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34-059-23315

Well Details

Well ID: 34-059-23315
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Country: United States
State: Ohio
County: Guernsey
Municipality: Londonderry Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: H. LAKE/C. SHARP
License Status: Final Restoration
License Date: 2011-08-05
Spud Date: 1982-07-22
Spud Drilling Contractor: [[JL COATS [COATS-GOFF]]]
Final Drill Date: 1982-07-28
Well Total Depth: 6097.00 ft
Configuration: Vertical
Latitude: 40.140000
Longitude: -81.300000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1982-04-29 Issued Date 4/29/82 Expired Date 11/15/82 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 06097 Proposed Drill Depth 06097
Original Spud 1982-07-22
Completed 1982-07-28
Reached Total Depth 1982-07-28
CO 1982-09-08 2143 CARLESS RESOURCES INC GeoDate 4/29/82
Completion Report Received 1982-09-08
Change of Owner 1998-06-15 Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC
Change of Owner 2009-12-14 Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC
Last Compliance Report 2011-04-07
APP 2011-08-05 Proposed Formations:CLINTON, Issued Date:8/5/2011, Expired Date:8/4/2013 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2011-09-07
Construction Permit Expires 2013-08-04
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 5852 5980 0
5852 5980 0
2006-09-11 5892 5915 18
5892 5915 18
5852 5980 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 70000 FRAC;H2O,70M# SAND,500G ACID

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1986 ZILKHA ENERGY INC 2922.00 13.00 294
1987 ZILKHA ENERGY INC 2542.00 0.00 146
1988 CARLESS RESOURCES INC 2100.00 0.00 336
1989 CARLESS RESOURCES INC 2032.00 0.00 350
1990 CARLESS RESOURCES INC 2511.00 0.00 365
1991 CARLESS RESOURCES INC 2242.00 0.00 365
1992 CARLESS RESOURCES INC 1776.00 0.00 365
1993 CARLESS RESOURCES INC 1825.00 0.00 365
1994 CARLESS RESOURCES INC 1914.00 0.00 365
1995 CARLESS RESOURCES INC 1795.00 0.00 365
1996 CARLESS RESOURCES INC 1174.00 0.00 365
1997 CARLESS RESOURCES INC 920.00 0.00 365
1998 EXCO - NORTH COAST ENERGY INC 1021.00 95.00 365
1999 EXCO - NORTH COAST ENERGY INC 728.00 0.00 365
2000 EXCO - NORTH COAST ENERGY INC 689.00 0.00 365
2001 EXCO - NORTH COAST ENERGY INC 674.00 0.00 365
2002 EXCO - NORTH COAST ENERGY INC 680.00 0.00 365
2003 EXCO - NORTH COAST ENERGY INC 603.00 0.00 365
2004 EXCO - NORTH COAST ENERGY INC 523.00 0.00 365
2005 EXCO - NORTH COAST ENERGY INC 520.00 0.00 365
2006 EXCO - NORTH COAST ENERGY INC 65.00 38.00 365
2007 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2008 EXCO - NORTH COAST ENERGY INC 0.00 0.00 366
2009 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1986 ZILKHA ENERGY INC Brine 140 294
1987 ZILKHA ENERGY INC Brine 147 146
1988 CARLESS RESOURCES INC Brine 61 336
1989 CARLESS RESOURCES INC Brine 157 350
1990 CARLESS RESOURCES INC Brine 60 365
1991 CARLESS RESOURCES INC Brine 78 365
1992 CARLESS RESOURCES INC Brine 124 365
1993 CARLESS RESOURCES INC Brine 62 365
1994 CARLESS RESOURCES INC Brine 123 365
1995 CARLESS RESOURCES INC Brine 62 365
1996 CARLESS RESOURCES INC Brine 62 365
1997 CARLESS RESOURCES INC Brine 0 365
1998 EXCO - NORTH COAST ENERGY INC Brine 65 365
1999 EXCO - NORTH COAST ENERGY INC Brine 365
2000 EXCO - NORTH COAST ENERGY INC Brine 46 365
2001 EXCO - NORTH COAST ENERGY INC Brine 62 365
2002 EXCO - NORTH COAST ENERGY INC Brine 0 365
2003 EXCO - NORTH COAST ENERGY INC Brine 132 365
2004 EXCO - NORTH COAST ENERGY INC Brine 0 365
2005 EXCO - NORTH COAST ENERGY INC Brine 0 365
2006 EXCO - NORTH COAST ENERGY INC Brine 90 365
2007 EXCO - NORTH COAST ENERGY INC Brine 0 0
2008 EXCO - NORTH COAST ENERGY INC Brine 0 366
2009 EXCO - NORTH COAST ENERGY INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1630206087 2004-8-27 0:00: PW No Violations
-2046125879 2011-9-1 0:00:0 PB No Violations
-439117089 2012-2-16 0:00: FR No Violations
0417459515 2003-10-22 Production Wells No Violations STATUS CHECK
0439117089 2012-02-16 Final Restoration No Violations Well site meets 1509.072 ORC.
0748255291 2008-09-29 Production Wells No Violations WELL IS IN PRODUCTION
0890944883 2009-09-09 Annular Disposal No Violations A.D. not hooked up well is shut in at present time,well is equipped with 1-210 bbl tank and 8 surface casing and 4.5 production casing and 1.5 tubing all valves at wellhead were shut on the day of my inspection will call company and discuss future plans for said well .
1300395514 2011-03-17 Production Wells Violations Noted Upon receiving complaint from land owner Terry Lake of idle well on property, inspection revealed that well has been idle since 2007 and all valves at well were shut on the day of my inspection.

Well is equipped with 8 surface casing and 4.5 production casing and 1.5 tubing and 1-210 bbl tank that appears that heater tube is leaking slightly. Plug or Produce well or file for temporary inactive status. Failure to comply may result in bond forfeiture.

1307787700 2011-06-10 Production Wells No Violations Inspection revealed that there has been no change in status of well it still remains idle and there is a slight sulfur odor detected at wellhead.
1308341137 2011-06-17 Production Wells No Violations Inspection revealed that there has been no change in status of well it still remains idle, landowner Ken Lake called and inquired about status of compliance notice told him it was on owner list to possibly repair well or plug said well.
1315435299 2011-09-07 Production Wells No Violations Well has been plugged resolving previous Compliance Notice issued 3/17/2011.
1627837208 2006-01-12 Production Wells No Violations STATUS CHECK
1630206087 2004-08-27 Production Wells No Violations STATUS CHECK. LAT/LONG ALREADY FNTERED
2046125879 2011-09-01 Plug / Plug Back No Violations Inspection revealed that Chipco LLC moved in on site to prepare to plug said well they load hole and removed tubing and they will perforate casing tomorrow 200 below Big Lime top and then run tubing back to bottom and pack off wellhead and be ready to set bottom hole and lime plug 9/6/2011.
417459515 2003-10-22 0:00 PW No Violations
748255291 2008-9-29 0:00: PW No Violations
890944883 2009-9-9 0:00:0 AD No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1300395514 US-OH-108451 2011-03-17 General Safety
1300395514 US-OH-108452 2011-03-17 Nonproduction; well shall be plugged or placed in temporary inactive status
1300395514 US-OH-108453 2011-03-17 Defective casing, leaking well

For data sources see[9]

References