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34-059-22461

Well Details

Well ID: 34-059-22461
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Country: United States
State: Ohio
County: Guernsey
Municipality: Richland Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: GREEN
License Status: Final Restoration
License Date: 2017-03-14
Spud Date: 1979-01-02
Spud Drilling Contractor:
Final Drill Date: 1979-01-09
Well Total Depth: 5644.00 ft
Configuration: Vertical
Latitude: 39.900000
Longitude: -81.490000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1978-09-14 2143 CARLESS RESOURCES INC GeoDate 9/14/78
Original Spud 1979-01-02 UPDATE LOCATION PER SURVEYOR COORDS 07/05/2017 ALE.
Completed 1979-01-09 UPDATE LOCATION PER SURVEYOR COORDS 07/05/2017 ALE.
Reached Total Depth 1979-01-09 UPDATE LOCATION PER SURVEYOR COORDS 07/05/2017 ALE.
Change of Owner 1998-06-15 Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC
Change of Owner 2009-12-14 Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC
APP 2017-03-14 Proposed Formations:CLINTON SAND, Issued Date:3/14/2017, Expired Date:3/14/2019 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2017-06-05 UPDATE LOCATION PER SURVEYOR COORDS 07/05/2017 ALE.
Record Last Modified 2017-12-08 UPDATE LOCATION PER SURVEYOR COORDS 07/05/2017 ALE.
Construction Permit Expires 2019-03-14 UPDATE LOCATION PER SURVEYOR COORDS 07/05/2017 ALE.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5442 5497 9
5442 5497 9
5442 5497 9

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1454 Bbl 55000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1986 ZILKHA ENERGY INC 4983.00 210.00 364
1987 ZILKHA ENERGY INC 4627.00 178.00 365
1988 CARLESS RESOURCES INC 3563.00 0.00 365
1989 CARLESS RESOURCES INC 2327.00 79.00 365
1990 CARLESS RESOURCES INC 3254.00 87.00 365
1991 CARLESS RESOURCES INC 3045.00 203.00 365
1992 CARLESS RESOURCES INC 2004.00 0.00 365
1993 CARLESS RESOURCES INC 1733.00 0.00 365
1994 CARLESS RESOURCES INC 1414.00 100.00 365
1995 CARLESS RESOURCES INC 2690.00 94.00 365
1996 CARLESS RESOURCES INC 2780.00 99.00 365
1997 CARLESS RESOURCES INC 2161.00 72.00 365
1998 EXCO - NORTH COAST ENERGY INC 1404.00 0.00 365
1999 EXCO - NORTH COAST ENERGY INC 1377.00 0.00 365
2000 EXCO - NORTH COAST ENERGY INC 1411.00 55.00 365
2001 EXCO - NORTH COAST ENERGY INC 1264.00 0.00 365
2002 EXCO - NORTH COAST ENERGY INC 631.00 0.00 365
2003 EXCO - NORTH COAST ENERGY INC 817.00 0.00 365
2004 EXCO - NORTH COAST ENERGY INC 1.00 41.00 365
2005 EXCO - NORTH COAST ENERGY INC 0.00 0.00 365
2006 EXCO - NORTH COAST ENERGY INC 0.00 0.00 365
2007 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2008 EXCO - NORTH COAST ENERGY INC 0.00 0.00 366
2009 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2010 ENERVEST OPERATING LLC 74.00 0.00 365
2011 ENERVEST OPERATING LLC 0.00 0.00 0
2012 ENERVEST OPERATING LLC 0.00 0.00 366
2013 ENERVEST OPERATING LLC 0.00 0.00 365
2014 ENERVEST OPERATING LLC 0.00 0.00 365
2015 ENERVEST OPERATING LLC 0.00 0.00 365
2016 ENERVEST OPERATING LLC 0.00 0.00 0
2017 ENERVEST OPERATING LLC 0.00 0.00 1

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1986 ZILKHA ENERGY INC Brine 195 364
1987 ZILKHA ENERGY INC Brine 186 365
1988 CARLESS RESOURCES INC Brine 110 365
1989 CARLESS RESOURCES INC Brine 40 365
1990 CARLESS RESOURCES INC Brine 141 365
1991 CARLESS RESOURCES INC Brine 82 365
1992 CARLESS RESOURCES INC Brine 0 365
1993 CARLESS RESOURCES INC Brine 0 365
1994 CARLESS RESOURCES INC Brine 31 365
1995 CARLESS RESOURCES INC Brine 117 365
1996 CARLESS RESOURCES INC Brine 134 365
1997 CARLESS RESOURCES INC Brine 56 365
1998 EXCO - NORTH COAST ENERGY INC Brine 0 365
1999 EXCO - NORTH COAST ENERGY INC Brine 14 365
2000 EXCO - NORTH COAST ENERGY INC Brine 2 365
2001 EXCO - NORTH COAST ENERGY INC Brine 0 365
2002 EXCO - NORTH COAST ENERGY INC Brine 0 365
2003 EXCO - NORTH COAST ENERGY INC Brine 0 365
2004 EXCO - NORTH COAST ENERGY INC Brine 40 365
2005 EXCO - NORTH COAST ENERGY INC Brine 0 365
2006 EXCO - NORTH COAST ENERGY INC Brine 0 365
2007 EXCO - NORTH COAST ENERGY INC Brine 0 0
2008 EXCO - NORTH COAST ENERGY INC Brine 0 366
2009 EXCO - NORTH COAST ENERGY INC Brine 0 0
2010 ENERVEST OPERATING LLC Brine 0 365
2011 ENERVEST OPERATING LLC Brine 0
2012 ENERVEST OPERATING LLC Brine 0 366
2013 ENERVEST OPERATING LLC Brine 0 365
2014 ENERVEST OPERATING LLC Brine 0 365
2015 ENERVEST OPERATING LLC Brine 0 365
2016 ENERVEST OPERATING LLC Brine 0 0
2017 ENERVEST OPERATING LLC Brine 41 1

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1029503420 2004-8-30 0:00: PW No Violations
-1095540569 2017-10-6 0:00: PB No Violations 0.80
-1444006630 2017-5-30 0:00: PW No Violations 1.00
-1974091064 2005-2-10 0:00: PW No Violations
-2007600630 2017-9-7 0:00:0 PB No Violations 1.00
-2121909031 2007-10-9 0:00: PW No Violations
-807397200 2017-6-1 0:00:0 PB No Violations 5.00
0794958353 2017-12-01 Final Restoration No Violations On the day of my inspection I witnessed that the site passed final restoration according to ORC 1509.072B.
0807397200 2017-06-01 Plug / Plug Back No Violations On the day of my inspection I witnessed Chipco LLC trip inside the 4.5 inch diameter casing their 4 inch tools and sat down at 3090 feet. Chipco then tripped inside the 4.5 inch diameter casing with an impression block and found that the casing is parted at 3090 feet. Chipco tripped out the wellbore and tripped back in with their 1.5 inch diameter tools sat down and then successfully made it 200 feet past the part. Discussion was held with Enervest Superintendent Tim McConaha and a decision was made to call out Appalachian well surveys (AWS). Chipco tripped back inside the 4.5 inch diameter casing and reached 5400 feet. AWS arrived and tripped inside the 4.5 inch diameter casing to the depth of 3969 feet and successfully perforated the casing with 10 shots from 3969 feet to 3959 feet. Chipco will trip 1.5 inch diameter tubing in to total depth and commence plugging tomorrow with the bottom hole plug and the Big Lime plug.
1029503420 2004-08-30 Production Wells No Violations STATUS CHECK, ID RE-POSTED.
1053887113 2008-06-18 Production Wells No Violations HOUSE GAS TO LANDOWNER ESTORED.
1080226225 2008-01-02 Production Wells No Violations PRODUCING WELL.
1087119254 2008-04-28 Production Wells No Violations TANK AREA RE-WORKED.
1095540569 2017-10-06 Plug / Plug Back No Violations On the day of my inspection I witnessed reclamation is completed with exception to the access road and still awaiting land owner waiver.
1270221906 2010-04-01 Production Wells No Violations Inspection revealed that well is shut in at present time, will call local pumper and inquire about status of well, it is equipped with 8 surface casing and 4.5 production casing(jet star system) and 1-210 bbl tank and separator there is no chart in meter box! According to well tender hole loaded up with water and they will access getting service rig to swab well.
1444006630 2017-05-30 Production Wells No Violations On the day of my inspection I met with Chip Smith of Chipco LLC and witnessed the well was equipped with 8.625 inch diameter casing, 4.5 inch diameter casing and a casing lift system with all valves in the closed position. The production equipment included a 210 barrel tank, a horizontal separator, 2 drips, a 2 inch salesmeter with a chart recorder and domestic gas service with valves closed to the domestic gas. Identification was present and production records were current with zero production reported since 2011. Chipco will be moving on to commence plugging operations possibly tomorrow.
1496655678 2017-06-05 Plug / Plug Back No Violations
1830710288 2017-01-18 Production Wells No Violations On the day of my inspection I witnessed the well was equipped with 8.625 inch diameter casing, 4.5 inch diameter casing and a casing lift system with all valves in the closed position. The production equipment included a 210 barrel tank, a horizontal separator, 2 drips, a 2 inch salesmeter with a chart recorder and domestic gas service with valves closed to the domestic gas. Identification was present and production records were current with zero production reported since 2011. I contacted Enervest requesting their plans for the well.
1974091064 2005-02-10 Production Wells No Violations STATUS CHECK.
2007600630 2017-09-07 Plug / Plug Back No Violations On the day of my inspection I witnessed the production equipment has been removed and the dike has been reclaimed. The access road has been graded abut not restored. Call was placed to Enervest requesting information on the access road. Call was received from Enervest Superintendent Tim McConaha and he stated that the land owner is going to use the road for a driveway and he will get a signed waiver.
2121909031 2007-10-09 Production Wells No Violations STATUS CHECK
794958353 2017-12-1 0:00: FR No Violations 1.00

For data sources see[9]

References