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Well ID: 34-029-20657 | Loading map...
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Country: United States | |
State: Ohio | |
County: Columbiana | |
Municipality: Knox Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: FRESHLEY ROBT R & PATRICIA | |
License Status: Producing | |
License Date: 1970-11-05 | |
Spud Date: 1970-12-15 | |
Spud Drilling Contractor: | |
Final Drill Date: 1970-12-30 | |
Well Total Depth: 5420.00 ft | |
Configuration: Vertical | |
Latitude: 40.860000 | |
Longitude: -81.080000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1970-11-05 | 9 EDC GeoDate 11/5/70 |
Original Spud | 1970-12-15 | GL=1220.4 |
Completed | 1970-12-30 | GL=1220.4 |
Reached Total Depth | 1970-12-30 | GL=1220.4 |
Change of Owner | 2008-07-21 | Operator changed from 9, POWER GAS MARKETING & TRANS to 1388, EXCO - NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
Record Last Modified | 2019-06-04 | GL=1220.4 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5268 | 5306 | 0 |
5268 | 5306 | 0 | |
5268 | 5306 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1200 Bbl | 50000 | R,P. 48 HRS. | ||
GEL | 0 | 1000 Gal | 0 | |||
ACID | 0 | 500 Gal | 0 | N.F. |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
1490726616 | 2017-03-16 | Production Wells | No Violations | The purpose of my inspection was to conduct a status check on well #2-0657. A review of RBDMS indicates the last reported production by the Owner was 2005. Lease access to the well and tank battery was through a residential driveway. The well location was in an agricultural field that was stable. Snow covered the location at the time of location. The 8.625 well head was below grade. The 4.5 production casing was equipped with a plunger lift assembly. Production valves were in the closed position. No audible or visual leaks were identified. A domestic supply connection was present. Identification was posted on the production tank. No earthen dike was present around the separator or production tank. No audible or visual leaks were identified on the separator. The meter house did not contain a current production chart. The 100 bbl production chart remained in good repair with no leaks or holes observed on the body. The identification sign contained correct and legible information. The load line and drain line valves were closed and plugged. The hatch lid was closed. No violations were observed during this inspection. |
For data sources see[9]