noted | Well Tag was not present. At the time of inspection, no E&S issue. Steel line from Separator to Brine contained a hole causing brine water to discharge to ground. Brine water was leaking from discharge point and snow covered ground was stained with light brown brine water. Well head consisted of 8¿x4¿x 2¿ production line. Production equipment of separator (50 psi), heater and data logger (50/25 psi) and 50 bbl brine tank (50 bbl fluid). DEP called ANR and left message about the discharge | 604763 |
1949597 | 2011-02-14 | Violation(s) Noted | Well Tag was not present. At the time of inspection, no E&S issue. Steel line from Separator to Brine contained a hole causing brine water to discharge to ground. Brine water was leaking from discharge point and snow covered ground was stained with light brown brine water. Well head consisted of 8¿x4¿x 2¿ production line. Production equipment of separator (50 psi), heater and data logger (50/25 psi) and 50 bbl brine tank (50 bbl fluid). DEP called ANR and left message about the discharge | 604764 |
1949597 | 2011-02-14 | Violation(s) Noted | Well Tag was not present. At the time of inspection, no E&S issue. Steel line from Separator to Brine contained a hole causing brine water to discharge to ground. Brine water was leaking from discharge point and snow covered ground was stained with light brown brine water. Well head consisted of 8¿x4¿x 2¿ production line. Production equipment of separator (50 psi), heater and data logger (50/25 psi) and 50 bbl brine tank (50 bbl fluid). DEP called ANR and left message about the discharge | 604765 |
1953489 | 2011-02-25 | No Violations Noted | Well Tag was present. At the time of inspection, no E&S issue. Steel line from Separator to Brine was repaired and no discharge to ground. Brine water was not leaking. Well head consisted of 8¿x4¿x 2¿ production line. Production equipment of separator (50 psi), heater and data logger (50/25 psi) and 50 bbl brine tank (20 bbl fluid). | |
2032523 | 2012-01-05 | No Violations Noted | Well Tag was present. At the time of inspection, no E&S concerns were present. The gas well was in production. |