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Well ID: 34-059-22732 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Center Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: LARRICK W | |
License Status: Final Restoration | |
License Date: 2013-04-22 | |
Spud Date: 1980-06-21 | |
Spud Drilling Contractor: | |
Final Drill Date: 1980-07-17 | |
Well Total Depth: 5562.00 ft | |
Configuration: Vertical | |
Latitude: 40.040000 | |
Longitude: -81.520000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-06-18 | 2143 CARLESS RESOURCES INC GeoDate 6/18/80 |
Original Spud | 1980-06-21 | |
Completed | 1980-07-17 | |
Reached Total Depth | 1980-07-17 | |
Change of Owner | 1998-06-15 | Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2013-04-22 | Proposed Formations:CLINTON, Issued Date:4/22/2013, Expired Date:4/22/2015 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2013-05-20 | |
Construction Permit Expires | 2015-04-22 | |
Record Last Modified | 2017-02-10 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5361 | 5416 | 2 |
5361 | 5416 | 2 | |
5361 | 5416 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
GEL | 0 | 900 Bbl | 150000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1743284308 | 2004-1-5 0:00:0 | PW | No Violations | |
-2132642035 | 2013-3-12 0:00: | PW | No Violations | |
-279779405 | 2013-5-20 0:00: | PB | No Violations | |
-991162674 | 2013-5-16 0:00: | PB | No Violations | |
0279779405 | 2013-05-20 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed the rig crew for Chipco rip the 4.5 casing 3365 then pulled forty three joints and set a plug one hundred foot out and two hundred foot in the 8.625 casing, then pull thirty eight joints and set a two foot plug to surface. |
0991162674 | 2013-05-16 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Appalachian Wire Line perforate the Queenston at 5395 with ten shots, the pit and flow ditch was constructed and lined with ten mill plastic up to the well head. |
1084447684 | 2004-05-12 | Production Wells | Violations Noted | WELL APPEARS TO HAVE BEEN SHUT IN FOR SOME TIME.NO PRODUCTION REPORTS SINCE 2002. |
1285554036 | 2007-03-27 | Production Wells | No Violations | WELL ON PLUGGING LIST. NOT PRODUCING. |
1369313661 | 2013-05-23 | Final Restoration | No Violations | On the day of my inspection I found all the production equipment removed, the lease road restored, the pit was filled, seed and straw was in place. |
1743284308 | 2004-01-05 | Production Wells | No Violations | STATUS CHECK |
1780123823 | 2013-10-24 | Plug / Plug Back | No Violations | This well is plugged. |
2132642035 | 2013-03-12 | Production Wells | Violations Noted | Pryor to my inspection I received a phone call from Mr. Denny Patterson requesting me to do a inspection on this well. My inspection at the well reveled four inch production casing with a ball valve that was closed, I reviewed the Divisions production records and found they are not current from the year of 1996/ 98/02/03/04/05/06/07/08/09/2010 and 2011, there is no I.D. posted at the well. The requirements to meet the Divisions Standards will be to make the well capable of commercial production within thirty days, or plugging is required within ninety days. Failure to comply may result in Forfeiture of Bond. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1084447684 | US-OH-101914 | 2004-05-13 | Well shall be plugged | |
2132642035 | US-OH-121867 | 2014-04-10 | General Safety | |
2132642035 | US-OH-121868 | 2014-04-10 | Failure to legibly identify well | |
2132642035 | US-OH-121869 | 2014-04-10 | Nonproduction; well shall be plugged or placed in temporary inactive status |
For data sources see[9]