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Well ID: 34-059-23331 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Londonderry Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: TOLAND M | |
License Status: Final Restoration | |
License Date: 2016-05-11 | |
Spud Date: 1982-07-29 | |
Spud Drilling Contractor: J E B DRLG | |
Final Drill Date: 1982-08-05 | |
Well Total Depth: 5950.00 ft | |
Configuration: Vertical | |
Latitude: 40.150000 | |
Longitude: -81.270000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1982-05-19 | 2143 CARLESS RESOURCES INC GeoDate 5/19/82 |
Oil and Gas | 1982-05-19 | Issued Date 5/19/82 Expired Date 11/15/82 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05950 Proposed Drill Depth 05950 |
Original Spud | 1982-07-30 | LOG TYPE=( GAS DETECTION STRATALOG ) IS NOT IN THERE |
Completed | 1982-08-05 | LOG TYPE=( GAS DETECTION STRATALOG ) IS NOT IN THERE |
Reached Total Depth | 1982-08-05 | LOG TYPE=( GAS DETECTION STRATALOG ) IS NOT IN THERE |
Completion Report Received | 1982-10-01 | LOG TYPE=( GAS DETECTION STRATALOG ) IS NOT IN THERE |
Change of Owner | 1998-06-15 | Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2016-05-11 | Proposed Formations:CLINTON, Issued Date:5/11/2016, Expired Date:5/11/2018 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2016-05-20 | LOG TYPE=( GAS DETECTION STRATALOG ) IS NOT IN THERE |
Record Last Modified | 2017-02-15 | LOG TYPE=( GAS DETECTION STRATALOG ) IS NOT IN THERE |
Construction Permit Expires | 2018-05-11 | LOG TYPE=( GAS DETECTION STRATALOG ) IS NOT IN THERE |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 5714 | 5845 | 0 |
5714 | 5845 | 0 | |
2006-09-11 | 5759 | 5845 | 32 |
5759 | 5845 | 32 | |
5714 | 5845 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 70000 | FRAC;H2O,70M# SAND,500G ACID |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | ZILKHA ENERGY INC | 4898.00 | 0.00 | 270 |
1987 | ZILKHA ENERGY INC | 4153.00 | 0.00 | 149 |
1988 | CARLESS RESOURCES INC | 3398.00 | 0.00 | 332 |
1989 | CARLESS RESOURCES INC | 5768.00 | 0.00 | 350 |
1990 | CARLESS RESOURCES INC | 3582.00 | 0.00 | 365 |
1991 | CARLESS RESOURCES INC | 1135.00 | 0.00 | 365 |
1992 | CARLESS RESOURCES INC | 2464.00 | 0.00 | 365 |
1993 | CARLESS RESOURCES INC | 3069.00 | 0.00 | 365 |
1994 | CARLESS RESOURCES INC | 2201.00 | 0.00 | 365 |
1995 | CARLESS RESOURCES INC | 2630.00 | 0.00 | 365 |
1996 | CARLESS RESOURCES INC | 362.00 | 0.00 | 365 |
1997 | CARLESS RESOURCES INC | 0.00 | 0.00 | 0 |
1998 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 0 |
1999 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 365 |
2000 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 0 |
2001 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 0 |
2002 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 0 |
2003 | EXCO - NORTH COAST ENERGY INC | 3408.00 | 0.00 | 0 |
2004 | EXCO - NORTH COAST ENERGY INC | 4339.00 | 0.00 | 365 |
2005 | EXCO - NORTH COAST ENERGY INC | 2412.00 | 0.00 | 365 |
2006 | EXCO - NORTH COAST ENERGY INC | 2016.00 | 0.00 | 365 |
2007 | EXCO - NORTH COAST ENERGY INC | 1695.00 | 0.00 | 365 |
2008 | EXCO - NORTH COAST ENERGY INC | 1732.00 | 0.00 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | 1241.00 | 0.00 | 365 |
2010 | ENERVEST OPERATING LLC | 1554.00 | 0.00 | 365 |
2011 | ENERVEST OPERATING LLC | 1098.00 | 0.00 | 0 |
2012 | ENERVEST OPERATING LLC | 1475.00 | 0.00 | 366 |
2013 | ENERVEST OPERATING LLC | 1736.00 | 3.00 | 365 |
2014 | ENERVEST OPERATING LLC | 1478.00 | 0.00 | 365 |
2015 | ENERVEST OPERATING LLC | 1172.00 | 5.00 | 342 |
2016 | ENERVEST OPERATING LLC | 485.00 | 0.00 | 140 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1051078278 | 2016-5-12 0:00: | PW | No Violations | 4.00 |
-1066936829 | 2005-10-14 0:00 | PW | No Violations | |
-1692846288 | 2003-7-8 0:00:0 | PW | No Violations | |
-1726367517 | 2012-7-30 0:00: | PW | No Violations | |
-1990961195 | 2016-5-19 0:00: | PB | No Violations | 16.00 |
-2048258817 | 2004-10-4 0:00: | PW | No Violations | |
-247649772 | 2004-5-14 0:00: | PW | No Violations | |
-319405940 | 2003-12-4 0:00: | PW | No Violations | |
-394968570 | 2016-5-16 0:00: | PB | No Violations | 13.00 |
-518715145 | 2016-5-11 0:00: | PW | No Violations | 2.00 |
-77038302 | 2016-5-9 0:00:0 | PW | No Violations | 1.00 |
-892484114 | 2016-11-10 0:00 | FR | No Violations | 1.00 |
0071126948 | 2016-05-18 | Plug / Plug Back | No Violations | On the day of my inspection following up on Compliance Notice- |
0077038302 | 2016-05-09 | Production Wells | No Violations | On the day of my inspection accompanied by ODNR Southeast Regional Supervisor Brent Bear following up on Compliance Notice- 1645786637 and Complaint ID 5314, H2S was detected with a discussion on safe procedures and plugging of the well. Phone conference was held with Enervest Supervisor Tim McConaha discussing the well and a meeting was scheduled for further discussion at the Zanesville Office on 5/10/16. |
0247649772 | 2004-05-14 | Production Wells | No Violations | STATUS CHECK |
0319405940 | 2003-12-04 | Production Wells | No Violations | STATUS CHECK |
0383699567 | 2007-08-09 | Production Wells | No Violations | STATUS CHECK |
0394968570 | 2016-05-16 | Plug / Plug Back | No Violations | On the day of my inspection following up on Compliance Notice-1645786637 and Complaint ID 5314, H2S readings were at 70ppm on the 4.5 inch casing with a safety meeting being held with Enervest Superintendent Tim McConaha, Appalachian Well Surveys, ODNR Inspector Joe Zollars and Chipco LLC employees. AWS tripped inside the 1.5 inch tubing and shot the tubing off at 5746 feet and Chipco pumped a 30 sack 400 foot Class A Clinton cement plug from 5746 feet to 5346 feet and displaced cement with 13.4bbls of brine. Tek Solve arrived on location and setup H2S monitoring and left the site. AWS tripped inside the tubing to 17 feet above the packer and shot the tubing at 4860 feet as they were tripping out of the tubing AWS lost their tools which consisted of a collar locater and 2 sinker bars. Attempts to retrieve and drive to bottom unsuccessful decision was made to shoot tubing again at 4092 feet. Chipco pulled 2 joints of 1.5 inch tubing as AWS tripped back in to perforate the Big Lime but could not drop out of the bottom of the tubing. AWS perforated the tubing with 10 shots from 4034 feet to 4024 feet. AWS tripped out of the tubing and Chipco pumped a 30 sack 500 foot Class A Big Lime plug from 4034 feet to 3534 feet and displaced cement with 9.5bbls of brine and shutting well in. AWS will tag Big Lime plug and re-perforating tomorrow with Chipco setting an additional isolation plug. |
0426639119 | 2016-05-17 | Plug / Plug Back | No Violations | On the day of my inspection following up on Compliance Notice-1645786637 and Complaint ID 5314, H2S readings were at 0ppm on the 4.5 inch casing with a safety meeting being held with Enervest Superintendent Tim McConaha, ODNR Inspector Joe Zollars, Appalachian Well Surveys and Chipco LLC employees. AWS tripped inside the 1.5 inch tubing, sat down at 3280 feet and shot the tubing off at 3275 feet. AWS perforated the 4.5 inch casing with 10 shots from 3215 feet to 3205 feet. Chipco pumped a 60 sack 200 foot Isolation plug in the Ohio Shale from 3215 feet to 3015 feet and displaced cement with 7.5bbls of fresh water. After displacement H2S alarms went off at 100ppm and the well was shut-in for the day with plans to complete tomorrow. |
0518715145 | 2016-05-11 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice-1645786637 and Complaint ID 5314, I met with Chipco representatives and detected H2S was detected. A Meeting was held on hot tapping the well, well control, positioning of the service rig and plugging of the well. |
0587024953 | 2016-05-13 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice-1645786637 and Complaint ID 5314, a safety meeting was held with Enervest Superintendent Tim McConaha and Chipco LLC employees. I witnessed that a second hot tap was performed yesterday on the 4.5 inch casing with the tubing annulus receiving 600 gallons of sulfa-clear. Pressure on the annulus was at 475psi with no H2S present Chipco began treating the well with an additional 10bbls of sulfa-clear and 10ppg brine. Chipco was unable to pump on the annulus so a controlled blowdown was done resulting in spikes of H2S. Chipco pumped the additional 10bbls of sulfa-clear along with 26bbls of 10ppg brine resulting in the well becoming static with no H2S present. Chipco changed out all wellhead valves and tripped inside the 1.5 inch tubing to 5750 feet, tripping out and loading the tubing with 10ppg brine. Plugging commencement will begin on Monday 5/16/16. |
0892484114 | 2016-11-10 | Final Restoration | No Violations | On the day of my inspection I witnessed that the site passed final restoration according to ORC 1509.072B. |
0976391443 | 2003-07-09 | Production Wells | No Violations | PACKER SET @ 4877.05 ON 1.5 TUBING. |
1051078278 | 2016-05-12 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice-1645786637 and Complaint ID 5314 accompanied by ODNR Inspector Joe Zollars, I met with Enervest Services Superintendent, Welder Jim Green and Chipco representatives and a safety meeting was held prior to hot tapping the well. H2S was detected with a fan blowing Jim Green successfully tapped the 4.5 inch casing valve nipple. A 1 inch valve was installed with H2S present and pressures of 475psi on the casing. Appalachian Well Service will be onsite later today to treat the well with Sulfa Clear and Chipco Rig #6 to be rigged up after well is treated. Tech Solv will be onsite Monday at 7:00am for H2S monitoring prior to plugging commencement and throughout with road closure from 9:00am to 2:00pm. |
1052134167 | 2003-05-02 | Production Wells | No Violations | FLARE ESTABLISHED TO BURN OFF H2S. 1350# PRESSURE NOTED ON CSG. |
1066936829 | 2005-10-14 | Production Wells | No Violations | STATUS CHECK |
1194031506 | 2009-09-08 | Production Wells | No Violations | Inspection revealed that well is equipped with 1-210 bbl tank within dike area and 8 surface casing and 4.5 production casing and 1.5 tubing(rabbit well) ,according to well tender casing has a hole in it and tubing is set on a packer. |
1270152427 | 2010-03-29 | Production Wells | No Violations | Inspection revealed that well is equipped with 8 surface casing and 4.5 production casing and 1.5 tubing set on packer due to hole in casing and there is 1-210 bbl tank and separator within dike area. |
1463665841 | 2016-05-18 | Plug / Plug Back | No Violations | The purpose of my inspection today is to assist ODNR Inspector Doug Bennet in the plugging of this well owned by Enervest. Three plugs have been set on days prior to my arrival at 11 a.m. Doug Bennet has witnessed the whole plug job and is the main inspector on site. This well contains high concentrations of H2S. During my inspection TekSolv had their TekNet gas- |
1464005706 | 2016-05-23 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed that the service rig has moved off and all contamination has been remediated. The top cement plug was checked and found to be at surface with 0ppm H2S present and all levels reading normal. |
1520776819 | 2005-04-26 | Production Wells | No Violations | TUBING SET ON PACKER, WELL BACK IN PRODUCTION. DIKE AREA RE-WORKED. |
1565392317 | 2003-07-02 | Production Wells | No Violations | COMPANY IS FLARING WELL DOWN TODAY TO ATTEMPT TO SET PACKER ON 1.5 TUBING TO TRY TO PRODUCE WELL AND GET AWAY FROM H2S PROBLEM.STRONG FLARE ESTABLISHED |
1616120752 | 2008-02-07 | Production Wells | No Violations | H2S WELL. BAYLON REPLACED. |
1645786637 | 2016-04-26 | Production Wells | Violations Noted | On the day of my inspection accompanied by ODNR Inspector Joe Zollars following up on Complaint ID 5311, I witnessed that the H2S was present in the air at the entry of the access road along with a sign stating Danger H2S. Flags were placed to determine wind direction as Inspector Zollars and I approached the well from the west. I found the well equipped with 8.625 inch casing; 4.5 inch casing, 1.5 inch tubing and a plunger lift system with valves open on the tubing and valves closed on the casing with deterioration present on the casing, valves and flowline. The production equipment included a 210bbl tank, a horizontal separator, a logically controlled motor valve, a 2 inch sales meter with a .875 inch orifice and a chart recorder all within an earthen dike. Identification was present and production records were current. I placed call to Enervest and spoke with Tim McConaha and stated my findings. Mr. McConaha stated that he would treat the well with sulfur clear and come up with a plan of action to address the well. The well owner/operator shall submit a written plugging schedule to Doug Bennett at 5880 Memory Road Zanesville, Ohio 43701-9553 within 15 days, per OAC 1501:9-11-05(B), and plug the well within 30 days. The well owner/operator will be notified if the plugging schedule is approved or denied. |
1692846288 | 2003-07-08 | Production Wells | No Violations | STATUS CHECK. RUNNING TUBING OUT OF WELL, TALLY PIPE , TO SET PACKER ON TUBING, TRY TO PRODUCE WELL ON PACKER. |
1726367517 | 2012-07-30 | Production Wells | No Violations | On the day of my inspection I found the well to be capable of production, all the valves were open and the chart was showing current production, there is (1) two hundred ten barrel production tank/ seperator/ drip and I.D. posted. |
1940082148 | 2016-06-08 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed the grade has been restored with the 210bbl tank remaining onsite and all other equipment removed. |
1952227319 | 2005-05-10 | Production Wells | No Violations | STATUS CHECK. PACKER SET ON TUBING 2002. H2S PROBLEMS PRIOR TO SETTING PACKER.STILL A GOOD PRODUCING WELL. |
1990961195 | 2016-05-19 | Plug / Plug Back | No Violations | On the day of my inspection following up on Compliance Notice-1645786637 and Complaint ID 5314 accompanied by Southeast Regional Supervisor Brent Bear, H2S readings were at 0ppm on the 4.5 inch casing with a safety meeting being held with Enervest Drilling Supervisor Joe Wade, Appalachian Well Surveys and Chipco LLC employees. Chipco inspected the wellhead and checked pressure on the casing revealing 25psi and then performed a controlled release to the half round spiking the H2S readings to >100ppm. Chipco pumped 22bbls of water clearing the perforations at 1332 feet and reducing the H2S levels to 0ppm. Volume was calculated at 160bbls to the fill the annulus along with 4.5 inch casing and a total of 70bbls being pumped since the last plug set the job was shut down waiting on water. ODNR Southeast Regional Supervisor Brent Bear and I made a sweep of the surrounding shale pads and conventional sites revealing normal levels of H2S with a strong odor on London Road. Upon arrival of the water Chipco pumped an additional 45bbls which filled the annulus and the casing. AWS perforate the 4.5 inch casing at 500 feet which is 58 feet below the cement that was pumped down the annulus of the casing in 1984. AWS tripped out of the hole and the well released trapped gas from the annulus spiking the H2S readings at the half round >100ppm. Levels returned to normal with Chipco tripping in 2.375 inch tubing and a packer to a depth of 1134 feet and then circulating 45bbls of water to the half round. Chipco pumped a 60 sack 200 foot Class A bottom of the surface casing plug through the perforations from 1334 feet to 1134 feet and the cement was displaced with 4bbls of water. Chipco then released the packer and tripped out of the well to 750 feet and circulating 15bbls of fresh water. Chipco tripped out of the hole revealing that the packer along with 236 feet of 2.375 inch tubing was lost in the well. Chipco shut-in the 4.5 inch casing with completion of plugging planned for tomorrow |
1996279410 | 2016-05-20 | Plug / Plug Back | No Violations | On the day of my inspection following up on Compliance Notice-1645786637 and Complaint ID 5314, pressure readings were at 0psi and H2S readings were at 0ppm on the 4.5 inch casing. A safety meeting was held with Enervest Drilling Supervisor Joe Wade and Chipco LLC employees. Chipco rigged up their 4 inch tools, tripped in the hole and tagged the tubing that was lost at 905 feet. Chipco tripped out of the hole and tripped 2.375 inch tubing back in to a depth of 750 feet. Chipco pumped a 57 sack 750 foot Class A cement plug inside the 4.5 inch casing from 750 feet to surface circulating cement to surface. Chipco tripped out of the hole with the 2.375 inch tubing, cement dropped to 100 feet and was topped off to surface with an additional 8 sacks of cement. The casing will be left open until Monday for monitoring with Compliance Notice-1645786637 and Complaint ID 5314 now resolved. |
2048258817 | 2004-10-04 | Production Wells | No Violations | STATUS CHECK, DIKE RE-WORKED. |
2111482681 | 2006-01-12 | Production Wells | No Violations | STATUS CHECK |
383699567 | 2007-8-9 0:00:0 | PW | No Violations | |
426639119 | 2016-5-17 0:00: | PB | No Violations | 9.00 |
587024953 | 2016-5-13 0:00: | PW | No Violations | 4.50 |
71126948 | 2016-5-18 0:00: | PB | No Violations | 16.00 |
976391443 | 2003-7-9 0:00:0 | PW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1645786637 | US-OH-116219 | 2016-06-06 | General Safety | |
1645786637 | US-OH-116220 | 2016-06-06 | Defective casing, leaking well |
For data sources see[9]