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34-007-20869

Well Details

Well ID: 34-007-20869
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Country: United States
State: Ohio
County: Ashtabula
Municipality: Richmond Township
Operator Name: STK INVESTMENTS LLC
Well Pad ID:
Farm/Lease Name: BROWN R & M
License Status: Plugged and Abandoned
License Date: 2017-05-08
Spud Date: 1978-06-02
Spud Drilling Contractor: PEP DRLG
Final Drill Date: 1978-06-10
Well Total Depth: 3880.00 ft
Configuration: Vertical
Latitude: 41.680000
Longitude: -80.560000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1978-03-22 3747 UNICORN OIL & GAS CO INC GeoDate 3/22/78
Oil and Gas 1978-03-22 Issued Date 3/22/78 Expired Date Acres 0055530 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
Original Spud 1978-06-02 R.I. 3-29-78
Completed 1978-06-10 R.I. 3-29-78
Reached Total Depth 1978-06-10 R.I. 3-29-78
Completion Report Received 1978-11-21 R.I. 3-29-78
CO 1994-07-26 28 CGAS EXPLORATION,INC GeoDate 3/22/78
Change of Owner 1999-07-09 Operator changed from 28, CGAS EXPLORATION to 3954, WILKES ENERGY INC
Change of Owner 2001-10-10 Operator changed from 3954, WILKES ENERGY INC to 6805, GAS ACQUISITION COMPANY LTD
APP 2003-04-10 Proposed Formations:CLINTON, Issued Date:4/10/2003, Expired Date:4/9/2004 6:00:00 AM, Drilling unit acres:55.53, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2011-11-22 Operator changed from 6805, GAS ACQUISITION COMPANY LTD to 8863, STK INVESTMENTS LLC
APP 2017-05-08 Proposed Formations:CLINTON SAND, Issued Date:5/8/2017, Expired Date:5/8/2019 12:00:00 PM, Drilling unit acres:55.53, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2017-05-19 R.I. 3-29-78
Record Last Modified 2017-10-20 R.I. 3-29-78
Construction Permit Expires 2019-05-08 R.I. 3-29-78

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3692 3729 17
3692 3729 17
3692 3729 17

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 26986 Gal 139788

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 EP OPERATING CO 684.00 89.00 0
1986 EP OPERATING CO 1270.00 162.00 365
1987 EP OPERATING CO 540.00 77.00 365
1994 CGAS EXPLORATION 0.00 0.00 365
1995 CGAS EXPLORATION 8.00 48.00 365
1996 CGAS EXPLORATION 2.00 0.00 365
1997 CGAS EXPLORATION 8.00 0.00 365
1998 CGAS EXPLORATION 26.00 0.00 365
1999 CGAS EXPLORATION 6.00 0.00 365
2009 GAS ACQUISITION COMPANY LTD 0.00 0.00 0
2012 STK INVESTMENTS LLC 0.00 0.00 0
2014 STK INVESTMENTS LLC 0.00 0.00 0
2015 STK INVESTMENTS LLC 0.00 0.00 0
2017 STK INVESTMENTS LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 EP OPERATING CO Brine 219 0
1986 EP OPERATING CO Brine 208 365
1987 EP OPERATING CO Brine 115 365
1994 CGAS EXPLORATION Brine 0 365
1995 CGAS EXPLORATION Brine 54 365
1996 CGAS EXPLORATION Brine 0 365
1997 CGAS EXPLORATION Brine 0 365
1998 CGAS EXPLORATION Brine 0 365
1999 CGAS EXPLORATION Brine 0 365
2009 GAS ACQUISITION COMPANY LTD Brine 0 0
2012 STK INVESTMENTS LLC Brine 0 0
2014 STK INVESTMENTS LLC Brine 0 0
2015 STK INVESTMENTS LLC Brine 0 0
2017 STK INVESTMENTS LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1117009800 2016-3-11 0:00: PW No Violations
-1710893990 2017-6-9 0:00:0 FR No Violations
-1965354054 2016-2-5 0:00:0 PW No Violations
-248043718 2014-7-1 0:00:0 PW No Violations
-281121530 2014-4-1 0:00:0 PW No Violations
-754956017 2017-9-18 0:00: FR No Violations
-949187057 2014-5-2 0:00:0 PW No Violations
-956624831 2017-5-31 0:00: FR No Violations
0101928091 2017-05-25 Final Restoration No Violations I arrived on site to find no activity at this time. The flow line has been removed.
0146510771 2016-12-06 Production Wells No Violations My inspection of this well found there still has been no action from the company to plug this well.
0248043718 2014-07-01 Production Wells No Violations Complaint # 4650. My inspection found there is no evidence the company has even attempted to comply with the compliance notice issued on 4-1-2014 and is due on 9-1-2014. I contacted Kirk Sherrill and left a message for him to contact me and update the status of plugging this well.
0281121530 2014-04-01 Production Wells Violations Noted I checked this well in response to a public complaint# 4650 from Margery Brown [ landowner ] claiming the well is idle and should be removed . My inspection found there is one 210 barrel steel tank and one separator at the tank battery location . The area inside the earthen impoundment wall around the tank and the separator is overgrown with small trees and brush . There is not a identification sign posted for this well at the tank battery or the well locations . Further inspection of the well head I found 4.5 casing with a swage to 2 with a valve which is closed . The well is not connected to the flow line . The RBDMS records showed the last reported production for this well was in 1999 and was only 6 million cubic feet of gas . This well is idle . REQUIRED REMEDIAL ACTION : PLUG WELL . I contacted the company and I spoke with Kirk Sherrill and told him of the compliance violations and that the well has to be plugged . He did not have a date for when they would plug the well .
0367002131 2017-04-06 Production Wells No Violations My inspection found there has been no action to plug this well.
0674057437 2005-06-09 Production Wells No Violations no violations .
0754956017 2017-09-18 Final Restoration No Violations My inspection of the Brown # 1 for final restoration revealed that the two (2) inch riser pipe had not been removed, the tank pad was still void of vegetation. I spoke with Matt Kleese, who said, that he will not work on a live line to remove the riser and does not know the lines owner or if there is a gate valve to isolate the riser and the material on the tank pad was placed there after the tank battery removal. He said, that he had that discussion with DOGRM personnel previously and wont proceed any further. The R & M Brown # 1 was not compliant with the Final Restoration rules.
0949187057 2014-05-02 Production Wells No Violations Complaint # 4650 . My inspection of this well found there has been no activity at this well to resolve the compliance violations . I called Kirk Sherrill and left a message with his service to contact me and update me of the status of plugging this well .
0956624831 2017-05-31 Final Restoration No Violations I arrived on site to find the production tank has been removed. The separator was placed on the east side of the lease road. There was a trailer with a string of tubing on it and a half tank in the entrance to the well.
0991051978 2015-03-04 Production Wells No Violations Complaint# 4650 follow-up. There has been no action from the company to plug this well.
101928091 2017-5-25 0:00: FR No Violations
1050049159 2017-05-24 Final Restoration No Violations My inspection found the company was in the process in removing the flow line.
1073478895 2016-09-20 Production Wells No Violations My inspection of this well found there has been no action from the company to plug this well.
1117009800 2016-03-11 Production Wells No Violations My inspection of this well found there has been no action from the company to plug this well.
1284316319 2017-05-17 Plug / Plug Back No Violations I was on site to witness the service rig go into the production casing with a drill bit on the tubing to attempt to drill through an obstruction in the well. They hit a obstruction at 2780 feet. They dry drilled on the obstruction for several minutes when they were able to drill through the obstruction. They run to bottom with the tubing. I left the site when they began pulling the tubing from the well.
1423084298 2014-08-20 Production Wells No Violations In response to a phone call from Margery Brown to Regional Supervisor Tom Hill, Inspectors Jerry Kohl, Josh Schiering and I met with Mrs. Brown regarding follow-up to Complaint #4650. Mrs. Brown voiced several concerns. She questioned why the idle well on her property was not yet plugged. We explained that there was an existing Notice of Violation (NOV) for the well requiring it to be plugged with a Required Action Date of 09/01/2014. We explained that if no action has taken place by that date, we would proceed with further legal processes following state law. Another concern was that she believed that unknown people were conducting oilfield activities on her property during the night, such as drilling new wells. She had heard noises and seen lights and people in or near the wooded area east of her home. We explained that no permitted drilling activities were taking place in Ashtabula County at the time of our meeting. We offered to do a visual survey of potential access points to her property to see if there were any fresh traffic patterns from the main roads onto her property. We also advised that if there were non-oilfield activities taking place on her property without her permission, she would need to contact a local law enforcement agency. Mrs. Brown also suggested that someone was taking gas from the idle well on her property. We told her we would re--south along the west side of her property. We also looked along Footville-Richmond Road, which is oriented east west along the south end of her property. There we
1423496884 2015-02-05 Production Wells No Violations Complaint# 4650 follow-up. My inspection found there has been no action by the company to plug this well. Since the issuance of the compliance notice on 4-1-2014 several attempts to contact the company has resulted in no response from the company.
146510771 2016-12-6 0:00: PW No Violations
1593562453 2015-05-01 Production Wells No Violations Follow-up, Complaint# 4650, Marjorie Brown. I checked this well in response to a phone call from Marjorie Brown, she claimed some one had changed the chart on a gas meter by the tank battery area. My inspection found a chart had been changed on a meter run near entrance to the tank battery. The meter run is owned by Phil Dietrich. Phil has no connection to the well on Marjories property. The well showed no activity to plug the well.
1710893990 2017-06-09 Final Restoration No Violations I arrived on site to find the separator, tank ladder, heater tube stack were still at the tank battery area. The tank battery had not been final graded. There were three two inch pipes coming from below the surface where the separator had been located. I called Jay with J-Well, he told me they will complete the final restoration at the first of the next week.
1965354054 2016-02-05 Production Wells No Violations My inspection of this well found there has been no action from the company to plug this well. Attempts to contact the company have had no responce from the company.
2069122144 2017-08-28 Final Restoration No Violations My inspection found that the Brown # 1 plugged and abandoned well was not in compliance with the final restoration rules. Per Tom Hill the flow line was previously removed. I found a meter box, two (2) inch pipe riser north of the old tank pad and one (1) inch orange plastic piping partially buried in the access road. The tank pad was void of vegetation. The Brown # 1 was not approved for final restoration.
2111695170 2017-05-23 Final Restoration No Violations I arrived on site to find the company in the process in reclaiming the wellsite.
367002131 2017-4-6 0:00:0 PW No Violations
467767239 2019-5-7 0:00:0 FR No Violations
674057437 2005-6-9 0:00:0 PW No Violations
991051978 2015-3-4 0:00:0 PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0281121530 US-OH-122920 2014-05-13 Well shall be plugged

For data sources see[9]

References