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Well ID: 34-059-22679 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Center Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: LARRICK WALLACE | |
License Status: Final Restoration | |
License Date: 2013-04-22 | |
Spud Date: 1980-01-10 | |
Spud Drilling Contractor: | |
Final Drill Date: 1980-02-19 | |
Well Total Depth: 5345.00 ft | |
Configuration: Vertical | |
Latitude: 40.040000 | |
Longitude: -81.520000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1979-12-31 | 2143 CARLESS RESOURCES INC GeoDate 12/31/79 |
Original Spud | 1980-01-10 | |
Completed | 1980-02-19 | |
Reached Total Depth | 1980-02-19 | |
Change of Owner | 1998-06-15 | Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2013-04-22 | Proposed Formations:CLINTON, Issued Date:4/22/2013, Expired Date:4/22/2015 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2013-05-30 | |
Construction Permit Expires | 2015-04-22 | |
Record Last Modified | 2017-02-10 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5149 | 5238 | 1 |
5149 | 5238 | 1 | |
5149 | 5238 | 1 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 57190 Gal | 55000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1266549432 | 2016-5-2 0:00:0 | FR | No Violations | 1.00 |
-1596048627 | 2013-7-1 0:00:0 | FR | No Violations | 1.50 |
-1775296694 | 2004-4-13 0:00: | PW | No Violations | |
-185318718 | 2007-3-27 0:00: | PW | No Violations | |
0185318718 | 2007-03-27 | Production Wells | No Violations | WELL ON WORK OVER LIST. IF NOT FEASABLE TO PRODUCE WILL PLUG. |
0254687169 | 2007-03-27 | Production Wells | No Violations | WELL TO BE SWABBED. LOADED UP. POSSIBLE CANDIDATE TO PLUG. |
1042889077 | 2004-05-12 | Production Wells | Violations Noted | WELL APPEARS TO HAVE BEEN SHUT IN FOR SOME TIME. PRODUCTION RECORDS SHOW LAST PRODUCTION FILED 2002 |
1078105638 | 2013-10-24 | Plug / Plug Back | No Violations | This well is plugged. |
1266549432 | 2016-05-02 | Final Restoration | No Violations | On the day of my inspection following up on prior final restoration which passed on 10/24/13 the site met ORC 1509.072B. |
1363273404 | 2013-03-12 | Production Wells | Violations Noted | Pryor to my inspection I received a phone call from Mr. Denny Patterson requesting me to do a inspection on this well. My inspection at the well reveled eight inch casing with four inch production casing and two inch tubing with a ball valve that was closed standing from the ground, the pumping unit has been disconnected and pulled back away from the well. I reviewed the production records and found there has been no production recorded from the year of 1996/98/02/03/04/06/07/08/09/ and 2011, there is no I.D.posted at the well. The requirements to meet the divisions standards will be to make the well capable of commercial production within thirty days, or plugging is required within ninety days. Failure to comply may result in Forfeiture of Bond. |
1399420137 | 2003-07-21 | Production Wells | No Violations | STATUS CHECK |
1596048627 | 2013-07-01 | Final Restoration | No Violations | On the day of my inspection I witnessed that the pit was filled, seed and straw were in place. Tank battery had been restored seed and straw were in place. |
1775296694 | 2004-04-13 | Production Wells | No Violations | STATUS CHECK |
2104111421 | 2004-01-05 | Production Wells | No Violations | STATUS CHECK |
254687169 | 2007-3-27 0:00: | PW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1042889077 | US-OH-100647 | 2004-05-13 | Well shall be plugged | |
1363273404 | US-OH-110625 | 2014-04-10 | General Safety | |
1363273404 | US-OH-110626 | 2014-04-10 | Failure to legibly identify well | |
1363273404 | US-OH-110627 | 2014-04-10 | Nonproduction; well shall be plugged or placed in temporary inactive status |
For data sources see[9]