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34-059-24193

Well Details

Well ID: 34-059-24193
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Country: United States
State: Ohio
County: Guernsey
Municipality: Wheeling Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: RHDK INVESTMENTS EV
License Status: Final Restoration
License Date: 2011-09-28
Spud Date: 2012-01-13
Spud Drilling Contractor: BOWMAN DRILLING
Final Drill Date: 2012-01-13
Well Total Depth: 2811.00 ft
Configuration: Vertical
Latitude: 40.150000
Longitude: -81.630000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2011-09-26 Proposed Formations:BEREA THRU TOP OF ONONDAGA, Issued Date:9/26/2011, Expired Date:9/25/2013 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:ESPW
APP 2011-09-28 Proposed Formations:BEREA THRU OHIO SHALE, CLINTON, Issued Date:9/28/2011, Expired Date:9/27/2013 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Correction to Well 2011-10-28 CHANGE IN PROPOSED TOTAL DEPTH, PROPOSED GEOLOGICAL FORMATION & CASING PROGRAM.
Reached Total Depth 2012-01-13
Plugged/Abandoned 2012-03-29
Completion Report Received 2012-05-17
Construction Permit Expires 2013-09-27
Record Last Modified 2014-10-08

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-49160842 2012-1-18 0:00: DD No Violations
-757041975 2013-6-27 0:00: FR No Violations 1.00
0049160842 2012-01-18 Drill / Deepen / Reopen No Violations Total depth has been reached at 2805. The operator loaded hole with brine while waiting on the logging truck.
0757041975 2013-06-27 Final Restoration No Violations Everything passed according to 1509.072B.
1333033708 2012-03-29 Plug / Plug Back No Violations On day of inspection well was being plugged by Chipco and cemented by Formation cementing.1st plug set @2770-2520ran 39 sks in6.25 open hole. Thru 1.5tubing.2nd plug set@1092-916.Ran 28 sks cement at 6.4 lb/gal.3rd plug set @694-494.Ran 32 sks at 6.4 lb/gal.4th plug set@200-0.Ran 42 sks cement. All cement was 2%gel .Cotton hulls were lost circulating material. Total of 141 sks .

For data sources see[3]

References