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34-055-20150

Well Details

Well ID: 34-055-20150
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Country: United States
State: Ohio
County: Geauga
Municipality: Parkman Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: ZAYLOR E & S
License Status: Final Restoration
License Date: 2013-10-11
Spud Date: 1975-11-17
Spud Drilling Contractor:
Final Drill Date: 1977-09-08
Well Total Depth: 4240.00 ft
Configuration: Vertical
Latitude: 41.380000
Longitude: -81.040000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1975-11-17 REV. LOC. 2-5-75, RE-IS. 7-16-75
Completed 1977-09-08 REV. LOC. 2-5-75, RE-IS. 7-16-75
Reached Total Depth 1977-09-08 REV. LOC. 2-5-75, RE-IS. 7-16-75
CO 1982-07-22 9 EDC GeoDate 7/22/82
Change of Owner 2008-07-21 Operator changed from 9, POWER GAS MARKETING & TRANS to 1388, EXCO - NORTH COAST ENERGY INC
Change of Owner 2009-12-14 Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC
APP 2013-10-11 Proposed Formations:CLINTON, Issued Date:10/11/2013, Expired Date:10/11/2015 12:00:00 PM, Drilling unit acres:146, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2014-09-10 REV. LOC. 2-5-75, RE-IS. 7-16-75
Construction Permit Expires 2015-10-11 REV. LOC. 2-5-75, RE-IS. 7-16-75
Record Last Modified 2017-02-10 REV. LOC. 2-5-75, RE-IS. 7-16-75

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4110 4196 21
4110 4196 21
4110 4196 21

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
Not Treated 0 1250 Bbl 47200

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 POWER GAS MARKETING & TRANS 3470.00 143.00 0
1985 POWER GAS MARKETING & TRANS 3292.00 130.00 365
1986 POWER GAS MARKETING & TRANS 1260.00 103.00 365
1987 POWER GAS MARKETING & TRANS 995.00 65.00 365
1988 POWER GAS MARKETING & TRANS 919.00 123.00 365
1989 POWER GAS MARKETING & TRANS 672.00 0.00 365
1990 POWER GAS MARKETING & TRANS 766.00 64.00 365
1991 POWER GAS MARKETING & TRANS 228.00 69.00 365
1992 POWER GAS MARKETING & TRANS 1527.00 0.00 365
1993 POWER GAS MARKETING & TRANS 1126.00 102.00 365
1994 POWER GAS MARKETING & TRANS 773.00 57.00 0
1995 POWER GAS MARKETING & TRANS 1437.00 80.00 0
1996 POWER GAS MARKETING & TRANS 1343.00 140.00 0
1997 POWER GAS MARKETING & TRANS 1459.00 62.00 365
1998 POWER GAS MARKETING & TRANS 1787.00 52.00 365
1999 POWER GAS MARKETING & TRANS 1307.00 118.00 365
2000 POWER GAS MARKETING & TRANS 1321.00 58.00 365
2001 POWER GAS MARKETING & TRANS 21.00 0.00 365
2002 POWER GAS MARKETING & TRANS 470.00 0.00 365
2003 POWER GAS MARKETING & TRANS 866.00 58.00 365
2004 POWER GAS MARKETING & TRANS 1394.00 58.00 365
2005 POWER GAS MARKETING & TRANS 1230.00 43.00 365
2006 EXCO - NORTH COAST ENERGY INC 1103.00 85.00 365
2007 EXCO - NORTH COAST ENERGY INC 1113.00 69.00 365
2008 EXCO - NORTH COAST ENERGY INC 862.00 55.00 366
2009 EXCO - NORTH COAST ENERGY INC 9.00 0.00 365
2010 ENERVEST OPERATING LLC 0.00 0.00 0
2011 ENERVEST OPERATING LLC 0.00 0.00 0
2012 ENERVEST OPERATING LLC 0.00 0.00 0
2013 ENERVEST OPERATING LLC 0.00 0.00 365
2014 ENERVEST OPERATING LLC 0.00 0.00 0
2015 ENERVEST OPERATING LLC 0.00 0.00 294

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 POWER GAS MARKETING & TRANS Brine 102 0
1985 POWER GAS MARKETING & TRANS Brine 85 365
1986 POWER GAS MARKETING & TRANS Brine 43 365
1987 POWER GAS MARKETING & TRANS Brine 42 365
1988 POWER GAS MARKETING & TRANS Brine 42 365
1989 POWER GAS MARKETING & TRANS Brine 19 365
1990 POWER GAS MARKETING & TRANS Brine 27 365
1991 POWER GAS MARKETING & TRANS Brine 1 365
1992 POWER GAS MARKETING & TRANS Brine 119 365
1993 POWER GAS MARKETING & TRANS Brine 81 365
1994 POWER GAS MARKETING & TRANS Brine 52 0
1995 POWER GAS MARKETING & TRANS Brine 79 0
1996 POWER GAS MARKETING & TRANS Brine 73 0
1997 POWER GAS MARKETING & TRANS Brine 0 365
1998 POWER GAS MARKETING & TRANS Brine 48 365
1999 POWER GAS MARKETING & TRANS Brine 0 365
2000 POWER GAS MARKETING & TRANS Brine 23 365
2001 POWER GAS MARKETING & TRANS Brine 25 365
2002 POWER GAS MARKETING & TRANS Brine 0 365
2003 POWER GAS MARKETING & TRANS Brine 0 365
2004 POWER GAS MARKETING & TRANS Brine 25 365
2005 POWER GAS MARKETING & TRANS Brine 0 365
2006 EXCO - NORTH COAST ENERGY INC Brine 0 365
2007 EXCO - NORTH COAST ENERGY INC Brine 150 365
2008 EXCO - NORTH COAST ENERGY INC Brine 50 366
2009 EXCO - NORTH COAST ENERGY INC Brine 0 365
2010 ENERVEST OPERATING LLC Brine 0 0
2011 ENERVEST OPERATING LLC Brine 0
2012 ENERVEST OPERATING LLC Brine 0 0
2013 ENERVEST OPERATING LLC Brine 0 365
2014 ENERVEST OPERATING LLC Brine 0 0
2015 ENERVEST OPERATING LLC Brine 0 294

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1068559653 2013-9-9 0:00:0 PW No Violations
-1195911313 2014-9-10 0:00: PB No Violations
-1765262019 2014-8-14 0:00: PW No Violations
-1916980025 2013-4-4 0:00:0 PW No Violations
0399559545 2014-10-08 Final Restoration No Violations My inspection found the location has been graded and vegetation is established. Final restoration can be passed when a flow line waiver is submitted.
1068559653 2013-09-09 Production Wells Violations Noted My inspection found the well to be equipped with a plunger lift unit. The tank battery consists of a 100 BBL production tank and a mechanical separator. The dike does not meet requirements and there was no identification sign on location. The production records show no production since 2009. The lease road is in stable condition. The well must be produced within 30 days or plugged within 90 days of this notice.
1195911313 2014-09-10 Plug / Plug Back No Violations I was on location for the plugging of this oil and gas well. Kleese Development & Assoc. was the plugging contractor on location for Enervest. Petroset was the cement contractor on location. KDA removed the 1.5 tubing from the well. Petroset rigged up and bull headed the bottom plug with 15 sacks of Class A cement. The plug was displaced and pressured up to 400 psi and shut in for 1 hour. Appalacian Well Survey shot the 2 7/8 casing off at 2700. KDA pulled 1 joint of 2 7/8 casing to 2670. Petroset rigged up and set 75 sacks of Class A cement to cover the big lime. When KDA pulled 12 joints of 2 7/8 casing the well began to unload itself. I had Petroset circulate on the well with heavy brine to remove any pockets of gas left in the formations. The company circulated and stopped to observe the well multiple times until it was decided the well no longer had any gas pressure on it. KDA had Petroset rig up and set another plug at 2300 to 2100, with 57 sacks of Class A cement. KDA pulled 62 joints of the 2 7/8 casing to 464. Petroset rigged up and pumped 60 sacks of Class A cement to cover the bottom of the surface casing. KDA pulled 9 joints of 2 7/8 casing to 200. Petroset rigged up and pumped 60 sacks of Class A cement to the surface. The remaining 5 joints of 2 7/8 casing was removed from the well. The hole was then topped off with cement. A total of 77 joints of 2 7/8 casing was removed from the well. GPS Coordinates are +/-8.
1391195230 2014-01-27 Production Wells Violations Noted This inspection is a follow up to compliance notice inspection # 1068559653. My inspection found the well to be equipped with a plunger lift unit. The tank battery consists of a 100 BBL production tank and a mechanical separator. The dike does not meet requirements and there was no identification sign on location. The production records show no production since 2009. The lease road is in stable condition. I will contact the company about the identification sign and the dike must be rebuilt if the well gets put back into production. The company has been issued a plugging permit for the well. I have contacted the company and the well is scheduled to be plugged.
1765262019 2014-08-14 Production Wells No Violations My inspection found no changes since my last inspection. The company has the well scheduled to be plugged this year.
1916980025 2013-04-04 Production Wells No Violations My inspection found the well to be equipped with a plunger lift unit. The tank battery consists of a 100 BBL production tank and a mechanical separator. The tank battery is in need of a dike and there was not a identification sign. The production records show no production since 2009. I contacted a supervisor from Enervest, Mr McDaniels, who stated he was going to find out more about the well and contact me later in the week. The lease road is in stable condition.
1927175372 2015-10-06 Final Restoration No Violations My inspection found the location has been graded and vegetation is established on the location. The landowner waiver has been submitted for the flow line. Final restoration can be passed.
399559545 2014-10-8 0:00: FR No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1068559653 US-OH-101416 2014-11-06 Well shall be plugged
1391195230 US-OH-111562 2016-07-26 NONE Well shall be plugged

For data sources see[9]

References